ML19253A512

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Submits TMI Daily Rept Re Reactor & Plant Status,Radwaste & Health Physics & Environ Measurements
ML19253A512
Person / Time
Site: Crane Constellation icon.png
Issue date: 05/17/1979
From: Vollmer R
Office of Nuclear Reactor Regulation
To: Stello V
Office of Nuclear Reactor Regulation
References
NUDOCS 7909100188
Download: ML19253A512 (20)


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UNITED STATES

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3T NUCLEAR REGULATORY COMMISSION

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WASHINGTON, D. C. 20s55 3, b

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.s*p May 17, 1979 o * *....

MEMORANDUM FOR:

Victor Stello FRCM:

Richard H. Vollmer t

SUBJECT:

Dil DAILY RE?O3T e

A.

Reactor and Plant Status 1.

The Presidential Commission visited the site this afternoon.

NRC personnel were not directly involved.

2.

Technical Progress Meeting - see Attachment for agenda and notes.

3 system Parareters and Core."ap - pressurizer pressure approxi-ately h59 psi with buoble drawn.

Cooldown suspended temporarily pending further developmert of plans and procedures.

L.

As suspected, containment level described in 5/16/79 eport was incorrect, due to error in measurement of location o#

pressure gauge, actual level is 238.5', 2' less than origi ally reported, which represents no i-ediate th eat to any equipment.

O p e ra t i on of JH-V2 on hold pending furt'er evaluation.

5.

JHR A loop hydro test on hold due to hig" area radiation 'ece's caused by :H-76 opening for containrer.t level readings.

Resolution under consideration.

6.

RCS sanale expectec 5/13/79 3.

Environ ental u aasura ents 1.

No radiation level cSove oackground sas detected bv JCE aerial surveys.

No reports were received from other agencies.

7 9 09100 /s)f' hk G

J

'/ictor Stello =

2.

A milk sample detected no 1-131 above a MOL of 10 picocuries per liter.

3.

Air samples at locat ions a rounc the s i te ranced f rom

?

3.4 x 10-I3 to 6.6 x 10-12, 3

J V-

/

Richard H. Vollmer Attachments cc:

2.

Eisenhut C.

Smith, II 1 Vollmer G. bainas J.

Collins J. Crutch #ield

3. Grimes Jaily Peport File r

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RELEASES 1100 (5/15/79) 1100 (5/16/79) 1100 (5/17/79)

-13 748 6.10 x 10-9 3.4 x 10-9 1.49 x 10

-10 7

219 1.12 x 10-11 1.4 x 10-10 4.4 x 10

-9

-9 j

Inlet 2.40 x 10 3.72 x 10-10 1.6 x 10

-1~?

Train #1*

Not Running 2.71 x 10-12 6.6 x 10

-l~'

Train #2*

1.72 x 10-11 4 1.79 x 10-13 8.44 x,10

-12

-12 Train #3*

9.65 x 10 6.90 x 10 12 3.8 x 10

-1 Train #4h 9.65 x 10-12 3.37 x 10-12 3.66 x 10 REACTOR COOLANT SYSTEM PROFILE PLANT STATUS 1100 (5/15/79) 1100 (5/16/79) 1100 (5/17/79)

A B

A 3

A 3

Th 167.5 168.5 166.9 168.3 169.5 170.6 Tc 155.8 99.1 155.9 99.1 157.7 114.5 T

11.7 69.4 11.0 69.2 11.8 56.1 Tstm 153.0 121.6 153.2 122.4 155.7 130.1 PZR LEVEL Cal.

Solid Solid 373 DVM LT-3 386,/

~0 R.C. Press.

614 446 S/G Level 415" 96%

415" 95%

420" 967.

Turb. B/P 84%

Closed 69 P.

Closed 60%

Closed I.C.T.

High 303.4 303.9 304.37 Avg.

191.3 Not Available 194.16 M.U.

Tenp.

124 127 123 L

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5/17/79 4

TECIETICAL WORKING GROUP 1300 5/17/79 l.

Agenda, 1300, 5/17/79 Technical Working Group 2.

Radioactive Releases and RCS Profile 3.

Top Priorities List 4.

Action Items from 1300, 5/16/79, Technical Working Group 5.

Task Lists U.

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AGENDA 5/17/79 TECHNICAL WORKING GRCUP 1300 5/17/79 1.

Radioactive Releases

~

a.

748, 219, Auxiliary Building Fans b.

Vent Header and Drair. Trunk c.

Dome Radiation Monitor i

d.

Measurement of Radiatian Level Inside Containment j

r 2.

Plant Status 7

a.

RCS Profile o A7A-b.

Plant Operations Schedule Q SP -la b Bypass Valve Adjustment Toward 64%

C# *

/,ff Ab.[lco de-oh o A,

IfJ fN6 y

DHP

'A' Test Replacement of 'B' train FHB charcoal filters w w.%, c ; 5 2

Obtain RCS Sample - 0900 5/13 DiowM bu NV -

Sanple Bleed Tank 'A' - Analysis should i'iclude Boron 7"*

Concentration i' N 3.

Containment Sumo Level j

a.

DHV-6B - Results of Containment Lavel Determination Shbb I

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b.

DHV-2 Operation g%

a g-4P m a u,od. ~to use Not 4.

Analysis Reevaluation of exist 'ng rec ^==end tion to) draw a bubble vs.

solid a.

f }.

seeg aperatioa C/01 c, a

b.

Procedure for verification of Solid PZR durine solid operations at 300 psi c.

Reductionto 300 psig - increase in loss of pressure protection?

d.

Use of Long-tern Cooling System

'3' OTSG 5.

Construction Status Esti=at ed Comoletion a.

Tank Farm M

w 5/2 b.

OTSC 'B' Long Term Cooling 7<w~

5/1 c.

EPICOR (CAP-GU'i II) 5/ 23 d.

RCS Pressure /Volu e Control T mnev e 5/1

}

for testing TI e sh c o d%

  • N

8% M

%.cl <# *\\,. M-Auxiliary Diesel Generator Auto Start %..g.

5/17 c.

f.

Alternate Decay Heat Removal System tie-in; 6/1

. D, 0 adb, of

.g e

5/17/79 TOP PRIOR 1 TIES Development of plan for management of radioactivity in A-1 Auxiliary and Containment Buildings.

e Identify and isolate sources of iodine leakage.

A-1 e

Complete tank farm in Unit 2 spent fuel pool.

A-1 Completion of EPICOR (CAP-GUi II) System A-2 Develop =ent of plan for treatment of Auxiliary Building B-1 liquid waste Complete

'B' OTSG cooling and =odific.atio G on g-t e rs)

C-1 Development of alternate systua f0c pressure /vor.tra C-1 control system.

Complete ext.ernal valve pit fc c ADHR System.

C-2 CATECORY A

Control (i.e., containment) of radioactivity in Auxiliary and Containment Buildings B

Recovery of Auxiliary Building to near normal operations C

Place the plant in a cold condition suitable for depressurization with long-tern pressura/

volume control

,t>

l

5/17/79 ACTION ITEMS TECHNICAL WORKING CROUP 1300 5/16/79 Item Action 1.

Determine proper hydro test pressure for UG-6.

Burns & Roe 2.

Evaluate building and river temperatute affects on Wilson /

maintaining negative pressure in the Reactor Building.

B&W 3.

Insure that adequate verification of continued solid Wilson operation is placed in the current procedure for solid RCS operation.

4.

Evaluate the best nethod for cooldoun of pressuriscr Wilson /

BEW a.

Venting steam frca bubble operations b.

Level cvele from 330 - 370" a 100 - 370" J l b' e

Page 1 of 2 1300 5/17/79 PLANT OPEPATION STAFF 4

Expected Task Task Ducriotion Priority Comoletion Status Coord.

l 1.

Obtain RCS sample (Primary C-1 5/18 Hetrict.

letdown).

=

2.

Obtain MEC approval (Tie-in C-1 Need ECM's Kunder/

I approval only).

170 R1 Faulkner /

264 R0 and 1, Seelluger 272 Rl.

3.

SSRU pump, "C" repair.

C-1 Comp. by 5/20.

4.

Decay Heat System.

C-1 Cycle DHV-6 Cycled 5/15.

Toole after hydro.

3.

Remove water from "B" Fuel Pool.

B-1 Not started Kunder 6.

Isolate Unit !!1 and 32 sample Need new sample Limroth/

stations.

sink.

McGoey 7.

Training on Diesel.

In progress.

Troffer/

Kunder/

Toole 3.

Training on Decay Heat.

C-1 In progress.

Westinghouse Troffer/

will provide Kinder /

training plan.

Toole 9.

Sample AB/FHB charcoal beds.

B-1 AB "A"

& "B" Kunder/

5/19.

Retrick FHB "A" 5/23.

10.

Gr'v diesel.

C-1 5/17 Both cocplete Toole except for Uhite diesel.

5/17 auto start 5/17.

Toole 11.

Move filters out of Aux. Bldg.

3-1 In progress.

12.

Repair DU-P-4A.

Working 4A.

6 0*.' comple te.

13.

Repair SW-P-13.

Need new Regn. No.

Shovlin shaft.

201-1720.

14 CO-P-1B repair.

In progress.

Shovljn 13.

Install self-cooling on Toole/

condensate pump 1A.

Gunn

Page 2 of a 1300 5/17/79 PLANT OPERATION STAFF Expected I

Task Task Descriotion Priorit's Comoletion Status coord.

16.

Rebuild breaker for Cap-Gun.

Need 51 relay Shovlin and CT.

e 17.

Maintain turbine sump empty.

Until comple-Kunder/

tion of "B" Frederick OTSG flush.

=

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1300 5/17/79 PLANT 510DIFICAT10NS Expected Task Tar.k Description Priority Co nietion Status Coord.

WG-1 Install AB/FHB Filter System.

A-1 Complete by System opera-Shubert 5/15.

tional 5/10; complete 5/15.

WG-2 Decon. wcter in AB using EPICCR A-1 Turn over Lacy /

(L-1) ion exchange process.

5/23.

Fricke WG-6 Install storage vessels in Fuel A-1 Turn over Gibson (L-2)

Pool "A".

by 5/23.

WG-ll Water Chemistry Lab for use A-1 System com-Tcile/

with CAP-GUN (WC-2).

plete by 5/17.

Rao WC-12 Ventilation filtration system A-1 Turn over Shubert for decay heat pits.

5/26.

TS-13 Install elec. heaters on Aux.

A-2 On hold.

Shubert Bldg. intake ducts.

TS-3C Develop complete package for C-1 Turn over Jordan /

lon;;-term cooling OTSG "B".

5/17.

Lanza Estimated com-Miller /

TS-6B F;S pressure control system.

C-1 Schedule

~

pletion 5/25.

Lilly being revised.

TS-11 Aux. diesel generators.

C-1 Testing.

Complete Gagliardo except for auto start 5/17.

TS-14 Shielding for decay heat pump.

C-2 Turn over Lieberman 5/23.

NOTE:

Plant !!cdification Prelininary Schedule for Westinghouse ADHR System indicates 6/21/79 completier. date.

i 4

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1300 5/17/79 TECH:iICAL SUP' PORT E::pected Task Task Description Priority Comoletion Status

' Coord.

L5.?

Tech. Spec. and Surveillance 1

?

Active:

NRC L. W. Hardin and Bases Changes to those interactions left deletions, additions.

under negotia-

tion, i

LS.3 Initial Reporting of Event.

1 5/15 to NRC.

Active.

R. A.

Lengel lCobean IM.23 Reactor Coolant System 1

5/23 Active.

P/V Control.

TM.30 Determine what 30P loads 1

Continuing.

Draft criteria Capodanno/

need backup electrical power.

document issued Langenbach 4/24.

TM.35 Long-tern plant instrumentation 1

On hold.

Criteria docu.

Capodanno/

requirements (criteria).

being revised.

Langenbach AA 61.

Update S!R.

1

?

Draft received.

d&W AA 66.

D.

How to caintain primary 1

?

Active.

GPUSC/MPR boron conc.

AA 69.

Define all plant mods needed 1

?

Croneberger for long-tern operations.

AA 30.

Analytical and Tech. Planning 1

?

Continuing.

J. A. Daniel Support for updated procedures (EP-32, etc.).

AA 33.

Identify critical valves and 1

?

Active.

Pre-R.

Long instruments which may be lin. list damaged by high su=p levels.

available.

AA S4 Identify flow paths from the 1

B&R investi-Active.

contain=ect sump.

gating.

AA 37.

Solid Pressurizer Analysis.

1

?

Active.

J. Moore AA 96.

Boren concentration in R3 sump 1

?

Active.

J. Moore 4/30 through 5/15.

TM.37 Installation of cartridge-type 1

ECM issued.

Revising Capodanno/

Demineralizer for clean-up of design.

Langenbach S.G.

"3" secondary side.

AA 1.

Letdown Flow Analysis 1

Continuing.

Active.

Met-Ed (continuing curve development).

Control Roorc AA 71.

Determine requirements to 1

?

?

perform sample analysis locally.

.\\n~

1300 5/17/79 WESTI:iCHOUSE Expected Task Task Descrintion Priority Comnletion Status Coord.

TS-15 ADHR Installation C-1 6/21/79 See sub-F. J. Serage (II.B) d ivis ions.

ECM 109: ADRR piping and C-1 5/18 F.J.Serah cabling ECM 119:

Excav. west side C-1 Complete.

of FHB ECM 120:

0 1 nce ek-up C-1 Complete.

2 training ECM 122: ADER skid off load C-1 R. Clark and tenp. shelter ECM 136:

Elect. control C-1 3/25 Exp. delivery Scrago/

trailer 5/19 Imagawa ECM 143:

ADHR skid assembly C-1 5/25 R. Clark ECM 16'.

Hydraulic valve C-1 Complete.

operator EC'1 132 :

F.1 Penetration C-1 5/31

~

J. W. Meyer EC:t 199: Valve pit C-1 6/13 Serago/

Meyer ECM 212:

Component cooling C-1 R. Clark skid ECM 226: Wiring ADHR skid C-1 3/25 R. Clark l

r

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Page 1 of 7 1300 5/17/79 WASTE MANAGEME::T GROUP Enpected Task Task Description Priority Cocoletion Status Coord.

L-1 Design, installation, and B-1 5/23 Remaining Snider /

operation of EPICOR for items are Ga rman/

Unit 2.

installation McCutcheon/cI of CAP-GUN kWeller/

equipment and

': Collins coating of the floor.

L-2 Design, intallation, and B-1 5/1 75% comp.

Reinmann/

operation of emergency surge piping in FH3.

Snider /

tanks (tank farn) in Unit 2 iWeller/

comp. welds "A"

Fuel Fool.

A 4 Collins in A3 pipe, FE pipe.

Prefab. pipe ready for installation in AB.

"B" train pour planned for 5/7; "A"

train pour complete.

~

'75% concrete slabs placed atop fuel pool.

L-10 Pursue activities on processing A-1 In progress.

Gar =an/

Unit 1 water through CAP-GUN to Geller both provide support to insure ava lable freeboard for Unit 2 and to develop resin formula-tions for Unit 2 water.

L-14 Evaluate waste gas vent nader A1.

Yorking per McConnell/

leakage prob:. ems and tetonmend J.

Seelinger's Arthur /

fixes depend _ng on results.

waste gas plan

  • Bland of 4/17/79.

MRC cantact

' /

i 1

Pap,., 2 of 7 1300 5/17/79 g 4,. c '1 1,.

....,.,,p,u.-..-

u u, g,.,,,

w suum..

..t 0c Er.pecteu_ _ _ _ _

Tash Ta e,'c Daccriution Priorit' Cc-iletion Status Coord.

L-36 Investigate the effects which C-1 In progress.

McCocy/

the operations associated Ross/

<eith reactor plant long-tera

  • Co llinsi, cooldoun ulll have on discharge

{

to the u<tste systems.

Related

-2, to L-o.

L-42 Development reco.r.,calations and C-1 McGoey[

,cocedure for draining and Ross/

c'2cpositica of RCCT. rater to

  • Collins support plant needs to nahe up
Lth degnssed dectin, uater.

L-4!.

.=aluate synte., designa rith E-1 Report being I; raft /

Technical functions and U to prepared; nueller assess pos:,ible interference delayed by problems frca standpoint of higher priority locations, operations, tasks.

.-.intenance, etc.

L

!< 7 l Resol.csar.plelabrquir272nts E-l Meeting held I;raf t j

,c sus capabilitics to 5/1/79;

\\ support E?ICCit I and II opera-resolution tions.

.in progress.

G-1 Install A3/F!!O of f-gan filter A-1 Phases I, II, Montgoa-

.ysten to b.:k-up plant systen and III design Itschne complete.

SCollins Systen descrip-tion and start-up procedures are c omplete.

Four M) fans are operable, l

3 or 4 are run-l ning.

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Page 3 of 7 1300 5/17/79 UASTE :Ud!ACFl!E:<T CROUP.

E:cpec ted Iask Task Descriotion Priority Concletion Status Coord.

G-5 Change out AB/FHB HVAC vent A-1 "A"

& "B" train McConnell filter train charcoal bed.

of the AB fil-Eduards/.

ters and "A"

  • Weller train of FHB j

filters removed and replaced, units back in service. FHB "B"

train in change-out scheduled for 5/17.

Deluge syste=3 secured on all runeued filter trains.

Spent filter tray rc= oval to storage com-pleted.

G-31 Determine air flow paths in A-1 Operating matri:

Nawaz/

AS/FEB.

developed and Itschner/

'available.

Robison/

  • Weller G-32 Determine that there are no A-1 E::anination of Nawaz/

unidentified air flow paths.

plant status /

Itschner/

configuration Robison/

under'ay.

':Bar rett First cust.

revicu complete 20 contact

}

l j

L I

Page 4 of 7 13 00 5/17/79 UASTE MAN'GEME::T GP.OCP.

E::p ec ted Task.

Tan't Deccriotion Priori 17 Caml e t ion Stat,ts Coord.

C-33 D welop plan for ventilation B-1 Meed identified Itschne systen operation based on fan /

to ~ t up a

  • Stoddat filter train status and on plan.

Control /

door openings and other plant advise on local operation evaluations.

and systen ven-e tilation p rac t ic e. '.,

C-40 Criteria for and con. trol tas.cs A-1 20 " Red Devil" SCollins resulting in the evolution of type local contacinates that could poison filtration

'c:n: coal filters.

systens on order to contro:

trelding faces.

L-3 Dcternination of leahage p2ths 2

Plant staff Kraft /

c cf flott rates in Unit 2 Aur..

f o llo t:ing.

Arthur /

' idi. and FHE and repair

  • Ct:alina of laaks tihere poss ibic.

Plant h~,

leaha;c ID and Status E0ard in Unit 2 Control Room.

Pursuc P l c o. : activities associated this.

L-12

.y level solid *.:aste disposal B-2 In progress.

Pastor /

inv:stigation.

Edt:ards

  • Weller/
  • Collins L-2r; Perforn assessnent of the value A-2 Price proposal Kraft /

r.d need for a closed circuit being accessed Lutz/

ll innitor to provide remote versus decon.

  • Stoddar ind icator of rach:2ste panel schedule of
tt Au
- Eldg.

i L-27

_.;iop senpling plan to access B-2 Identified 4 Passell 4

,.,.:a u t e for transuranic sampics, agreed Uillian

_ m ant.

I n:,ur e that II:t-Ed on 3.

Agreement,

  • Collins Cp-coardinate canple require-reached on using,

_nts ith O?'.:L to insure previously takan

,I - __sfactory cnal',:is re nlic.

l cn".91cs f rota i

I su: :a and bleed tanks; nM i Lio nal 6,

namplen to se i

I

Pa t,e i ot 7 1300 5/17/79 UASTE ILiM!E L_ :.::T CEOUP E::pected Task TasL D0scrintion Priorirl Cc olet_ ion Status Coord.

L-29 Investigate reported uater B-2 Uater fro =

Uillice:

collection in the "B" fuel pool Unit 2 const.

AEarrett obtain samples and take plans Sample needed.

for disposition.

Also investi-gate the preoperational condition of the fuel pool from a leahage standpoint.

L-33 Develop a plan for tying in tha E-2 System cr2lteria Reinnant tank fara to EPICOR 2.

seat to 3&R on Snider /

5/1/79.

~47eller/

ACollins L-35 Irvastigate the nea:1 for 3 3-2 Alternate McConnel design and construction task to design Unit 1 Uilliant erect a barrier betueen the side to be EEarrett Unit 1 and Unit 2 Fuel liandling submitted Bldg. to enable Unit 1 opera-4/27/79.

ions uith Unit 2 in processing bde.

L-37 D2celop a plan for removing all B-2 Requires com-McConnel radioactive gases from the pletion of L-14 SCollins systens in the AB c.nd FHC.

G-7 Condenser vacuun pung discharge A-2 filter system.

Filter opera-Robison/

tional.

Inves-Montgomr_

tigating opera-

  • Collins ting criteria.

Uill evaluate DF.

G-30 P.2 actor-Purge Syster t.harcoal A-2 RB purge filter McConnel Filter Sample.

Scheduled week sanple all ready

^ Collins of 5/20 for analysis.

C-33

'.,,sensitia A3 and FEB Eilter A-2 i'r elimina ry Sieg/

miters.

l investigatioa -

LStoddart desensitization ini cr :1 tilt.

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', c o n ".n e t i

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l'a ge 6 ot 7 1300 5/17 /79 UASTE ?Ud: ACE::E:;r GRCC?

E::pected Task Ta s*e Description Priorit?

Co s_T e -ion Status Coord.

G-39 Develop and asaccs back-up gas B-2 S&R has devel-McConne filtration schc=2 to cross-oped a concept.

  • Lee S

connect the Auxiliary Euildina Second esticate e

Elltars to the RB purg,e filters-scheduled shous I

n 14 day +

schedule.

Heiscan Co. has developed drau-ings.

Exposure, schedule cost i

appears too hi;;h.

Con-tingency plan is to open roughing filter mantray if emer-gency vencila-tion of Auxiliary Euilding is needed.

Standard proce-McConnel G-41

(:v a lo p filter run:gement B-2 dures to sample ntrc:c37 charcoal systems in revicu.

G-42 Devclop a proZrr. to assess B-2 Four-part McConnc and nanitor I releasa sources.

approach:

McGoey/

Montgo:

1. ESR to com-3g1:

plete revie" Cline /

of release Pelitt j

candidates.

yolleg l

2. Pursue a trater progran to I

find leak.

3. Pursue an l

nir noni-toring pro-i l

gram with SAI/EPRI to plot I i

levels.

4.

Revieu local I

s ventilation cond i tio n i

J-(

to verify

(

., / (

1 tJ(c din t: L-t

)t 1I. EO ;1G.

.r-

'_^ut i

Page 7 of 7 1300 5/17/19 UASTE MANACDii.' T CRO!!P-(_ _.

Expected Task Tar'.j De n c r.i o t i o n Priorit.

Cemletion Status Coord.

I i'

L-11 Investiga te/ develop procccs for E-3 eliainating Unit 2 vater in Proposal to be Snider received fro'.

AUelle.r.

RCST's.

Process planning for chem-nuclear Units 1 and 2.

Design (con-5/4/79.

ceptually) a unute processing system for Unit 2 liigh Level Liquid Uastes.

L-16 Lou-level '. ste (paper, rags, E-3

.ood, etc.) disposal.

In progress; Edward second com-

^Weller pactor ordered.

Develop CIJ-CU
- 3 Systen.

B-3 Initial planning Snider only.

Detail

  • Ueller design
  • Collin scheduled to start 4/25/79.

L-20 Obtain a level nc:sure 2at and E-3 I!easurement Ross/

a canple of uater from the RS using Heise

  • Cwalin.

r,ung and basc. meat.

gage being explored.

L-22

D2velop a plar. for long-term B-3 Open/

I cleanup to prov;.d2 access to

  • Collin-Au:.iliary F,ld;;. for restoration actititiet..

L-30

} Duclop pinn for radiation L-3 Open/

t survey in Aur.iliary and Fuel

}iiandlingEldt.

SStodda-I G-13

!rnergency RB Cas Purge Cleanup A-3 On hold; no Open/

System.

t plan to

^Collin-i, inplenent.

C 29

. t.: to.

Io-c B-3

.irlock Inac ti-unncaessary at Starret

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this time.

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