ML19253A512
| ML19253A512 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 05/17/1979 |
| From: | Vollmer R Office of Nuclear Reactor Regulation |
| To: | Stello V Office of Nuclear Reactor Regulation |
| References | |
| NUDOCS 7909100188 | |
| Download: ML19253A512 (20) | |
Text
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UNITED STATES
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3T NUCLEAR REGULATORY COMMISSION
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WASHINGTON, D. C. 20s55 3, b
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.s*p May 17, 1979 o * *....
MEMORANDUM FOR:
Victor Stello FRCM:
Richard H. Vollmer t
SUBJECT:
Dil DAILY RE?O3T e
A.
Reactor and Plant Status 1.
The Presidential Commission visited the site this afternoon.
NRC personnel were not directly involved.
2.
Technical Progress Meeting - see Attachment for agenda and notes.
3 system Parareters and Core."ap - pressurizer pressure approxi-ately h59 psi with buoble drawn.
Cooldown suspended temporarily pending further developmert of plans and procedures.
L.
As suspected, containment level described in 5/16/79 eport was incorrect, due to error in measurement of location o#
pressure gauge, actual level is 238.5', 2' less than origi ally reported, which represents no i-ediate th eat to any equipment.
O p e ra t i on of JH-V2 on hold pending furt'er evaluation.
5.
JHR A loop hydro test on hold due to hig" area radiation 'ece's caused by :H-76 opening for containrer.t level readings.
Resolution under consideration.
6.
RCS sanale expectec 5/13/79 3.
Environ ental u aasura ents 1.
No radiation level cSove oackground sas detected bv JCE aerial surveys.
No reports were received from other agencies.
7 9 09100 /s)f' hk G
J
'/ictor Stello =
2.
A milk sample detected no 1-131 above a MOL of 10 picocuries per liter.
3.
Air samples at locat ions a rounc the s i te ranced f rom
?
3.4 x 10-I3 to 6.6 x 10-12, 3
J V-
/
Richard H. Vollmer Attachments cc:
2.
Eisenhut C.
Smith, II 1 Vollmer G. bainas J.
Collins J. Crutch #ield
- 3. Grimes Jaily Peport File r
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RELEASES 1100 (5/15/79) 1100 (5/16/79) 1100 (5/17/79)
-13 748 6.10 x 10-9 3.4 x 10-9 1.49 x 10
-10 7
219 1.12 x 10-11 1.4 x 10-10 4.4 x 10
-9
-9 j
Inlet 2.40 x 10 3.72 x 10-10 1.6 x 10
-1~?
Train #1*
Not Running 2.71 x 10-12 6.6 x 10
-l~'
Train #2*
1.72 x 10-11 4 1.79 x 10-13 8.44 x,10
-12
-12 Train #3*
9.65 x 10 6.90 x 10 12 3.8 x 10
-1 Train #4h 9.65 x 10-12 3.37 x 10-12 3.66 x 10 REACTOR COOLANT SYSTEM PROFILE PLANT STATUS 1100 (5/15/79) 1100 (5/16/79) 1100 (5/17/79)
A B
A 3
A 3
Th 167.5 168.5 166.9 168.3 169.5 170.6 Tc 155.8 99.1 155.9 99.1 157.7 114.5 T
11.7 69.4 11.0 69.2 11.8 56.1 Tstm 153.0 121.6 153.2 122.4 155.7 130.1 PZR LEVEL Cal.
Solid Solid 373 DVM LT-3 386,/
~0 R.C. Press.
614 446 S/G Level 415" 96%
415" 95%
420" 967.
Turb. B/P 84%
Closed 69 P.
Closed 60%
Closed I.C.T.
High 303.4 303.9 304.37 Avg.
191.3 Not Available 194.16 M.U.
Tenp.
124 127 123 L
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5/17/79 4
TECIETICAL WORKING GROUP 1300 5/17/79 l.
Agenda, 1300, 5/17/79 Technical Working Group 2.
Radioactive Releases and RCS Profile 3.
Top Priorities List 4.
Action Items from 1300, 5/16/79, Technical Working Group 5.
Task Lists U.
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AGENDA 5/17/79 TECHNICAL WORKING GRCUP 1300 5/17/79 1.
Radioactive Releases
~
a.
748, 219, Auxiliary Building Fans b.
Vent Header and Drair. Trunk c.
Dome Radiation Monitor i
d.
Measurement of Radiatian Level Inside Containment j
r 2.
Plant Status 7
a.
Plant Operations Schedule Q SP -la b Bypass Valve Adjustment Toward 64%
C# *
/,ff Ab.[lco de-oh o A,
IfJ fN6 y
DHP
'A' Test Replacement of 'B' train FHB charcoal filters w w.%, c ; 5 2
Obtain RCS Sample - 0900 5/13 DiowM bu NV -
Sanple Bleed Tank 'A' - Analysis should i'iclude Boron 7"*
Concentration i' N 3.
Containment Sumo Level j
a.
DHV-6B - Results of Containment Lavel Determination Shbb I
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b.
DHV-2 Operation g%
a g-4P m a u,od. ~to use Not 4.
Analysis Reevaluation of exist 'ng rec ^==end tion to) draw a bubble vs.
solid a.
f }.
seeg aperatioa C/01 c, a
b.
Procedure for verification of Solid PZR durine solid operations at 300 psi c.
Reductionto 300 psig - increase in loss of pressure protection?
d.
Use of Long-tern Cooling System
'3' OTSG 5.
Construction Status Esti=at ed Comoletion a.
Tank Farm M
w 5/2 b.
OTSC 'B' Long Term Cooling 7<w~
5/1 c.
EPICOR (CAP-GU'i II) 5/ 23 d.
RCS Pressure /Volu e Control T mnev e 5/1
}
for testing TI e sh c o d%
- N
8% M
%.cl <# *\\,. M-Auxiliary Diesel Generator Auto Start %..g.
5/17 c.
f.
Alternate Decay Heat Removal System tie-in; 6/1
. D, 0 adb, of
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5/17/79 TOP PRIOR 1 TIES Development of plan for management of radioactivity in A-1 Auxiliary and Containment Buildings.
e Identify and isolate sources of iodine leakage.
A-1 e
Complete tank farm in Unit 2 spent fuel pool.
A-1 Completion of EPICOR (CAP-GUi II) System A-2 Develop =ent of plan for treatment of Auxiliary Building B-1 liquid waste Complete
'B' OTSG cooling and =odific.atio G on g-t e rs)
C-1 Development of alternate systua f0c pressure /vor.tra C-1 control system.
Complete ext.ernal valve pit fc c ADHR System.
C-2 CATECORY A
Control (i.e., containment) of radioactivity in Auxiliary and Containment Buildings B
Recovery of Auxiliary Building to near normal operations C
Place the plant in a cold condition suitable for depressurization with long-tern pressura/
volume control
,t>
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5/17/79 ACTION ITEMS TECHNICAL WORKING CROUP 1300 5/16/79 Item Action 1.
Determine proper hydro test pressure for UG-6.
Burns & Roe 2.
Evaluate building and river temperatute affects on Wilson /
maintaining negative pressure in the Reactor Building.
B&W 3.
Insure that adequate verification of continued solid Wilson operation is placed in the current procedure for solid RCS operation.
4.
Evaluate the best nethod for cooldoun of pressuriscr Wilson /
BEW a.
Venting steam frca bubble operations b.
Level cvele from 330 - 370" a 100 - 370" J l b' e
Page 1 of 2 1300 5/17/79 PLANT OPEPATION STAFF 4
Expected Task Task Ducriotion Priority Comoletion Status Coord.
l 1.
Obtain RCS sample (Primary C-1 5/18 Hetrict.
letdown).
=
2.
Obtain MEC approval (Tie-in C-1 Need ECM's Kunder/
I approval only).
170 R1 Faulkner /
264 R0 and 1, Seelluger 272 Rl.
3.
SSRU pump, "C" repair.
C-1 Comp. by 5/20.
4.
Decay Heat System.
C-1 Cycle DHV-6 Cycled 5/15.
Toole after hydro.
3.
Remove water from "B" Fuel Pool.
B-1 Not started Kunder 6.
Isolate Unit !!1 and 32 sample Need new sample Limroth/
stations.
sink.
McGoey 7.
Training on Diesel.
In progress.
Troffer/
Kunder/
Toole 3.
Training on Decay Heat.
C-1 In progress.
Westinghouse Troffer/
will provide Kinder /
training plan.
Toole 9.
Sample AB/FHB charcoal beds.
B-1 AB "A"
& "B" Kunder/
5/19.
Retrick FHB "A" 5/23.
10.
Gr'v diesel.
C-1 5/17 Both cocplete Toole except for Uhite diesel.
5/17 auto start 5/17.
Toole 11.
Move filters out of Aux. Bldg.
3-1 In progress.
12.
Repair DU-P-4A.
Working 4A.
6 0*.' comple te.
13.
Repair SW-P-13.
Need new Regn. No.
Shovlin shaft.
201-1720.
14 CO-P-1B repair.
In progress.
Shovljn 13.
Install self-cooling on Toole/
condensate pump 1A.
Gunn
Page 2 of a 1300 5/17/79 PLANT OPERATION STAFF Expected I
Task Task Descriotion Priorit's Comoletion Status coord.
16.
Rebuild breaker for Cap-Gun.
Need 51 relay Shovlin and CT.
e 17.
Maintain turbine sump empty.
Until comple-Kunder/
tion of "B" Frederick OTSG flush.
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1300 5/17/79 PLANT 510DIFICAT10NS Expected Task Tar.k Description Priority Co nietion Status Coord.
WG-1 Install AB/FHB Filter System.
A-1 Complete by System opera-Shubert 5/15.
tional 5/10; complete 5/15.
WG-2 Decon. wcter in AB using EPICCR A-1 Turn over Lacy /
(L-1) ion exchange process.
5/23.
Fricke WG-6 Install storage vessels in Fuel A-1 Turn over Gibson (L-2)
Pool "A".
by 5/23.
WG-ll Water Chemistry Lab for use A-1 System com-Tcile/
with CAP-GUN (WC-2).
plete by 5/17.
Rao WC-12 Ventilation filtration system A-1 Turn over Shubert for decay heat pits.
5/26.
TS-13 Install elec. heaters on Aux.
A-2 On hold.
Shubert Bldg. intake ducts.
TS-3C Develop complete package for C-1 Turn over Jordan /
lon;;-term cooling OTSG "B".
5/17.
Lanza Estimated com-Miller /
TS-6B F;S pressure control system.
C-1 Schedule
~
pletion 5/25.
Lilly being revised.
TS-11 Aux. diesel generators.
C-1 Testing.
Complete Gagliardo except for auto start 5/17.
TS-14 Shielding for decay heat pump.
C-2 Turn over Lieberman 5/23.
NOTE:
Plant !!cdification Prelininary Schedule for Westinghouse ADHR System indicates 6/21/79 completier. date.
i 4
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1300 5/17/79 TECH:iICAL SUP' PORT E::pected Task Task Description Priority Comoletion Status
' Coord.
L5.?
Tech. Spec. and Surveillance 1
?
Active:
NRC L. W. Hardin and Bases Changes to those interactions left deletions, additions.
under negotia-
- tion, i
LS.3 Initial Reporting of Event.
1 5/15 to NRC.
Active.
R. A.
Lengel lCobean IM.23 Reactor Coolant System 1
5/23 Active.
P/V Control.
TM.30 Determine what 30P loads 1
Continuing.
Draft criteria Capodanno/
need backup electrical power.
document issued Langenbach 4/24.
TM.35 Long-tern plant instrumentation 1
On hold.
Criteria docu.
Capodanno/
requirements (criteria).
being revised.
Langenbach AA 61.
Update S!R.
1
?
Draft received.
d&W AA 66.
D.
How to caintain primary 1
?
Active.
GPUSC/MPR boron conc.
AA 69.
Define all plant mods needed 1
?
Croneberger for long-tern operations.
AA 30.
Analytical and Tech. Planning 1
?
Continuing.
J. A. Daniel Support for updated procedures (EP-32, etc.).
AA 33.
Identify critical valves and 1
?
Active.
Pre-R.
Long instruments which may be lin. list damaged by high su=p levels.
available.
AA S4 Identify flow paths from the 1
B&R investi-Active.
contain=ect sump.
gating.
AA 37.
Solid Pressurizer Analysis.
1
?
Active.
J. Moore AA 96.
Boren concentration in R3 sump 1
?
Active.
J. Moore 4/30 through 5/15.
TM.37 Installation of cartridge-type 1
ECM issued.
Revising Capodanno/
Demineralizer for clean-up of design.
Langenbach S.G.
"3" secondary side.
AA 1.
Letdown Flow Analysis 1
Continuing.
Active.
Met-Ed (continuing curve development).
Control Roorc AA 71.
Determine requirements to 1
?
?
perform sample analysis locally.
.\\n~
1300 5/17/79 WESTI:iCHOUSE Expected Task Task Descrintion Priority Comnletion Status Coord.
TS-15 ADHR Installation C-1 6/21/79 See sub-F. J. Serage (II.B) d ivis ions.
ECM 109: ADRR piping and C-1 5/18 F.J.Serah cabling ECM 119:
Excav. west side C-1 Complete.
of FHB ECM 120:
0 1 nce ek-up C-1 Complete.
2 training ECM 122: ADER skid off load C-1 R. Clark and tenp. shelter ECM 136:
Elect. control C-1 3/25 Exp. delivery Scrago/
trailer 5/19 Imagawa ECM 143:
ADHR skid assembly C-1 5/25 R. Clark ECM 16'.
Hydraulic valve C-1 Complete.
operator EC'1 132 :
F.1 Penetration C-1 5/31
~
J. W. Meyer EC:t 199: Valve pit C-1 6/13 Serago/
Meyer ECM 212:
Component cooling C-1 R. Clark skid ECM 226: Wiring ADHR skid C-1 3/25 R. Clark l
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Page 1 of 7 1300 5/17/79 WASTE MANAGEME::T GROUP Enpected Task Task Description Priority Cocoletion Status Coord.
L-1 Design, installation, and B-1 5/23 Remaining Snider /
operation of EPICOR for items are Ga rman/
Unit 2.
installation McCutcheon/cI of CAP-GUN kWeller/
equipment and
': Collins coating of the floor.
L-2 Design, intallation, and B-1 5/1 75% comp.
Reinmann/
operation of emergency surge piping in FH3.
Snider /
tanks (tank farn) in Unit 2 iWeller/
comp. welds "A"
Fuel Fool.
A 4 Collins in A3 pipe, FE pipe.
Prefab. pipe ready for installation in AB.
"B" train pour planned for 5/7; "A"
train pour complete.
~
'75% concrete slabs placed atop fuel pool.
L-10 Pursue activities on processing A-1 In progress.
Gar =an/
Unit 1 water through CAP-GUN to Geller both provide support to insure ava lable freeboard for Unit 2 and to develop resin formula-tions for Unit 2 water.
L-14 Evaluate waste gas vent nader A1.
Yorking per McConnell/
leakage prob:. ems and tetonmend J.
Seelinger's Arthur /
fixes depend _ng on results.
waste gas plan
- Bland of 4/17/79.
MRC cantact
' /
i 1
Pap,., 2 of 7 1300 5/17/79 g 4,. c '1 1,.
....,.,,p,u.-..-
u u, g,.,,,
w suum..
..t 0c Er.pecteu_ _ _ _ _
Tash Ta e,'c Daccriution Priorit' Cc-iletion Status Coord.
L-36 Investigate the effects which C-1 In progress.
McCocy/
the operations associated Ross/
<eith reactor plant long-tera
- Co llinsi, cooldoun ulll have on discharge
{
to the u<tste systems.
Related
-2, to L-o.
L-42 Development reco.r.,calations and C-1 McGoey[
,cocedure for draining and Ross/
c'2cpositica of RCCT. rater to
- Collins support plant needs to nahe up
- Lth degnssed dectin, uater.
L-4!.
.=aluate synte., designa rith E-1 Report being I; raft /
Technical functions and U to prepared; nueller assess pos:,ible interference delayed by problems frca standpoint of higher priority locations, operations, tasks.
.-.intenance, etc.
L
!< 7 l Resol.csar.plelabrquir272nts E-l Meeting held I;raf t j
,c sus capabilitics to 5/1/79;
\\ support E?ICCit I and II opera-resolution tions.
.in progress.
G-1 Install A3/F!!O of f-gan filter A-1 Phases I, II, Montgoa-
.ysten to b.:k-up plant systen and III design Itschne complete.
SCollins Systen descrip-tion and start-up procedures are c omplete.
Four M) fans are operable, l
3 or 4 are run-l ning.
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Page 3 of 7 1300 5/17/79 UASTE :Ud!ACFl!E:<T CROUP.
E:cpec ted Iask Task Descriotion Priority Concletion Status Coord.
G-5 Change out AB/FHB HVAC vent A-1 "A"
& "B" train McConnell filter train charcoal bed.
of the AB fil-Eduards/.
ters and "A"
- Weller train of FHB j
filters removed and replaced, units back in service. FHB "B"
train in change-out scheduled for 5/17.
Deluge syste=3 secured on all runeued filter trains.
Spent filter tray rc= oval to storage com-pleted.
G-31 Determine air flow paths in A-1 Operating matri:
Nawaz/
AS/FEB.
developed and Itschner/
'available.
Robison/
- Weller G-32 Determine that there are no A-1 E::anination of Nawaz/
unidentified air flow paths.
plant status /
Itschner/
configuration Robison/
under'ay.
':Bar rett First cust.
revicu complete 20 contact
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Page 4 of 7 13 00 5/17/79 UASTE MAN'GEME::T GP.OCP.
E::p ec ted Task.
Tan't Deccriotion Priori 17 Caml e t ion Stat,ts Coord.
C-33 D welop plan for ventilation B-1 Meed identified Itschne systen operation based on fan /
to ~ t up a
- Stoddat filter train status and on plan.
Control /
door openings and other plant advise on local operation evaluations.
and systen ven-e tilation p rac t ic e. '.,
C-40 Criteria for and con. trol tas.cs A-1 20 " Red Devil" SCollins resulting in the evolution of type local contacinates that could poison filtration
'c:n: coal filters.
systens on order to contro:
trelding faces.
L-3 Dcternination of leahage p2ths 2
Plant staff Kraft /
c cf flott rates in Unit 2 Aur..
f o llo t:ing.
Arthur /
' idi. and FHE and repair
- Ct:alina of laaks tihere poss ibic.
Plant h~,
leaha;c ID and Status E0ard in Unit 2 Control Room.
Pursuc P l c o. : activities associated this.
.y level solid *.:aste disposal B-2 In progress.
Pastor /
inv:stigation.
Edt:ards
- Weller/
- Collins L-2r; Perforn assessnent of the value A-2 Price proposal Kraft /
r.d need for a closed circuit being accessed Lutz/
ll innitor to provide remote versus decon.
- Stoddar ind icator of rach:2ste panel schedule of
- tt Au
- - Eldg.
i L-27
_.;iop senpling plan to access B-2 Identified 4 Passell 4
,.,.:a u t e for transuranic sampics, agreed Uillian
_ m ant.
I n:,ur e that II:t-Ed on 3.
Agreement,
- Collins Cp-coardinate canple require-reached on using,
_nts ith O?'.:L to insure previously takan
,I - __sfactory cnal',:is re nlic.
l cn".91cs f rota i
I su: :a and bleed tanks; nM i Lio nal 6,
namplen to se i
I
Pa t,e i ot 7 1300 5/17/79 UASTE ILiM!E L_ :.::T CEOUP E::pected Task TasL D0scrintion Priorirl Cc olet_ ion Status Coord.
L-29 Investigate reported uater B-2 Uater fro =
Uillice:
collection in the "B" fuel pool Unit 2 const.
AEarrett obtain samples and take plans Sample needed.
for disposition.
Also investi-gate the preoperational condition of the fuel pool from a leahage standpoint.
L-33 Develop a plan for tying in tha E-2 System cr2lteria Reinnant tank fara to EPICOR 2.
seat to 3&R on Snider /
5/1/79.
~47eller/
ACollins L-35 Irvastigate the nea:1 for 3 3-2 Alternate McConnel design and construction task to design Unit 1 Uilliant erect a barrier betueen the side to be EEarrett Unit 1 and Unit 2 Fuel liandling submitted Bldg. to enable Unit 1 opera-4/27/79.
ions uith Unit 2 in processing bde.
L-37 D2celop a plan for removing all B-2 Requires com-McConnel radioactive gases from the pletion of L-14 SCollins systens in the AB c.nd FHC.
G-7 Condenser vacuun pung discharge A-2 filter system.
Filter opera-Robison/
tional.
Inves-Montgomr_
tigating opera-
- Collins ting criteria.
Uill evaluate DF.
G-30 P.2 actor-Purge Syster t.harcoal A-2 RB purge filter McConnel Filter Sample.
Scheduled week sanple all ready
^ Collins of 5/20 for analysis.
C-33
'.,,sensitia A3 and FEB Eilter A-2 i'r elimina ry Sieg/
miters.
l investigatioa -
LStoddart desensitization ini cr :1 tilt.
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', c o n ".n e t i
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l'a ge 6 ot 7 1300 5/17 /79 UASTE ?Ud: ACE::E:;r GRCC?
E::pected Task Ta s*e Description Priorit?
Co s_T e -ion Status Coord.
G-39 Develop and asaccs back-up gas B-2 S&R has devel-McConne filtration schc=2 to cross-oped a concept.
- Lee S
connect the Auxiliary Euildina Second esticate e
Elltars to the RB purg,e filters-scheduled shous I
n 14 day +
schedule.
Heiscan Co. has developed drau-ings.
- Exposure, schedule cost i
appears too hi;;h.
Con-tingency plan is to open roughing filter mantray if emer-gency vencila-tion of Auxiliary Euilding is needed.
Standard proce-McConnel G-41
- (:v a lo p filter run:gement B-2 dures to sample ntrc:c37 charcoal systems in revicu.
G-42 Devclop a proZrr. to assess B-2 Four-part McConnc and nanitor I releasa sources.
approach:
McGoey/
Montgo:
- 1. ESR to com-3g1:
plete revie" Cline /
of release Pelitt j
candidates.
yolleg l
- 2. Pursue a trater progran to I
find leak.
- 3. Pursue an l
nir noni-toring pro-i l
gram with SAI/EPRI to plot I i
levels.
4.
Revieu local I
s ventilation cond i tio n i
J-(
to verify
(
., / (
1 tJ(c din t: L-t
)t 1I. EO ;1G.
.r-
'_^ut i
Page 7 of 7 1300 5/17/19 UASTE MANACDii.' T CRO!!P-(_ _.
Expected Task Tar'.j De n c r.i o t i o n Priorit.
Cemletion Status Coord.
I i'
L-11 Investiga te/ develop procccs for E-3 eliainating Unit 2 vater in Proposal to be Snider received fro'.
AUelle.r.
RCST's.
Process planning for chem-nuclear Units 1 and 2.
Design (con-5/4/79.
ceptually) a unute processing system for Unit 2 liigh Level Liquid Uastes.
L-16 Lou-level '. ste (paper, rags, E-3
.ood, etc.) disposal.
In progress; Edward second com-
^Weller pactor ordered.
- Collin L-17
- Develop CIJ-CU
- - 3 Systen.
B-3 Initial planning Snider only.
Detail
- Ueller design
- Collin scheduled to start 4/25/79.
L-20 Obtain a level nc:sure 2at and E-3 I!easurement Ross/
a canple of uater from the RS using Heise
- Cwalin.
r,ung and basc. meat.
gage being explored.
- D2velop a plar. for long-term B-3 Open/
I cleanup to prov;.d2 access to
- Collin-Au:.iliary F,ld;;. for restoration actititiet..
} Duclop pinn for radiation L-3 Open/
t survey in Aur.iliary and Fuel
}iiandlingEldt.
SStodda-I G-13
!rnergency RB Cas Purge Cleanup A-3 On hold; no Open/
System.
t plan to
^Collin-i, inplenent.
C 29
. t.: to.
Io-c B-3
.irlock Inac ti-unncaessary at Starret
\\
this time.
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