ML19242C047

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IE Insp Rept 50-313/79-09 & 50-368/79-09 on 790414-0511.No Noncompliance Noted.Major Areas Inspected:Previously Noted Items,Refueling Activities & Licensee Actions Taken in Response to IE Bulletin 79-05A
ML19242C047
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 05/30/1979
From: Johnson W, Spangler R, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19242C039 List:
References
50-313-79-09, 50-313-79-9, 50-368-79-09, 50-368-79-9, NUDOCS 7908090691
Download: ML19242C047 (15)


See also: IR 05000313/1979009

Text

.

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION IV

Report Nos. 50-313/79-09

50-368/79-09

Docket No.

50-313

License No. DPR-51

50-368

NPF-6

Licenace:

Arkansas Power and Light Company

P. O. Box 551

Little Rock, Arkansas 72203

Facility Name: Arkansas Nuclear One (ANC), Units 1 and 2

Inspection At: ANO Site, Russellville, Arkansas

Inspection Conducted: April 14 through bby 11, 1979

Inspectors:

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W. D. Johnson, Resident Reactor Inspector

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R. G. Spangler, Ifenctd'r Inspector

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M. W. Dickerson, kcactor Inspector

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E. II. Johnson, Reactor Inspector

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Reviewed By:

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T. Y. Westerman, Chief, Reactor Proj ects Section

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.

590193

790809069;

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Inspection Summary

,, , _ _

Inspection conducted during period of April 14 through Fby 11, 1979 (Report

No. 50-313/79-09)

Areas Inspected:

Routine, announced inspection of previously identified

inspection items, refueling aceP ; ties, surveillance (ref ueling), naintenance

(ref ueling), and licensee actic as taken in response to IE Bulletin 79-05A.

The

inspection involved 192 inspec.or-hours on-site by six (6) NRC inspectors.

Results: Within the five areas inspected, no items of noncompliance were

identified.

Inspection conducted during period of April 14 through Fby 11, 1979 (Report

No. 50-368/79-09)

Areas Inspected:

Routine, announced inspection of licensee actions taken in

response to IE Bulletin 79-06B.

The inspection involved 107 inspector-hours

on-site by six (6) NRC inspectors.

Results: Within the area inspected, no items of noncompliance were identified.

-

59G194

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DETAILS

1.

Peracns Contacted

Arkansas Power & Light Company Employees

J. P. O'Hanlon, ANO Plant Manager

G. H. Miller, Engineering & Technical fupport Manager

L. Alexander, QC Engineer

B. A. Baker, Operations Superintendent

T. N. Cogburn, Nuclear Engineer

E. C. Ewing, Production Startup Supervisor

D. R. Hamblin, QC Engineer

T. Holcomb, Scheduler

P. Jones, bbintenance Supervisor

B. A. Terwilliger, Operations and Maintenance Fbnager

J. Robertson, ANO-1 Operations Supervisor

S. Petzel, Licensing Engineer

F. Foster, Plant Administrative Fbnager

R. Elder, I&C Supervisor

J. McWilliams, Planning & scheduling Supervisor

J. Vandergrift, Training Supervisor

T. Green, Training Coordinator

L. Trimble, Licensing Manager

F. Boswell, Safety and Fire Prevention Coordinator

C. Shively, Plant Performance Engineer

2.

Plant Status

Unit 1

.

The plant was shutdown for refueling during this inspection peri,d.

Unit 2

The plant was shutdown for maintenance following testing at the 20% power

plateau.

3.

Followup on Previously Identified Item

(Closed) Open Item (368/313/79-07-03) - Specific duties of Shif t Supervisor

during a fire emergency.

The inspector discussed this item with the licensee.

The licensee feels the

present wording defining the Shift Supervisor's duties during a fire

emergency is satisfactory.

The licensee has questioned the Shift Supervisors

to verify that they understand their duties and responsibilities under these

conditions.

This item is closed.

590195

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4.

Refueling Activities (Unit 1)

r

The inspector reviewed activities concerning the refueling of Unit 1.

This review consisted of:

Review of prefueling activities

.

Fuel handling crew requirements

.

Core monitoring during refueling

.

Containment integrity

.

Fuel accountability

Observation of fuel movements

.

The reviews and observations were conducted to verify that refueling

activities were conducted in accordance with Technical Specifications, NRC

requirements and approved plant procedures.

No items of noncompliance or deviations were identified.

5.

Surveillance (Refueling) (Unit 1)

The inspector reviewed the procedures and results of the following survail-

lance activity conducted during the refueling outage.

Diesel Generator Inspection ("A" Diesel Generator)

A review of Procedure 1405.02, Rev. 1, 1/27/78, and the results of the

inspection covered by this procedure was made by the inspector to verify that

the activities were in accordance with Technical Specifications and approved

plant procedures.

6.

Major Maintenance Activities (Refueling) (Unit 1)

The inspector reviewed the follcwing maintenance activity during the refueling

outage.

Emergency Cooling

This maintenance activity consisted of installation of two (2) safety grade

cooling units to cool electrical equipment during post-accident conditions.

The inspector reviewed the Design Change Request sDCR 589), the purchase

orders and material receiving reports concetulug the work activities. The

inspector also observed latter portions of the work in progress.

The documentation on seismic and environmental qualification is not c.omplete.

Also, at the time of this inspection the final acceptance test of the

installed equipment had not been performed.

This item will remain open

pending qualification review and satisfactory acceptance testing.

(313/79-09-01)

59G196

.-

-5-

7.

Continued Review of Licensee Actions Taken in Response to

IE Bulletin 79-05A (Unit 1)

A.

On-site Inspection of Engtgeered Safety Features (ESP)

(1) Valve / Breaker / Switch Alignment Procedures

The inspectors completed the review of valve / breaker / switch

alignment procedures for all ESF systems against current

P6ID's and single-line drawings to verify adequacy of

alignment procedures.

(Reference paragraph 13 of inspection

repott 79-07).

The systems and the results of this review are as follows:

Service Water System

The inspector compared the valve / breaker lineup specified in

Attachments A, B, C and D to Operating Procedure 1104.29 to

drawing M210 for the Service Water System and found:

(a) Per M-210 SW-44, RE3810 Isolation Valve, should be SW-93; and

SW-45, RE3810 Isolation ValV6, should be SW-89 on Attachment

D to 1104.29, page 1/5.

(open item 313/79-09-02)

(b) That the addition of the valves f astalled under DCR 589, Vital

Switchgear Room Coolers, in Attachment B and C valve lineup

sheecs of 1104.29 had not yet been completed.

(0 pen Item

313/79-09-03)

Diesel Generator Starting Air System

No problems identified.

Penetratian Room Ventilation

No problems identified.

(2) Administrative Controls After Testing / Maintenance

The inspector reviewed the licensee's administrative controls to

verify that they assure proper return to service of ESF components

following test and maintenance activities.

This review was

tentered on the following procedures:

1004.14, Rev.

1, PC 1,

Initiation and Processing of Job Orders

1004.19, Rev. 4, Hold, Caution and QC Tagging Procedure

1005.04, Rev. 3, Control and Use of Bypasses and Jumpers

(a) The licensee's response to item 10 of IEB 79-05.1 reported

that the job order form was being revised to specify all

pre-maintenance and post-maintenance requirements and to

include verification that they are met to assure redundant

component operability prior to maintenance and to assure

590197

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affected component operability after maintenance or testing.

This revision is considered neces'sary to strengthen the job

order procedure and it will be reiiewed by the inspector

prior to unit startup.

(Open Item 313/79-09-04)

(b)

1004.19

This procedure has the apparent. weakness of not specifying

the desired valve / breaker / switch position upon removing hold

tags.

The hold card request sheet has a signature space

labeled " Tags Removed: System Returned to Normal," without

stating what " normal" alignment is.

After discussions with

licensee representatives, the inspector stated that this

procedure may be acceptable as is when used in conjunction

with a properly revised and strengthened 1004.14.

(c)

1005.04

This procedure appears to require proper control of bypasses

and jumpers.

The inspector has indicated to the licensee

that it would be acceptable, in order to simplify the

administration of 1005.04, to eliminate logging require-

ments for jumpers and bypasses whose installation and

removal are controlled by specific docunented steps of

surveillance test procedure.

an appro,

<

(3)

Review of ESF Surveillance Tests

The purpose of this inspection effort was to review the surveil-

lance test procedures for the ESF systems to ensure that the

procedure restored the system to operability following the test

and that appropriate testing was performed to meet Technical Speci-

fication requirements.

The following test procedures were reviewed:

1104.01 Supp. 1

- Core Flood Tank Operability

1104.02 Supp. 1

- High Pressure Inj ection (llPI) Valve

Operability

Supp. 2-4 - HPI Pump Operability

1104.04 Supp. 1-2

- Low Pressure Injection Pump and Valve Operability

1104.04 Supp. 2

- NaOH Addition Tank Valves

Supp. 3-4

- Reactor Building (RB) Spray Pump

Supp. 4

- RB Spray Valves

Supp. 6

- RB Spray Nozzles

1104.33 Supp. 1-5 - Reactor Building Cooling

1104.36 Supp. 1

- Diesel Generator (DG) Operability

Supp. 2

- DG Air Start Compressors Operability

Supp. 3

- DG Fuel Oil Transfer Pump

Supp. 4

- DG Overspeed

1104.43 Supp. J-2

- Penetration Room Ventilation Filter Trains

1106.06 Supp. 1

- Electric Energency Feedwater lump (EFS)

Supp. 2

- Steam Driven EFW Pump

Supp. 3

- EFW Valve Operability

Supp. 4

- EFW Flow Path Verification

1304.08 Supp. 1-6 - Integrated ES Test

{[g('fg[3

1405.02

- Annual DG Inspection

.

-7-

No items of noncompliance or deviations were noted in this area

of the inspection.

However, the inspector had several questions

and observation.s regarding certain procedures which were

discussed with the licensee during the inspection.

These items

are considered open.

The inspector noted that there is no flow indication for the

Emergency Feedwater (EFW) system and that the operation to shift

EFW to its safety grade water supply (service water) must be done

manually.

The licensee is pursuing several modifications to the

EFW system.

(open Item 313/79-09-05)

During review of the low pressure injection (LPI) system procedure

the inspector noted that the acceptance :r.teria for pump Ap is

130-143 psid. The FSAR states that the rat 9d pump Ap at rated

capacity is 151 psid.

The Technical Specifications require the

pump to perform within + 10 percent of initial values.

The above

acceptance criteria were established by the licensee for the ASME

Section XI testing program.

The inspector questioned whether or

not these values were within the criteria of the Technical Specifi-

cations noting that the physical placement of pressure detectors

in the system can cause readings to vary from design values. A

licensee representative indicated that these criteria would be

compared to the results of preoperational testing to determine if

the appropriate acceptance criteria have been specified.

(open

Item 313/79-09-06)

The inspector aise noted that valves CV1401 and 1402 in the low

pressure injection system are not cycled during the performance of

surveillance testing on the LPI system valves.

The valves form the

boundary between the high pressure and low pressure side of the

system and are excluded frca the ASME Section XI testing while

the plant is at normal operating pressure to preclude the possibility

of overpressurizing the low pressure portion of the system.

A

Technical Specification Change is needed to reficct this exclusion

from testing.

(open Item 313/79-09-07)

Supplement 1 to Procedure 1104.36, Diesel Generator Operability,

test contains a procedural step that requires placing the diesel

generator control switch in the maintenance position.

Although

subsequent test steps require that this switch be returned to the

remote position, the inspector expressed concern that the restor-

ation steps of the procedure do not include provisions to verify

the diesel generator alignment for standby operation using control

room indications.

(0 pen Item 313/79-09-08)

During review of Procedure 1106.06, Emergency Feedwater (EFW)

Operation, the inspector noted that step 6.2.2.2 requires the

operator to verify the steam supply pressure to the EFW turbine.

N C i, 9 .9

-8-

llowever, no pressure valve is specified in order for the operator

to determine that the pump is operating normally. A licensee

representative indicated that such a value will be provided in

the procedure.

The inspector further noted that valves CV2813 and

CV2814 are not cycled during the performance of the routine valve

operability test.

These valves will be added to the procedure.

(open Item 313/79-09-09)

The inspector reviewed Procedure 1304.08, Integrated ES Test, and

noted that the service water valve alignment specified in the

preliminary steps of the procedure was in error.

Establishing

such an alignment would secure cooling water to the operating

decay heat removal pump bearing cooler.

It was further noted that

the restoration steps of the procedure did not include several

manual valves that were aligned in the preliminary steps of the

procedure.

Although the alignment of these valves would be checked

prior to startup during the performance of valve lineups, these

valves should be included in the surveillance procedure. A

licensee representative indicated that the procedure would be

changed to reflect these concerns.

(open Item 313/79-09-10)

(4)

Review of ESF Surveillance Test Results

The purpose of this inspection effort was to review the results

of the latest surveillance test on all ESF components to determine

that the acceptance criteria for these tests were met.

The surveillance tests reviewed were the latest tests conducted by

the licensee for each of the procedures reviewed above.

No items of noncompliance or deviations were noted.

The inspector

noted the following discrepancy which was discussed with the licensee

during the exit interview.

This item is considered to be an open

item.

(313/79-09-11)

During the performance of the filter train monthly test on the

penetration room ventilation systcm on >brch 24, 1979, it was

noted by the operator tnat the door to the upper north electrical

penetration room would not properly shut due to a security monitor

on the door.

The inspector expressed his concern that this could

affect the capability to properly seal this room.

A licensee repre-

sentative indicated that prompt action would be taken on this

matter.

(5) Administrative Controls after Outage

The inspector reviewed the licensee's administrative controls to

verify that ESF systems are returned to operability at the

conclusion of extended outages.

This review was centered on

the following procedures:

59021 0

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1102.01, Rev. 5, PC 6 - Plant Preheatup and Precritical

Checklist

1102.02, Rev. 6, PC 1 - Plant Startup

Two apparent discrepancies were identified. The Hydrogen Purge

System is not specified by these procedures to be aligned prior

to startup, although licensee representatives informed the

inspector that the alignment of this system is normally checked

prior to startup after an extended outage.

(0 pen Item 313/79-09-

12)

The startup procedure does not specify the desired hand switch

position for the High Pressure Injection Pumps. Although the

mispositioning of these switches would not make the system

inoperable, their desired position should be specified.

(0 pen

Item 313/79-09-13)

(6)

Independent Verification

The inspector determined that the licensee does not use "indep-

endent verification of valve / breaker / switch alignments when

performing those alignments following extended outages and

after maintenance or test activities.

B.

On-site Assessment of Operating Procedures

(1) Partial Actuation of Safety Injection to Aid in Pressurizer

Level Control

Anticipated operational occurrences that have a characteristic

of falling pressurizer level occur whenever s. ,ondary heat

removal exceeds primary heat generation for a short period of

time following the initiating event.

Some examples of these

include reactor trip, dropped control rod, feedwater control

malfunctions, and secondary safety relief valve or turbine

control valve malfunction.

The pressurizer level instrument

tap span is 320 inches at ANO Unit 1 with approximately 100

inches of additional level both above and below this span.

Normal level is 180 inches.

Early in the operation of Unit 1

(during 1974), at least one reactor trip occurred during which

indicated pressurizer level was lost.

Analyses by AP&L and B&W

following this event showed that the level fell approximately

8. inches to 10 inches below the low level tap.

The pressurizer

level charts reviewed by the inspector support this analysis

provided one assumes a smooth trend of level from the time it

went of f scale low until it reappeared (approximately 40 seconds)..

AP&L and B&W concluded that the main cause for this problem

was primary temperature stabilizing at a lower point than

design due to excessive feedwater flow and secondary relief

valve settings on the low end of the acceptable band.

Adj us tments

590ZC1

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were made within the Integrated Control System (ICS) and to the

safety relief valves to improve the transient response of pressurizer

level.

Less of pressurizer level has not been experienced since this

event.

Prior to the above adjustments and as an interim measure,

procedures were modified to require manual initiation of HPSI

to maintain RCS water inventory.

After the above adjustments

were nade, procedures were again modified to include pre-

cautionary steps instructing the operator to start the standby

makeup pump but to inj ect only through CV 1220, the normal makeup

return valve.

As the result of discussions with several senior

reactor operators, the inspector understands that operators

typically, during these types of transients, take manual control

of the pressurizer level system and start the standby HPI pump.

It appears that the system, if left to itself, would stabilize

without the loss of pressurizer level indication; however,

operator intervention terminates level drop and returns level to

normal much more quickly than could otherwise be expected.

(2) Procedures for Feeding Dry Steam Generators

No procedures currently exist for feeding a dry steam generator

from the emergency feedwater system.

It would appear that there

are two poss'ible areas of concern:

(1) tube intergity; and (2)

excessive primary cooldown.

The EFW system sprays into the OTSG

directly onto the tube bundle in the slightly superheated

steaming region.

The plant staff feels that the EFW is therefore,

rapidly brought to saturated conditions minimizing thermal

shock to the OTSG tubes and thus do not regard tube integrity

as a concern.

The Operations Supervisor is considering adding

a caution statement to the appropriate proceduces to warn

operators of the possibility of inducing too rapid a cooldown

on the primary with the sudden injection of EFW.

(3)

Control Panel Tagging

The inspectors reviewed the licensee's control panel tagging

practices to determine whether potential exists for obsecuring

status indicators such as valve or switch position, meter

indicators or alarms.

Current practices appear to minimize

the potential for obscuring status indicators, but the licensee

has been asked to add an appropriate caution statement to

Procedure 1004.19.

(open Item 313/79-09-14)

8.

Review of Licensee Actions in Response to IEB 79-06B (Unit 2)

A.

On-site Inspection of Engineered Safety Features (ESP)

(1) Valve / Breaker / Switch Alignment Procedures

The inspectors reviewed valve / breaker / switch alignment procedures

for all ESF systems against current P&ID's and single line diagrams

to verify the adequacy of alignment procedures.

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The inspectors reviewed the following:

Operating Procedures

P&ID Number

System

' ~ ~

-

2106.06

M-2204 Sh. 4/4

Emergency Feedwater

2104.01; 2104.39;

M-2232

Safety Inj ection System

2104.40

2104.05

M-2236

Containment Spray

2304.70

M-2206

Steam Gen. Secondary System

2104.36

M-2717 Sh 1, 2

Emerg. DG Systems

2104.43

M-2264

Containment Penetration

Room HV

2104.29

M-2210 Sh. 1,2,3

Service Water

2104.44

M-2261

Hydrogen Analysis System

As a result of this review and discussions between the inspectors

and licensee personnel, the following items are to be implemented:

Add a sign-off step for Procedure 2304.70, Containment

.

Isolation and Miscellaneous Valve Stroke Test and Position

Verification, to Procedure 2102.02, Plant Startup, within

Section 8,

Cross reference the Category E Valve list in 2102.02 to the

.

valve list attachments of the operating procedures such

that valve positions are shown as -locked on both.

Add valves 2SW-73 and 2CV1406-2 to the attachment to 2104.29.

.

Add valves 2HPA-37 and 2HPA-38 to category E valve list

.

(locked open)

Add locked open designation to 2HPA-37 and add 2HPA-38

.

(locked open) to the valve list for OP 2104.44

These items are collectively designated open item 368/79-09-01.

(2) Administrative Controls Af ter Testing /FL2intenance

The licensee's administrative controls for assuring proper

return to service of ESF components following test and main-

tenance activities are the same for Units 1 and 2.

For details,

refer to paragraph 7.A(2) of this inspection report.

(3)

Review of ESF Surveillance Tests

The purpose of this inspection effort was to review the surveil-

lance and maintenance procedures for the ESF systems to verify

that the procedures restored the systems to operability following

maintenance or testing.

The surveillance testing supplements

of the following procedures were reviewed:

MCZC3

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2104.01, R2

Safety Inspection Tank Operations

2104.03, R1, PC3 Chemical Addition

2104.05, R3

Containment Spray System

2104.29, R0, PC3 Service Water

2104.33, R2, PCl Containment Atmospheric Control

2104.36, R1

Emergency Diesel Generator Operations

2104.39, 21

High Pressure Safety Injection System Operations

2104.40, R0, PC5 Low Pressure Safety Injection System Operations

2104.43, R0

Penetration Room Vent.ilation

2104.44, R1, PC2 Containment Hydrogen Purge & Recombiner Operations

2106.06, R1, PC9 Emergency Feedwater Pump Operations

In addition, Procedures 2304.67, LPSI Pump Maintenance, and

2304.67, Containment Spray Pump Maintenance, were reviewed.

No items of noncompliance or deviations were identified and all

of the above procedures contained the necessary steps to restore

the systems to operability.

(4)

Review of ESF Surveillance Test Results

The inspector reviewed the results of the latest surveillance

test performed for all ESF components to verify that the

acceptance criteria for these tests were met.

The surveillance

procedures involved in this review were the test supplements for

the above operating procedures.

No items of noncompliance or deviations were identified, but the

February 1979 test data for 2104.05, Supplement 3, could not be

located. This item is unresolved. (368/79-09-02)

(5) Administrative Controls After Outage

The inspector reviewed the licensee's administrative controls to

verify that they assure the ESF systems are returned to operability

at the conclusion of extended outages. The procedures involved

were:

.

2102.01, Rev. 1, PC 2 Preheatup and Precritical Checklists

2102.02, Rev. 1, PC 11 Plant Startup

2102.03, Rev. O, PC 5 Optional Plant Startup

The inspector noted that 2102.02 and 2102.03 are inconsistent

in the positioning of the hand switch for the third high

pressure injection pump.

2102.03 leaves this switch in

" normal af ter stop" while 2102.02 leaves it in " pull to lock."

A licensee representative agreed to verify the desired switch

condition and make the appropriate procedure change.

(0 pen

Item 368/79-09-03)

5902C4

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(6)

Independent Verification

. , _ _

The inspector determined that the licensee does not use

" independent verification of valve / breaker / switch alignments

when performing those alignments following extended outages and

after maintenance or test activities.

B.

On-aite Assessment of Operating Procedures

(1) Partial Actuation of Safety Injection

Since Unit 2 has reached no higher power levels than 207., the

inspector was unable to determine if this Unit will require

partial actuation of safety injection to assist in pressurizer

level control during transients induced by routine operational

events.

(2) Procedures for Feeding Dry Steam Generators

The licensee does not have procedures for feeding dry steam

generators.

(3) Control Panel Tagging

Refer to paragraph 7.B(3) of this report.

9.

Additional Questions and Answers Investigated by Region IV Inspectors

A.

What is the normal status of the ECCS pump room doors for Units 1

and 2?

Is this status specified by Procedure? How are we to be

sure that the pump room doors will be sealed during the recirculation

phase of LOCA cooling?

The ECCS pump room doors for both Units 1 and 2 are normally

.

open and are presently required to be closed by procedure

only in the event of flooding.

The Assistant Operations Super-

visor.,has agreed to add steps in the followup action of the

LOCA emergency procedures for Units 1 and 2 to require that

the pump room doors be secured with the initiation of the

recirculation phase of LOCA cooling.

(0 pen Item 313/79-09-15;

368/79-09-04)

B.

Do Units 1 and 2 have procedures for the failure of a primary PORV

or safety valve to close?

Emergency Procedure 1202.29, Pressurizer Problems, requires

.

that the PORV be isolated in the event that it fails to

operate or is leaking. The emergency procedures for a small

LOCA are used in the event that the PORV or a safety valve

fails open.

5902. 5

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C.

Can the Unit 1 pressurizer reference leg flash? If so, has it

happened here?

The temperature of the Unit 1 reference leg is on the order

.

of 150 F and though it could possibly flash, it is difficult

to envision that system pressures would ever decrease to the

saturation pressure for this temperature.

As far as is known,

this event has never occurred at ANO, Unit 1.

D.

Are the pressurizer pressure and level instruments safety-related?

Are they powered f rom redundant vital buses?

Pressurizer pressure is not sensed.

RCS pressure is sensed and,

.

as it inputs to the RPS, these instruments are safety-related

and meet the design criteria requiring independent and

redundant vital power supplies.

Pressurizer level instrumen-

tation is not used in any analyzed accident as a limiting or

mitigating design feature.

In this sense, it can be said to

be non-safety related; although the loss of pressurizer level

indication is not an insignificant event.

There are two level

instruments at ANO, both powered from one vital bus through the

ICS cabinet and a third level instrument powered from a non-

vital instrument bus.

These instruments are considered 'Q

Parts' since they are part of the primary pressure boundary and

they appear to be identical to other instruments that are post

LOCA qualified.

E.

What are the ef fects of ICS power failures on the EFW system?

The ICS cabinet is normally powered from a vital AC source

.

through a transfer network that will, on a loss of this normal

source, switch to an alternate non-vital source, if available.

It appears that a total loss of power to ICS would start the

steam driven emergency feedwater pump but would leave the

emergency feedwater block valves closed, thus requiring

operator action to feed the OTSG's if that should become

necessary. The inspectors have reviewed the consequences of

some failures within the ICS cabinet.

The results of this

review can be summarized by saying that the system design was

not intended to meet class 1E standards and these failures

lead to varying degrees of degradation within the automatic

circuitry.

E.

Has an analysis been done for the loss of off-site power which con-

sideres a single failure of the steam driven emergency feedwater pump?

No analysis of an accident involving the single failure of the

.

steam driven EFW pu=p coincident with a loss of off-site power

has been performed since operator action is required to mitigate

the consequences of this accident.

At ANO, Unit 1, the backup

electric driven EFW pump is powered from non-vital bus A1.

Emergency Procedure 1202.05, Degraded Power, requires that

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all Al bus breakers be opened and defeated by the operator,

except for the electric emergency fe6dwater pump load and that

the Al to A3 tie breaker be closed by the operator.

This

allows a diesel generatcr (DG) set to supply the electric EFU

pump.

The licensee indicates that a load study was performed

to verify that the DC set is capable of supporting the running

ESF loads and the running load of the electric EFW pump.

The

licensee's analysis of DG response to starting and tripping the

electric ERI pump is not yet completed.

(0 pen Item 313/79-09-16)

G.

Has an analysis been done for a loss of feedwater from full power

which considers single failures involving the EFW pump?

No analysis of this type of event has been performed since

.

operator action is required to mitigate the consequences of

this event.

That is, the operator would be required to start

the backup electric EFW pump to deliver emergency feedwater to

the OTSG's.

H.

Can the primary safety valves and the FORV pass water by design?

These valves were not designed by B&W to pass water.

The

.

licensee indicates that B&W believes that these valves would pass

water and continue to function as designed; however, no documen-

tation to support this opinion is available.

I.

Is the power operated relief valve isolation valve capable of shutting

against design steam flow and/or water flow?

The Operations Supervisor indicated in the one case where this

.

isolation valve was required to close against steam flow, the

valve stroked to the seat but tripped on over-torque without

scaling.

The torque switch was defeated and the valve was then

fully seated.

No information exists regarding the ability of

this valve to close against water flow.

10.

Unresolved Item

Unresolved items are matters about which more information is required to

ascertain whether they are acceptable, items of noncompliance or deviations.

The unresolved item identified during this inspection is described in para-

graph 8. A(4) .

11.

Exit Meetirts

Exit meetings were conducted at the end of various segments of this

inspection with Mr. J. P. O'Hanlon (Plant Manager) and other members of

the AP&L staff.

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