ML19242A821

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LER 79-021/03L-0 on 790702:steam Line Snubber,Pump Suction Snubber & Main Steam Relief Smubbers Found Inoperable. Caused by Seal Failure.Snubbers Rebuilt,Functionally Tested & Reinstalled
ML19242A821
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/01/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19242A818 List:
References
LER-79-021-03L-01, LER-79-21-3L-1, NUDOCS 7908060415
Download: ML19242A821 (1)


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