05000366/LER-1979-057-03, /03L-0 on 790624:while Performing Test for Svc Water Operability,Valve Closed & Would Not Reopen Electrically.Caused by Torque Switch Corroding to Switch Shaft.Torque Switch Repaired

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/03L-0 on 790624:while Performing Test for Svc Water Operability,Valve Closed & Would Not Reopen Electrically.Caused by Torque Switch Corroding to Switch Shaft.Torque Switch Repaired
ML19225B073
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/10/1979
From: Dayley C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19225B072 List:
References
LER-79-057-03L, LER-79-57-3L, NUDOCS 7907230482
Download: ML19225B073 (2)


LER-1979-057, /03L-0 on 790624:while Performing Test for Svc Water Operability,Valve Closed & Would Not Reopen Electrically.Caused by Torque Switch Corroding to Switch Shaft.Torque Switch Repaired
Event date:
Report date:
3661979057R03 - NRC Website

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i coen. Recpeneo valve by hand, restarted Reactor Sldg. chiller, recovered dry ell pres:

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Juif 12, 1979 F232 2 (cont'd) Cause Description and Corrc-ctive Action 2P41-F315A was satisfactcry. Reference previcus LER's 2-78-33, ? . and 2-79-54 f 9 i / }}