05000366/LER-1979-054-03, /03L-0 on 790619:drywell Pressure Exceeded Tech Specs Limit Following Shutdown from Load Reject Test.Caused by Loss of Drywell Cooling from Tripped Chillers.Drywell Venting Returned Pressure Below Limit within 15 Minutes

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/03L-0 on 790619:drywell Pressure Exceeded Tech Specs Limit Following Shutdown from Load Reject Test.Caused by Loss of Drywell Cooling from Tripped Chillers.Drywell Venting Returned Pressure Below Limit within 15 Minutes
ML19225A004
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/06/1979
From: Baxley S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19224D836 List:
References
LER-79-054-03L, LER-79-54-3L, NUDOCS 7907170105
Download: ML19225A004 (1)


LER-1979-054, /03L-0 on 790619:drywell Pressure Exceeded Tech Specs Limit Following Shutdown from Load Reject Test.Caused by Loss of Drywell Cooling from Tripped Chillers.Drywell Venting Returned Pressure Below Limit within 15 Minutes
Event date:
Report date:
3661979054R03 - NRC Website

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Unit was already in Hot Shutdown. Drywell venting was initiated per HNP-2-1500 and Drywell pressure was < 0.75 psig within 15 minutes.

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