ML19220C368

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IE Insp Rept 50-320/75-14 on 751215-18.Noncompliance Noted: Lack of Complete Documentation for Spool Piece 2-DH-124 & for Hangers Bsh 88 & 89
ML19220C368
Person / Time
Site: Crane Constellation icon.png
Issue date: 01/13/1976
From: Barker F, Heishman R, Narrow L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML19220C364 List:
References
50-320-75-14, NUDOCS 7904300482
Download: ML19220C368 (25)


See also: IR 05000320/1975014

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I:I Forcr 12

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'Jan 75) (F.cv)

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U. S. NUCLEAR RECUL* STORY C0:C!IES10::

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0FFICE OF II SPECTIO'l AND F.NFORCCIE'TT

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RECION I

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E Inspection Report No:

50-320/75-14

_ Docket No:

50-320

Licensec: }ktropolitan Edison Company

Licence Uo:

CPPR-66

B x 542

Priority:

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Reading, Pennsylvania 19603

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Ca tegory:

Safcquards

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Middletown, Pennsylvania (TMI-2)

Gr up-

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Location:

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Type of Licensec:

PWR 959 MWe (B&W)

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Routine - Unannounced

73

of Insp ction:

December 15-18, 1975

Dates of Inn; ection:

Oct ber 20-23, 1975

Dates cf Previcus In pection:

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Reportin;, Inspecter: _

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[.NarrowjReactorfsp ' or

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Accompanying Inspectors: M

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F. Barker, Reactor Inspector

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QL l b,I$]fD

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DATi:

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A. Finkel, Reactor Inspector

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DATE

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Other /.ccompanyinp, Personnel:

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Reviewed By:

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[R. F He shnan, . crio ' Lea der

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SUNIARY OF FINDINGS

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Enforcement Action

A.

Items of Nonecmo11ance

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Deficiency

Contrary to 10 CFR 50, Appendix B, Criterion VII:

Documentary evidence of conformance to procurc=ent requirements

was inco=plete for Spool Piece 2-DH-124 and for Haagers BSH 88 and

89.

(Details, Paragraph 2)

B.

Deviations

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None

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Licensee Action on Previousiv Identified Enforcecent Items

The deviation with respect to chloride and nitrate content of grout has

been resolved.

(Detaile,, Paragraph 3)

Design Changes

None

Unusual Occurrences

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None

Other Significant Findings

A.

Current Findings

1.

The following items are unresolved:

Installation of cable tray and cor.duit hangers in accord-

a.

ance with sketches which have not been approved by

engineering. (Details, Paragraph 5)

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b.

Lack of procedures to require temperature conditioning

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of cable prior to cable pulling as recommended by the

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manufacturer.

(Details, Paragraph 6)

Angular misalignment at joint 128Q between spool piece

c.

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DH 128 and penetration No. 52 and failure to provide

tolerance limits for such misalignment.

(Details,

Paragraph 7)

d.

Procedures are not available for control and calibration

of crimping tools.

(Details, Paragraph 4)

2.

The following items are considered to be acceptable:

QC procedures for electrical cables and terminations.

a.

(Details, Paragraph 8)

b.

Training and qualification of QA/QC personnel.

(Details,

Paragraph 9)

Observation of cable pulling.

(Details, Paragraph 10)

c.

d.

Conformance of installed piping to drawing and location

requirements.

(Details, Paragraph 11)

Observation of welding in progress, completed welds and

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veld records ; Decay Heat and NuclearService Water lines.

(Details, Paragraph 12)

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B.

Status of Previousiv Reported Unresolved Items

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The following items have been resolved:

1.

Audit of vendor documentation.

(Details, Paragraph 13)

2.

Seismic integrity of supports for Control Rod Drive AC

Breaker Cabinets.

(Details, Paragraph 14)

3.

Modification of reactor internals handling fixture.

(Details,

Paragraph 15)

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Procedure for Qualified Release of nonconforming items.

4.

(Details, Paragraph 16)

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5.

NDE Personnel Qualifications.

(Details, Paragraph 17)

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6.

UT indications on CRD motor tubes.

(Details, Paragraph 18)

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Metal coatings within reactor building.

(Details, Paragraph

7.

19)

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(Details,

Voids in exterior wall of Fuel Handling building.

8.

Paragraph 20)

Exit Interview

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18, 1975.

An exit interview was held at the site on December

Persons Present

General Public Utilities Service Corporation

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R. F. Fenti. QA Auditor

W. T. Gunn, Project Site Manager

R. W. Heward, Project Manager

P. A. Levine, QA Auditor

G. Roshy, QA Engineer

M. J. Stromberg, Sr. Site. Auditor

R. L. Wayne, QA Manager

J. E. Wright, Site QA Manager

United Engineers and Constructors

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G. M. Ahearn, Asst. Project Superintendent

J. Carrabba, Field Supervisor QC

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V. E. Cichocki, Construction /QC Coordinator Superintendent

D. C. Lambert, Field Supervisor QC

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K. Merryman, Safety Engineer

Burns & Roe

W. P. Dornsife, Asst. Project Engineer

F. X. Pindar, Jr.,' Lead QA Engineer

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The items discussed are summarized below.

In each case, the licensee

acknowledged the information.

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A.

Scope of Ir.spection

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the inspection was conducted to review

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The inspecto'r stated that

installation and QC records of safety-related piping; electrical

and the status of outstanding items.

QC procedures and installation;

B.

Enforcement Items

lack of complete documentation for spool

The inspector stated that

piece 2-DH-124 and pipe hangers BSH 88 and 89. is considered to be an ite=

of noncompliance. (Details, Paragraph 2)

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C.

Unresolved Items

The inspector identified the items listed in Part A-1 of Other Sig-

nificant Findings of the Se= mary of Findings and stated that these

items are unresolved.

(Details, Paragraphs 4, 5, 6 and 7)

D.

Acceptable Items

The inspector identified the items listed in Part A-2 of Other

Significant Findings of the Surnary of Findings and stated that

these ite=s are considered to be acceptable. (Details, Paragraphs

8, 9, 10, 11 and 12)

E.

Previousiv Resorted Items

The inspector identified the itc=s listed under Previously

Identified Enforcement Items and Previously Reported Unresolved

Ite=s of the Su==ary of Findings and stated that these items

have been resolved.

(Details, Paragraphs 3, 13, 14, 15, 16,

17, 18, 19 and 20)

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DETAILS

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Persons Conracted

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General Public Utilities Service Cornoration

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R. F. Fenti, Quality Assurance Auditor

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W. T. Gunn, Site Manager

N. Hollerbush, QA Engineer

P. A. Levine, QA Auditor

D. Perry, QA Engineer

G. L. Roshy, Quality Assarance Engineer

M. J. Stomberg, Site Quality Assurance Auditor

J. E. Wright, Quality Assurance Manager

J. H. Wright, Resident Civil Engineer

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United Engineers and Constructors

S. Abbott, Welding Superintendent

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V. E. Cichocki, Construction /QC Superintendent

R. Crofton, Welding Engineer

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B. Glick, Uelder

C. W. Hunter, Electrical Supervisor

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M. Mason, QC Engineer

J . . C. Spinak, Lead QA Engir.eer

Babcock and Wilcox

B. E. Treadway, Project Mancger

R. Kunz, QC Supervisor

D. Larson, Project Engineer

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Conam inapection, Inc.

P. Rentzell, Site Supervisor

K. Hobba, Welding Records Coordinator

J. McKevis, Inspector

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2.

QC Documentation

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The inspector cy.amined the documentation listeo below for selected

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pipe hangers and spool pieces.

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a.

Spool Piece No. 2-CF-7 (Core Flood System)

(1) Receiving Inspection Report No. 92 dated January 6, 1973

which had been signed by Receiving Inspection and the

Authorized Code Inspector.

(2)

M. W. Kellogg (} EGO Company Drawing No. F-1673 for this

14-inch, schedule 160 pipe; A375 Type 304 stainless

part;

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steel; Heat No. 2193-3.

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(3) Material Test Certification from Curtiss-Wright Corporation

providing chemical analysis and physical characteristics

and certifying that this part had been hydrostatically

tested, heat treated and UT examined with no reportable

indications.

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(4) Manufacturers Data Report, Form NP-1 which cc tified

that the design, materials fabrication and inspection

comply with the appropriate chapters of USAS B31.7 and

which was signed by the Authorized Code Inspector.

Docu=entation fdr this item confirmed compliance with the

2555-64.

requirements of the FSAR and B&R specification No.

b.

Spool Piece No. 2-CF-6

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(1) Receiving Inspection Report No. 150, dated February 19,

1973 signed by UE&C Receiving Inspection and the Author-

ized Code Inspector.

(2) MWK Drawing No. F-1672 Rev. 2 wh'ich showed this part to

have been fabricated of the following pieces:

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(a) 14-inch Seamless Pipe; A-376 Type 304; Heat No.

2193-1.

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(b) 14-inch elbow;

A-403 type 304; Heat No. 120855.

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(c)

lb-inch 6000 pound half compling; A-182 Type 304;

Heat No. CF-6.

(d) 6-inch Seamless Pipe; A-312 Type 304; Heat No.

8650361.

(3) Material Test Certifications for each of the above heats

providing chemical analysis, physical characteristics

and other test results.

ReportofRTandPTinspectionresultsforvekdjoints.

(4)

(5) Weld History Records.

(6) Material certifications for consumable insert, and weld

rod.

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(7) Manufacturers Data Report - Form NP-1 which had been

signed by the Authorized Code Inspector.

This documentation confirmed compliance with t e requirements

of the FSAR and B&R Specification No. 2555-64.

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Spool Piece 2-DH-125 (Decay Heat)

c.

(1) Receiving Inspection Report No. 171 dated July 19, 1973

signed by Receiving Inspection and the Authorized Code

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Inspector.

(2) FEnt Drawing No. F-510 which identified the following

pieces:

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(a)

12-inch Scamics: Pipe; A-376 Type 304; Heat No.

2200-1.

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(b)

12-inch Weld ells; A-403 Type WP 304; Heat No.

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150261.

(c)

12-inch x 12-inch x 8-inch reducing tee; SA 403

type WP 304; Heat No. 150566.

06675.

(d). 3-inch pipe; A-376 Type 304; Heat No.

(3) Material Test Certifications for each of the above heats

providir,g chemical analysis, physical characteristics

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and other test results.

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(4) Weld history records and caterial certifications for con-

sumable inserts and weld rods.

(5) Reports of RT and PT inspection results.

(6) Manufacturers Data Report - Form NP-1 which had been

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signed by the Authorized Code Inspector.

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This documentation confirms compliance with the requirements

of the FSAR and B&R Specification No. 2555-64.

d.

Surge Line Assemblies A-80 and A-83

(1)

Assembly Drawings A-80 and A-83 which identified the parts

for each of these 10-inch spool pieces including specifica-

tion and type of caterial and heat numbers for each.

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(2) Material Test Certifications for each heat providing

chemical analysis, physical characteristics and other

tert results.

(3) Weld history records and material certifications for

consumable Inserts and weld rod.

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Manufacturcrs Data Report - Form NP-1 which certified.that

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the design, materials, fcbrication and inspection comply

with the appropriate chapters of USAS B31.7 and which was

signed by the Authorized Inspecter.

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Documentation for these items confirn compliance with the

FSAR requirements.

Spool Piece 2-DH-124_

e.

Receiving Inspection Report No. 135 dated February 14,

(1)

1973 signed by Receiving Inspection and the Authorized

Code Inspector.

(2) ' MWK Drawing No. F-509 identifying the following parts

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and requirements.

(a) 12-inch Seamless Pipe; A-376 Type 304; Heat No.

2200-3.

(b)

1\\-inch x 3/4-inch x 3-inch Lor g Lugs; Type 304

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stainless steel; Heat No. 610621.

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The drawing showed the pipe to be bent and established

(c)

requirements for heat treatment after bending,

maximun ovality and vidigage wall thickness measurements.

(3) Material Test Certifications for the above items.

Weld history records and material certifications for weld

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(4)

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rod.

(5) Report of PT inspection of welds.

2ers Data Report - Form NP-1 signed by the

(6) Manufat

Authorized Code Inspector.

MWK Drawing No. 2551 Rev.1 which had been issued for

(7)

reeleaning of this spool piece and also provided UT

measurements of the outer periphery of the bend.

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The inspector observed that records of post-bending heat

included

treatment, ovality and vidigage measurements were not

with the documentation package.

Prior to completion of the

inspection, the inspector was furnished a copy of Drawing No.

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F-509 which showed ovality measurements and stated that an

treatment chart was available at the 115; plant

approved heat

these

and F-523 showing vidigase measurements and stating that

measurements would be forwarded to B&R for review.

f.

_ Hangers. Nos. BSH 88 and BSH 89 (Building Snray System)

79380 which had

(1) Receiving Checklist / Inspection Report No.

been signed by Receiving Inspection.

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Certifications which provided chemical and

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Material Test

(2)

physical data for the material in the 3/8-inch thick x 5-

inch x 14-inch lugs which had been attached by FGS; to the

assembled hangers furnished by Bergen - Patterson.

A Certification of Compliance from NWK dated March 6, 1975

(3)'

which states that the pipe assemblies listed on Packing

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List No. 165-W conforms to the requirements of B&W Spec-

ification No. 2555-64.

On the same letter, a Release for Shipment Statement had

been supplied by UE&C. This statement referenced the

same packing list, states that review and approval of

Mill Test Reports related to fabrication of the pipe

assemblies has been completed. The inspector requested

Packing list No.165-U or some means identifying the

This information

hangers listed on that Packing List.

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was not available.

The QA Engineer later provided a Certification of Compli-

ance from Bergen - Paterson which referenced an 155; pur-

chase order and stated that hanger material furnished

under that order is in accordance with the applicable

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governing codes and job specifications.

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Release for construction of spool piece 2-DH-124 and

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hangers BSH-88 and BSH-89 without complete documentation

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is considered to be a deficiency with respect to 10 CFR

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50, Appendix B, Criterion VII which states, in part:

"... Documentary evidence that material and equipment con-

form to the procurement requirements shall be available

at the nuclear power plant site prior to installation or

use of such material and equipment..."

3.

Chemical Requirements for Grout

Failure to verify confor=ance to ASME III, Division 2 for chloride

and nitrate content of freshly mixed grout had previbusly been

identifica as a Deviation.

(Inspection Report 75-08)

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The information shown below is for the grout material previously

used and still in use for tendon grouting.

a.

Admix

The admix used is Sika DP-23-3 (now known as Sikamix 122,

Grout Aid). The inspector examined a letter from Mr. Cordon

N. Scott, Consultant to B&R stating that this admix.has been

studied with respect to possible corrosion of the tendons and

that there need be no concern about the chemicals in the grout

for this application.

At the request of the inspector, the

licensee telephoned the chief chemist of Sika Chemical Corpora-

tion and was infor=ed that this admix contains no chlorides or

nitrates.

b.

Cement

A general analysis of the cement (Medusa) furnished by the

manufacturer shows chloride centent to be .003 .103 parts per

million (PPM). Test reports of cement sa ples taken period-

ically at the site during April - Nove=ber 1975, show chemical

content to be consistent with the general analysis.

A Pittsburgh

Testing Laboratory report of their analysis of a sample re-

cently taken at the site shows .01 PPM of chlorides and less

than .001 PPM of nitrates and sulphides.

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Water

The licenses stated that water used in the grout.is from a

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treated municipal supply and their routine analyses show

negligible amounts of chlorides and nitrates.

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This item is resolved.

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4.

Control of crimpine Tools

The inspector reviewed B&R Specification No. 2555-70, " Electrical

Equipment Installation."

Tables 1 and 2 of Paragraph 3.1.1.2.c, Section 16A of Division 16

and Paragraph 3.1.2 of Section 16D define the compressign require-

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ments for various sizes of cable and wire.

Paragraph 16D requires

compliance with the latest addenda of IEEE 336-1971.

Section 4 of IEEE 336-1974 requies that harduare shall be installed

in accordance with:

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Drawings,

b.

Manufacturers Instructions.

Installation Specifications (In this case B&R Specification

c.

2555-70)

and also that " Care shall be especially exercised in following the

provisions of the above documents for operations such as," ... In-

cluded in such operations is cable terminations. .

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Item 4 of Paragraph 5.11 of IEEE 336-1971 establishes the require-

ments for tightness of connections and f astenings.

The licensee

was unable to furnish to the inspector any

procedures for con-

trol, periodic calibration or visual ~ inspection of crimping tools

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used on cable and wire terminations which would be ensential for

compliance with the above requirements.

This item is unresolved.

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Ir stallation of Cable Tray and Conduit Hanners

2 DC 87 for confor-

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During inspection of installation of conduit

marce to E6R Drawing No. 3174-1 Rev. 7, the inspector observed

white tags on the hangers indicating that the hangers were a

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Observation of installed cabic trays and

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tem 3orary installation.

other conduits shoved a large nurber of temporary hangers to

have been installed.

Approximately fifty such temporary hangers

have been int .alled on safety-related systems.

The QC check-off

lista showed that these cable trays and conduits

have been

released for cable pulling in accordance with appro' ed B&R Drawings.

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Howeser, hanger installation is in accordance with the sketches

been reviewed by B&R and uhich are

prepared by UE&C which have not

not shown on the released B&R drawings.

It was noted that the QC check-off lists do indicate that the

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Also the inspector noted that

hanger installation was temporary.

a proesdure (UE&C ECP/8-2 Rev. 13) ha.d been issued which permits

the use 6f temporary hangers on a limited basis. However, the

number of white tags observed on installed hangers indicates that

use of temporary hangers is the normal practice rather than an

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.occ.asional deviation.

GPU site audit report dated December 11, 1975 had identified the

same prcblem and the inspector uas inf ormed that a meeting had

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been scheduled for Deccaber 19, 1975 to resolve the apparent

contradiction in requirements.

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This item is unresolved.

6.

Temperature Conditi_oning of Cables

B&R Specification 2555-70 requires conformance to vendor installa-

The cable vendor's instructions

tion and bandling requirements.

for "Movenent, storage and installation" of cabic states in para-

to a warm area (70 F,

graph C " Move the reel, avoiding impact,

for eighteen (18) to twenty-four (24) hours is probably a good

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safe temperature) to condition the cable" prior to cable pulling.

QC procedures and check-off sheets do not.have any requirements

for cabic conditioning prior to cable pulling.

This item is unr-solved.

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Tolcrance-Incident Angle Ectueen Pine Socols

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inspection of decav heat oinc line.. it

During the

field wcld joint DH-128Q between spool piece No.

was noted that

DH 128 and Reactor Euilding penetration No. 525 vas a mitered

The inspector asked site QC personnel what the alignment

joint.

The inspector was

acceptance criteria were for mitered joints.

referred to the Burns and Roe

Specification No. 2555-75,

which addresses piping welding, fit-up and other cechanical

Division 15, Section ISD, Paragraph 4.2

component. installation.

inches and larger

states, " Erection of shop fabricated pipe 2

shall be in accordance with the Nuclear Power Piping Code ASSI

31.7 1969."

B&R Drawing No. 2077 Revision No. 7 provides details

tolerances, which are in accordance with Figure

of alignment

1-727-3.1 of ANSI E31.7 1969.

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in numerous instances

Discussions with site personnel indicated that

due to normal fabrication sequences,there was an angle between

the closure joint.

The inspector

centerlines of the components at

asked what angular tolerances were considered acceptable and when

The inspector was

a Deficiency Report was required to be issued.

provided specific acceptance criteria

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informed that the A/E had not

The licensee stated he would have the A/E

for such conditions.

evaluate this matter and provide acceptance criteria for site use.

This matter is considered unresolved pending evaluation and issuance

of more definitive acceptance criteria for these types of joints.

QC Procedures - Electrical Cables and Terminations

8.

The inspector reviewed UESC procedures as listed below for handling,

inspection and testing of electrical wire

storage, installation,

and cable.

Electrical Construction Procedure (ECP) ECP-3-2 for Receiving,

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a.

Storing, Handling and Installing Uire and Cable Rev.

dated December 1, 1975.

This procedure defines the QC require-

ments for inspection and record keeping during receipt.on site

storage, identification and docu=entation of qualifica' tion

tests.

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This procedure also establishes the requirements for cable

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handling and installation; inspection of conduit and cable

trays; cable identification, color coding, separatian and

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redundancy ; and wire.vay loading.

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TMI TP 250/2 " Testing and Checking of Mechanical and Electrical

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b.

Equipment" Rev. TCN-3 dated November 6,1975 ubich catablishes

the requirements for testing and terminations of cables.

QC Procedure QC-2-2 Rev. 6 dated May 14, 1975 which provides

c.

color

requirements for inspection of cable identification,

coding, termination and segregation and control of noncon-

forming materials.

Procedure ECP-5-2, Rev. 10, dated December 1, 1975." Receiving,

d.

Storage, Handling and Installations of Wire and Cable," which

establishes the requirements for wire-way separation, size,

type of cable, routing and protection including specification

of materials for fire barriers and wireway seals.

Procedure ECP-8-2, Rev. 3 dated August 29, 1974 " Quality Sur-

e.

veillance Plan," which defines requirements for inspection con-

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trol of changes to established specifications.

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Except as indicated in paragraphs 5 and 6 abcve, this item is

considered to be acceptable.

9.

Training and Qualification of OA/0C Personnel

_

The inspector reviewed UELC Procedure QC-29-2, Rev. 3, dated April

18,1975 " Quality Control Personnel Training and Qualification."

This procedure requires that orientation and indoctrination of a

new employee be performed, evaluation of the employee's perf ormance

be made within 30 days and again within one year.

The inspector

examined personnel records of three UESC employees and found that

in cach case the orientation, indoctrination and performance evalta-

tion had been performed.

The inspector also examined audit records

of personnel training and qualifications as follows:

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14, 1975 which

GPUSC Audit Report 75-05 dated February

showed documentatica of evaluation of three QC inspectors

a.

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by a QC Engineering Report.

75-24 which documenced review of qualifica-

b.

GPUSC Audit Report

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tions of two Conam inspectors.

.

75-14 dated April 5,1975 which reported

GPUSC Audit Report

that qualifications of NDT personnel were current and satis-

c.

factory.

This item is considered to be acceptable.

10.

Cable Pulling

E25VDC

The inspector witnessed pulling of four safety-related

supply system cables; cable' circuits and conduits are shown be-

low;

2DC-87.

Cable Circuits 2DC-88 and 12DC-89 in Conduit

a.

Cable circuits 2DC-85 and 2DC-86 in conduit 2DC-85.

i

b.

the current of the

A calibrated current meter was recordingFor this pull, the current reading of the

cable pulling motor.

The maximum reading on the two

motor was requ, ired not to exceed 15 amps. Prior to pulling the cables

pulls witnessed wrs le. ; than 7 amps.through the conduit a vacuu

fish was pulled through to assure that no burrs were in the con-

procedure is in accordance with UE&C Procedure

duit.

This

Wire

ECP-3-2 for Receiving, Storing, Handling and Installing

10.

.

and Cable, dated December 1,1975 Rev.

This item is considered to be acceptable.

.

,

11.

Piping Installation

The inspector visually inspected the main ranctor coolant loop pipe line

B-44-1 (RC pump 1B/A to the RPV) & the decay heat pipe line from reacto

It was

coolant pipe line A-32-1 to the No.1B decay heat pump.

found that the pipe lines, were run and connected as described in

the FSAR with redundant connections provided as co=mitted in the

Pipe spools pieces, fittings, and hangers (where cc=plete)

in accordance with isometric and

FSAR.

were installed

The following is an listing of pipes inspected,

layout drawings.

inspection.

responsible contractor, and drawings used for the

(

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.-

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-17-

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.

a.

Line:

RC B-44-1 (RC Pu=p 1B/A to RPV)

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.

.

Contractor:

Babcock and Wilcox

.

.

Applicable Drawings: " Location of Field Welds for Reactor

"

Coolant System"

.

Drawing No. 4467 Rev. 4

Change Notice No. 2832 Rev. 2

Comments :

It was observed that the reactor coolant pipe

B-44-1 was installed in accordance with the

applicable drawings and change notices.

Reactor

coolant pipe restraint CP-2 was installed and

modified in accordance with change notic.e 2832.

B&W Inspection Report documented visual inspec-

tion of restraint CP-2 as satisfactory (It.spected

9/12/75). B5W docu=entation (Field Construction

Procedure No. 13) found the installation of B-44-1

'

acceptable.

.

b.

Line:

Decay Heat 12", (Hot Leg of "B" Generator to

Second Isolation Valve DR-V2)

Contractor: Babcock and Wilcox

Applicable Drawings: Piping Isometric Drawings 2-8-23,

2-8-24 and 2-8-25.

Hanger Sketch A-9459-FS-02-HS-DH HH-1

Figure 9.2-3 of the FSAR

Comments: The 12-inch diameter decay heat removal system

piping was installed in accordance with the

applicable sketches, drawings and FSnR cccmit-

ments. Pipe Hangers DHH-102, DHH-104, DHH-105

and DHH-107 vere located as shown on the appli-

cable drawings.

c.

Line:

Decay Heat (DH-V2 through Reactor Contain=ent

to Decay Heat Removal Pu=p DH-P-13)

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Centractor: United Engineers and Constructors

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s

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Applicable Drawings: Piping Isometric Drawing 2-8-1, 2-8-2

3

and 2-8-3.

.

FSAR Figure 9.2-3

The piping was ' installed and welded between the

,

termination points outlined. Pipe hanger and

Comments:

support installation was not complete and no

attempt was made to verify hanger and support

All fittings and field welds were.

location.

installed and visual appearance of the finished

field weld surfaces was considered acceptable.

Cross connection between the decay heat pumps

DH-P-1A and DH-P-1B was provided for redundant

'

operation.

.

,

This item is considered to be acceptable.

12.

Observation of Field Welding

The inspector witnessed the field welding of three welds in three

systees and examined the as welded final condition and

reviewed the supporting documentation for one completed weld.

different

e

Welding operations observed and records audited indicated that the

velding was performed in an acceptable manner.

Table of Weld Joints Witnessed emd Data Reviewed:

a.

_C) served Conditions

'

Joint

Completed weld surface excmined'.

'

2-DH-171 (Decay Heat)

No undercuts or visual discon-

8" diameter, Nuclear

tLauities. Weld transition to

.

Class I

valve body meets 3:1 taper spec-

Schedule 160 pipe

ified by ANSI N31.7 - 1969.

Butt Weld

Reviewed quality records.

'

Weld joint approximately one-half

2-DH-92C (Decay Heat)

Observation of the work

complete.

8" diameter, Nuclear

found the in. process veld appear-

Class II

ance acceptable. The craftsman

Schedule 40 pipe

was using the prescribed weld

Butt Weld.

filler material (3/32" ER 316L).

-

!

C. 1

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-19-

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.

.

Joint

Observed Condition

'

The file used for veld bead

surface conditioning was marked

-

'

for stainless steci use in

accordance with the site pro-

-

cedures.

GTAW procedure was

used (UE&C Procedure No. 20

and 8), the inspector verified

that the welding amperage,

shield gas and purge gas were

in accordance with the proced-

ure. Weld History Record For=

7005 was completed co==ensurate

with status of the weld and as

required by QC-8-2 Revision 4.

2-NS-42 (Nuclear Services

Veld joint flush, welder in

Closed Cooling Water)

process of removing porosity

3" diameter

from surf ace to correct the

Schedule 40

condition prior to co=pleting

Butt Weld

the weld.

Filler metal 7018

electrode in use, was controlled

within the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> time span

(issue to use). UE&C weld -

Procedure No. I was in use and

~ was appropriate for base materials-

being welded.

139-C-6 (Make Up System)

Completed surface of first pass

"v Nuclear Class II

of fillet weld.

Shielding gas

Schedule 160

flow and filler metal 3/32" ER

Fillet Weld

30SL acceptable and in accord-

ance with UESC welding procedure

No. 20 and 8.

Weld History

Record available and co==ensurate

with status of weld.

.

.

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4

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3

b.

Welder Qualification

I

the three

Reviev of UE&C and B&W site records showed that

welders performing the welds and the two welders who had

,

?

perforced the completed weld were qualified as required by

The welders whose

.

the applicable codes and site procedures.

qualification records were examined are as follows:

Welders Symbol

Contractor

Joint

B&W

2-DH-171

5049 and 3835

UE6C

2-DH-92C

5B

UE&C

2-NS-42

23-F

UE&C

139-C-6

20S

,

.

NDE Personnel Oualification

c.

The inspector audited B&W site records documenting the qualif-

ication and annual vision checks for the two NDE examiners

It was found

who'had performed tests on joint 2-Dd-171

that the NDE personnel were properly qualified to perform the

liquid penetraat and radiographic examination of weld DH-171

i

(Level 11 SNT-TC-1A as applicable) .

Weld Material Certification - Joint DH-171

d.

The inspector audited QC records for ene heat of weld filler

metal (3/32" E 316; Heat No. 6343B) which was certified by

the requirements of AWS A5.4-69.

the manufacturer to meet

The manufacturer's chemical analysis and physical tests of

the re-

as deposited metal were reviewed and found to meet

quirements of AWS A5.4-69.

,

This item is considered to be acceptable.

13. Vendor Documentation

Lack of documentation on site to validate the integrity of certi-

the vendor facility had been

fication of acceptance inspection at(Inspection Report 74-06)

identified as an unresolved item.

.

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-21-

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the

The inspector examined a report of a documentation review at

Documen-

Barberton and Lancaster, Ohio.

vendors plants at

-

tation examined pertained to the reactor internals, steam generators,

feedwater piping, reactor coolant surge and spray piping and control

?

Documentation included process sheets,

rod drive motor housings.

weld histories, welder qualification records, welding procedure

qualifications, weld inspection records, weld material

test re-

Th'e report

ports, NDE personnel qualifications and radiographs.

concluded that satisfactory evidence of adequate documentation

exists to support vendor certification for the equip =ent.

.

This ites is resolved.

14.

Seismic Integrity of CRD AC Breaker Cabinets

15, 1975 the licensee reported"a deficiency

.

By letter dated January

in design of the structural supports for the Control Rod Drive AC

Breaker Cabinets.

The lic~ensee stated that modification of these supports had been

completed and.the inspector examined the following documents:

27, 1975

Engineering Change Memo (ECM) No. 278, dated May

which provided details for a revised.sppport pad and attach-

a.

ments for this cabinet.

-

b.

Concrete placement check out sheet daced October 30, 1975

which was signed off:.by Field QC on October 31, 1975.

sheet dated October 31, 1975

Inspector's concrete check out

c.

which referenced ECM No. 278.

.

d.

Concrete Status Report dated October 31, 1975.

'

Reports of placement, batch plant inspection, curing and

e.

concrete cylinder tests.

This item is resolved.

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77

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15.

Reactor Internals Handling Fixture

'

A requirement for modification of the reactor internals handling

fixture had previously been identified.

(Inspection Report 75-01)

j

~

The licensee stated that modifications to this fixture had b;en

made at the Barbert on, Ohio shop of B&W.

The inspector examined B&W Field Change (FC)-41 Rev. 1 dated April

3,1974 for modification of the Handling Adaptor Pendant and Field

Construction Procedure No. 245; Item 4.1.3 which showed that QC

had verified satisfactory completion of this work.

FC-41 provides for the modification authorized by B&R Field Change

Request No. 29.

,

This item is resolved.

16.

Qualified Release of Nonconforming Items

Lack of an adequate B&W procedure for control of " Qualified Release"

of nonconforming items had.previously been identified as an un-

resolved item.

(Inspection Report 75-02)

The inspector examined B&W Procedure 9A-107-1/C-6 Rev. I which

established a procedure for " Qualified Release" of nonconfor. sing

items and established a requircaent that approval of the Owner /

Agent be obtained in writing for release of such items.

.

This item is resolved.

17. NDE Persot ,el Oualification

Incomplete information and inconsistencies in eye correction

limitations had previously been identified as an unresolved item.

(Inspection Report 75-10)

'

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4 5 9

I)

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-23-

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The inspector examined personnel qualification records of NDE

personnel particularly with respect to eye correction limitations.

.

Forms were complete for all. personnel and were found to be

j

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acceptable.

,

This item is resolved.

18.

UT Indications on CRD Motor Tubes

On August 24, 1975, the licensee reported observations of UT

indications on CRD motor tubes during pre-service inspection and

stated that a further 12vestigation sould be made.

The inspector examined a letter dated December 10, 1975.from Conam

Inspection, Incorporated which reported the results of a trip by

two Conam Level II inspections at GPU request.

The purpose of the trip was to analyze the UT indications noted

during examination of the CRD motor tubes and determine if these

indications were actual cefect conditions.

As a result of their analysis it was concluded that the indications

were due to irregular geometry of the part in sc=e locations and

enlarged grain structure in others but were not indications of

actual defect conditions.

'

The report did recoc=end certain modifications to the in-service

inspection procedure which the licensee said would be followed.

This item is resolved.

.

19.

Metal Coatines within Reactor Building

The licensee had reported by letter dat'ed August 26, 1975, defec-

tive coating on cable trays within the reactor building. During

a previous inspection (Inspection Report 75-13) the inspector had

reviewed corrective action which had been completed except for

completion of a review of all coatings within the reactor building.

The inspector examined:

.

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B&R Specification '555-85 Amendment No. 6 dated June 25,

-

a.

1975 " Nuclear Area Cleaning and Coating of all Steel and

'

Equipment."

Field Change No. 2 to Construction Procedure CCP-12-2 which

b.

-

established the requirements for high tempetature aluminum

paint on certain NSSS equipment.

Inspection Reports No.

3549, 3550, 3559, 3560 and 3561

f 6r cleaning and painting of equipment within the reactor

c.

bu 1 ding.

17, 1975 from QC to QA_ stating that as

Memo dated December

d.

in-

date QC had inspected the coatings of all itect

of that

side the reactor containment requiring coatings and had docu-

-

mented either a satisfactory or unsatisfactory inspection

.

report.

This item is resolved.

Voids in Exterior k'all of Fuel Handing Building

20.

(

By letter dated Nove=ber 14, 1975, the licensee had reported a

void in the south exterior wall of the Fuel Handling Building.

The inspector examined the following documents:

(DR1 No. 0522 dated October 16,19 75 which

Deviation Report

described the deviation and provided for B&R to issue an

a.

-

Engineering Change Meme (ECM) for its repair.

ECM No. 3140 which provides a repair procedure using epoxy

in area 1 and an epoxy bonding agent plus concrete in area 2.

b.

Inspection Reports No . S-2903, S-2910 and S-2926 for grouting,

chipping, cleaning,and inspection of the work.

c.

The inspection report documented the satisfactory completion of

void repairs.

This item is res*olved.

.

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