ML19220B784
| ML19220B784 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 01/08/1975 |
| From: | Folsom S, Gage L, Heishman R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML19220B776 | List: |
| References | |
| 50-320-74-09, 50-320-74-9, NUDOCS 7904270345 | |
| Download: ML19220B784 (10) | |
See also: IR 05000320/1974009
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U.S. ATC:!IC E!:ERGY CC:MISSIO::
DIRECTORATE OF REGUIATORY OPERATIOliS
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REGIO:1 I
EO Inspection Report 1 o:
50-320/74-09
Docket I o:
50-320
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CPPR-66
Metropolitan' Edison Co:pany
License !!o:
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Licensec:
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Box 542
Priority:
A
Reading, Pennsylvania 19603
Category:
Middletown, Dauphin County, Pa. (Three Mile Island 2)
Location:
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Ty[eofLicensee:
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Routine, Unannoun:M
Type of Inspection:
18-20, 1974
Dates of Inspection: December
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October 22 and 23,1974
Dates of Previous Inspection:
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Reporting Inspector.:
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Seth. A. Forsom, Reactor Inspector
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Accompanying Inspectors:
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L. W. Cage, Reactor Inspector
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Other Accompanying Personnel:
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Reviewed By:
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R. F. Heishman, Senior _ Reactor Inspector
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SUMMARY OF FINDINGS
Enforecuent Action
centact with the uninsulated
Storage battery cells were found in direct
This is in violation
racks.
metal side reils of the battery support
FR 50, Appendix B.
(Details,
1.
of site directives and Criterion V of 10 C
Paragraph 2)
k
structure reinforcing steel was heated to an un nownh prior to wire
temperature with an oxy-acetylene cutting torcThis was in
Contain=ent
V of
2.
ing.
(Details, Paragraph 3)
field stick
Superseded drawings were f ound in significant nu=be
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d
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3.
files. This
and Criterion VI of 10 CFR 50, Appendix B.
t Matters
Licensee Action on Previous 1v Identified Enforcemen
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the inspection.
The control of weld filler caterial was resolved dur ng
.
(Details, Paragraph 5)
Des'ign Channes_
None identified
Unusual Occurrences _
.
None identified
.
Other Sienificant Findings
Current Findings
d no deficiencies
A.
The f ollowing were examined during the inspection, an
1.
were identified.
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Seismic qualification records for installed instrumentat on
a.
and controls,
Seismic mounting of installed electrical equipment.
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b.
Storage of instrumentation in the control room.
c.
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acceptance
Battery inspection results were not being related to
2.
(Details, Paragraph 12)
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criteria.
Installed switchgear was not being protected from cement dust,(Details, Parag
and environmental conditions were not defined.
3.
13)
Status of Previcusiv Rennrted Unresolved Items
B.
The f ollowing ite=s were resolved during the inspection:
1.
oly replacement.
Control red drive undervoltage trip
a.
(Details, Paragraph 6)
ODetails, Paragraph 7)
Spent fuel pool siphon breakers.
b.
(Details, Paragraph 8)
Station battery storage.
c.
(Details ,
Steam generator access control and cleanliness.
d.
Paragraph 9)
(Details ,
ASTM material designation in FSAR tabulation.
e.
.
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Paragraph 10)
f.
Audit close-out records.
(Details, Paragraph 11)
Management Interview
20, 1974, with
The manage =ent interview wa's held at the site on December
the following personnel in attendance:
General Public Utilities Service Company
Mr. R. F. Fenti. Quality Assurance Auditor
Mr. G. L. Kopp, Quality Assurance Auditor
Mr. M. J. Stronberg, Site Quality Assurance Auditor
Mr. W. T. Sturgeon, Quality Assurance Auditor
Mr. R. J. Toole, Test Superintendent
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Site Quality Assurance Manager
Mr. J. E. Wright,
Mr. J. H. Wright, Resident Civil Engineer
United Entineers and Constructors
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Mr. V. E. Cichccki, Quality Assurance / Quality Control Superintendent
Mr. D. C. lanbert, Field Supervisor Quality Control
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Burns and Roe
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Mr. T. R. Block, Site Quality Assurance Engineer
Mr. G. T. Harper, Jr., Site Project Engineer
The following was discussed:
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telecepies nay now be transmitted to Region
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1.
The inspector stated that
1 on a 24-hour, seven-day basis by dialing (215) 337-1159.
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The regular telephone service to RO I continues on a 24-hour, seven-day
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basis by dialing (215) 337-1150.
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The licensee agreed to provide this inf or=ation to all concerned.
2.
The licensee agreed to the inspector's request to ba notified when the
into sections
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grouted 170-foot prototype tendon sheath had been cut
for examination.
This ite= is unresolved.
3.
The licensee agreed to the inspector's request to have all records
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available at the site in January 1975 which demonstrated the validity
This
of certificates of confor=ance on vendor-supplied cc=ponents.
ites rc=ains unresolved.
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4.
The inspector stated that the following previously reported items hal
been resolved:
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Control of weld filler material.
(Details, Paragraph 5)
a.
b.
Control rod drive undervoltage trip asse=bly replacement.
(Details ,
Paragraph 6)
Spent fuel pool siphon breakers.
(Details, Paragraph 7)
c.
d.
Station battery storage.
(Details, Paragraph 8)
Steam generator access control and cleanliness.
CDetails, Paragraph
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e.
9)
ASTM mater..a1 designation in FSAR tabulation.
(Details, Paragraph
4
f.
10)
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g.
Audit close-out records.
(Details, Paragraph 11)
The licensee acknowledged this information.
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5.
The inspector stated that Inspection Report No. 50-320/74-07, Current
Findings, 1tes 1, had reported that the possible generic deficiency
in the Emergency Power Diesel generator was considered " reportable."
This should have read "not reportable". The licensee ccknowledged
this inf or=ation, and stated that the vendor's examination of the
Diesel parts at the site had confirmed their previous judgement
concerning reportability.
The inspector stated that this item would
rc ain unresolved pending his exacination of the documentation on
this catter.
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6.
The' inspector stated that the f ollowing violations had been identified
during the inspection:
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Storage battery cells in contact with uninsulated battery support
a.
racks.
(Details, Paragraph 2)
b.
Reinforcing steel heated to unknown temperatures with an oxy-
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acetylene torch.
(Details, Paragraph 3)
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c.
Superseded drawings found on field stick files.
(Details, Paragraph
4)
The licensee acknowledged this information.
7.
The inspector stated that he had exa=ined the following, and no non-
conformances had been identified.
a.
Seismic qualification records for installed instrumentation and
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controls.
,
b.
Seismic =ounting of installed electrical equipment.
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c.
Storage of instrumentation in the control room.
The licensee acknowledged this information.
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8.
The inspector stated that the following items had been observed, and
were considered to be unresolved:
a.
Failure to interpret results of battery inspectior.s.
(Details,
Paragraph 12)
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b.
Failure to protect installed switchgear.
(Details, Paragraph 13)
The licenste acknowledged this information.
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9.
The inr.pettor stated that he had been notified by the li.censee on
Dececher 16, 1974 that the seis-it integrity.of the control red AG
breaker cabinet countings vas being re-evaluated.
This item it.
unresolved.
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10.
The licensee stated that some concrete strength tests re=ained on
the investigation into possible sub-standard cement used in a portion
of the contain:ent concrete.
This item re=ains unresolved.
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DETAILS
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1.
Persons Contacted
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General Public Utilities Service Cc=cany
Mr. R. F. Fenti. Quality Assurance Auditor
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Mr. C. L. Kopp, Quality Assurance Auditor
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16. P. Levine, Quality Assurance Engineer
Mr. M. J. Stro= berg, Site Quality Assurance Auditor
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Mr. W. T. Sturgeon, Quality Assurance Auditor
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Mr. R. J. Toole, Test Superintendent
Mr. J. E. Wright , Site Quality Assurance Manager
Mr. J. M. Wright, Resident Civil Engineer
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United Engineers and Constructors
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Mr. R. T. Carlson, Startup Test Engineer
Mr. V. E. Cichocki, Quality Assurance / Quality Control Superintendent
Mr. D. C. Lambert, Field Supervisor Quality Control
Mr. R. Liscom, Quality Control Engineer, Elcetrical
Mr, F. F. Long, Assistant Supervisor, Structural Quality Control
Eurns and Roe
Mr. T. R. Block, Site Quality Assurance Engin:-er
Mr. G. T. Harper, Jr. , Site Project Engineer
Mr. F. I. Pindar, Electrical Quality Assurance Engineer
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United Scale Models
Mr. C. E. Powers, Model Group Leader
2.
Storage Battery Cells in Contact with Racks
The inspector examined the storage battery installation and found that
several of the scorage cells were in direct contact with the uninsulated
metal side rails of the battery support racks.
This was contrary to
the constructor's site procedure ECP4.2, Paragraph 5.2.1, which states
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" Cells should not touch each other nor should any cell touch metal
sup;2rts of the rack."
The licensee's representatives later agreed
that the installation drawings required plastic insulation strips on
the side rails in addition to the bottes rails.
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The f ailure to provide the insulating strips was a vio.lation of
Criterion V,10 CFR 50, Appendix B, and the licensee's FSAR, Paragraph
17.1.5.4.
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3.
lleating Reinforcine Steel to Unknown Temperaturcq
The inspector found a large nudber of No. 18 reinforcing steel bars
in the containment structure being heated with an oxy-acetylene torch
preparatory to scratchbrush cleaning.
The =cchanics adnitted that
they should have been using Tempilstiks to indicate the rebar temperature.
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When this work location was rechecked by the inspector later in the day,
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Tempilstiks were being used.
The constructor'c procedure QC-1-2, Appendix B, Revision 5, July 13,
1973 limits the preheating temperature of rebar to 212-300'F prior to
scratchbrushing.
This is a violation of Criterion V,
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4.
Drawing Control
The inspector randomly selected 43 drawings on field stick files.
The
selection included electrical, piping, and structural drawings.
The
revision nu=ber of each of the 43 drawings was compared to the latest
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revision nu=ber listed in the Engineering office card file.
Four of the
43 drawings (9.3%) on the stick files were found to be out of date.
This is a violation of Criterion VI of 10 CFR 50, Appendix B.
5.
Control of Weld Filler Material
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In a previous inspection, a violation in weld filler material control
was identified by the inspector. The licensee has instituted corrective
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action which was examined by the inspector, including re-instruction
of issue crib attendants, nu= bering of all electrode containers, increased
efforts on controlling electrode stubs.
The inspector examined the
corrective action, and audited field locations for the eff ectiveness
of the control =easures, and no deficiencies were identified.
ite= is resolved.
This
6.
Control Rod Drive Undervoltage Trio Assembly Coil Replacement
Documentation was examined by the inspector which showed that all CRD
undervoltage trip assembly coils had been replaced.
The documentation
included:
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Certificate of Conformance frc= Diamond Power 9/10/74
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B&W Field Correspondence 9/18/74.
This item is resolved.
7.
Spent Fuel Pool Siphon Break
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A siphon break has been installed in the spent fuel tank fill line.
The inspector examined the 1/2 inch hole drilled for this purpose.
The drawings show the hole to be located 6 inches b low the normal
water level.
This item is resolved.
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8.
Station Eatterv Charcine in Storace
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Prior to installation the station batteries were stored in a warehouse
and the charging schedule specified by the vender was not followed.
The vendor's reccamended re-charging recommendations were then obtained
and implemented.
The inspector examined the re-charging and subsequent
records, and no deficiencies were identified.
This item is resolved.
9.
Steam Generator Access Control and Cleanliness
The inspector examined the following documentation on the corrective
action taken on major equipment access control and cleanliness require-
ments.
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B&W Access Control QC Procedure 9A-127/C-6, Revision 4, September
a.
4, 1974; covering scope, responsibilities, zone classification,
clean areas, restriction list.
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b.
B&W, Cleanliness Requirement QC Procedure 9A-128/C-6, Revision
5, Septe=ber 4, 1974; defining classes of cleanliness, methods for
achieving described cleanliness, scope, responsibilities.
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This item is resolved. .
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10.
ASTM Material Designation for FSAR Tabulation
The FSAR Table 9.2-5 has been revised (Amendment 16 June 18, 1974) to
list "shell material - carbon steel ASTM ASIS, Grade 70" and is new
in accordance with Burns & Roe Specification 2555-25, Table 3.
Thi=
item is resolved.
11. Audit Close-Out Records
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At a previous inspectiet, the inspector found two audit: closed out
where correctlya uction had not been completed.
The Audit Status Report
dated NovaT;er 26, 1974, Attachrrat A Page 10, has been revised to show
Audit Rwports 74-18 and 74-49 still opcn.
This item is resolved.
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12.
Batterv Insocetion Results
The inspection records for the storage battery room were reviewed.
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inspector fcund that
The
were not being cc= pared to allcwable values.the periodic specific gravity
The licensee could not
explain how these readings were being cvaluated, but
detailed information in the data sheets and/cr procedure thatagreed to provide
assure the evaluation of these reading.
This iten re=ains unrescived.
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13.
Protection of Installed Switchgear
The room in which 4KV switchgear was installed was examined.
inspector found an accumulation of cement dust
The
on the switchgear.
Scall electric heaters were pieced en the floor of two ,f the cabinets
and a small ( pound) bag of dessicant had been placed on the floor
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of each cabinet.
devices for te=perature and humidity to provide evidence thatT
envircnment was satisfactorily controlled.
the
The switchgear vendor's instructions for equipment storage
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in the architect-engineer's Equipment
contained
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Specification 2555-23, Paragraph
111.6.3, Novc=ber 1971, " Indoor switchgear which cannot be. . . . put
in service i=nediately should be stored in a dry, clean place, preferab
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indoors in a heated building.
in temperature, cement dust and corrosive at=osphere should bCond
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against."
atmospheric values and tolerances.The switchgear vendor's instructions did
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This item remains unresolved.
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