ML19211C681
| ML19211C681 | |
| Person / Time | |
|---|---|
| Site: | Calvert Cliffs |
| Issue date: | 12/31/1979 |
| From: | Grier B NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Lundvall A BALTIMORE GAS & ELECTRIC CO. |
| References | |
| NUDOCS 8001140192 | |
| Download: ML19211C681 (1) | |
Text
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- o UNITED STATES 8
k NUCLEAR REGULATORY COMMISSION 3
p REGION I 631 PARK AVENUE
,o',c KING oF PRUSSIA, PENNSYLVANIA 194o6 Docket Nos. 50-317 50-318 DEC 31 Jg79 Baltimore Gas and Electric Company ATTN:
Mr. A. E. Lundvall, Jr.
Vice President, Supply P. O. Box 1475 Baltimore, Maryland 21203 Gentlemen:
This Information Notice is provided as an early notification of a possibly significant matter.
It is expected that recipients will review tre infor-mation for possible applicability to their facilities.
No specific action or response is requested at this time.
If NF2 evaluations so indicate, further licensee actions may be requested or requiced.
If you have questions regarding this matter, please contact this office.
Sincerely, hhN i
g?vBoyceH.Grie T
Director
Enclosures:
1.
IE Information Notice No. 79-37 with attachments 2.
List of Recently Issued IE Information Notices CONTACT:
L. E. Tripp (215-337-5282) cc w/encls:
R. M. Douglass, Manager, Quality Assurance L. B. Russell, Chief Engineer W. Gibson, General Supervisor, Operational QA R. C. L. Olson, Senior Engineer K. H. Sebra, Principal Engineer 1742 283 800114010 h
ENCLOSURE 1 UNITED STATES ISINS NO.:
6870 NUCLEAR REGULATORY COMMISSION Accession No.:
OFFICE OF INSPECTION AND ENFORCEMENT 7910250525 WASHINGTON, D.C.
20555 IE Information Notice No. 79-37 Date:
December 31, 1979 Page 1 of 2 CRACKING IN LOW PRESSURE TURBINE DISCS Description of Circumstances:
An anonymous letter was received by the Director of the Office of Inspection and Enforcement, on November 17, 1979 which alleged possible violation of Part 10 CFR 50.55(e) and/or 10 CFR 21 Regulations concerning reportability of recently discovered stress corrosion cracking in Westinghouse 1800 rpm low pressure turbine discs.
Westinghouse had made a presentation on the turbine disc cracking to electric utility executives on October 30, 1979.
Telephore discussions between the NRC staff and Westinghouse's Turbine Division on November 20, 1979 established that cracking, attributed to stress corrosion phenomena, had been found in the keyway areas of several LP turbine discs at operating plants and that inservice inspection techniques (i.e., in situ ultra-sonic examination) for crack detection have been developed and are being imple-mented in the field.
The Office cf Inspection and Enforcement was also notified on November 20, 1979 that during the current overhaul of Commonwealth Edison's Zion Unit 1 LP turbine, ultrasonic examination revealed embedded cracks located on the inlet side on the disc bore area where no cracks had been previously observed.
Ultrasonic measurements indicate this disc bore cracking is of greater depth than the keyway cracks found to date.
According to Westinghouse, these bore cracks have been metallurgically examined and preliminary findings show them not to be typical of classical stress corrosion cracking observed in the keyways.
The probable cracking mechanism and impact on disc integrity is being further evaluated by Westinghouse.
A meeting was held on December 17, 1979 between the NRC staff, Westinghouse and utility representatives to discuss the disc cracking problem, repair alter-natives, turbine missile evaluation, inspection techniques and plant inspection priorities.
In response to the staffs' request, Westinghouse provided the staff an updated report on December 21, 1979 regarding the current field inspection program that included a list of nuclear power plants already inspected, recom-mended inspection schedules and pertinent information related to LP turbines where cracks have been observed.
Inspe disc cracks at Surry Unit 2, Point Beac and Zion Unit 1.
All units except Poin the plants return to power.
Point Beac DUPLICATE DOCUMENT with a small crack in the No. 2 disc of Westinghouse indicated that the observe Entire document previously during 28 additional months of turbine entered into system under:
the turbine inspection results and anal gghQ[
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