ML19211A261

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Monthly Operating Rept for Nov 1979
ML19211A261
Person / Time
Site: Rancho Seco
Issue date: 11/30/1979
From: Colombo R
SACRAMENTO MUNICIPAL UTILITY DISTRICT
To:
Shared Package
ML19211A260 List:
References
NUDOCS 7912170278
Download: ML19211A261 (8)


Text

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NARRATIVE SD' MARY OF PLINT OPERATIONS r

11-1 thru Plant operatin2 at approximately 100% full power. Performed 11-16 routine surveillance and preventive maintenance items.

11-17 (0016)

Started reducing Reactor power from 100% (%910 MWe) at 15 L'/ minute to inspect inaccessible snubbers in the Reactor Building and to initiate the new under/over voltage protection scheme for the vital buses,

f (0107)

Generator off line (opened OCB's 220 and 230).

(0109)

Tripped Turbine.

-0 (0130)

Holding Reactor at 10 amps.

8 (2233)

Maintenance /nodifications complete - reactor at 8% power.

(2338)

'Reacter at 157 power.

(2358)

Generator on line (closed OCB's 220.and 230).

11-18 (0011)

Raising Reactor power to 92%. At 17% power (%170 MWe), the "B" Reheater Safety Valve lifted and would not reseat.

Started load reduction.

(0215)

Generator off line (opened OCB's 220 and 230).

i (0408)

Generator on line (closed OCB's 220 and 230).

l (0409)

Raising Reactor power.

(0449)

Reactor at 17% power (%170 MWe).

The "B" Reheater Safety Valve lifted and would not reseat. Separated from grid (opened OCB's 220 l

and 230).

I (0700)

Closed OCB's and began Reactor power escalation.

l (0721)

' Stopped escalation due to "B" Reheater Safety Valve failin~g to reseat.

(0730)

Reactor at 25*: (%220 MWe).

Began reducing power to separate from grid to perform repairs to "B" Reheater Safety Valve.

(0843)

Generator off line (opened OCB's 220 and 230).

(1123)

Repairs complete - generator on line (closed 00B's 220 and 230).

(1124)

Raising Reactor power.

1591 346 7 9121'J O 2 78'

. (1231)

Stopped power ascent at 55% power (400 W e) due to vacuum problem and power imbalance.

(1514)

Problems improved. Started increasing power to 92%.

(1545)

Reactor at 72% power (672 We).

(1710)

Reactor at 88% power (800 We) for 2-hour hold.

(2035)

Increasing Reactor power to 100%.

4 (2330)

Reactor at 100% full power.

11-19 (0102)

Began reducing power to 10%, developed electro hydraulic oil leak

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on #1 Intercept Valve.

(0131)

Reactor at 20% power (180 We).

l l

(0135)

Turbine generator at 90 We (10% power).

I (0528)

Started increasing Reactor power to 92% af ter replacing "0" ring in ill Intercept Trip Solenoid Valve.

(0835)

Reactor at 87% power (785 We) for 2-hour hold.

(1035)

Raising Reactor power to 100%.

(1110)

Reactor at 100% full power.

f 11-25 (0147)

Secured Makeup Pump due to weld leak at intersection of Drain Valve SIM-579 line and HPI header (23620-4" CA) on discharge side of M.U.

l Pump (p-236). Started shutdown at 1 W / minute.

(0240)

Increased shutdown rate to 10 W/ minute due to the leak being non-isolable from supply header.

(0355)

Unit off line (opened OCB's 220 and 230).

(0357)

Tripped Turbine.

l (0420)

Reactor at 10-8,mp3, (0612)

Tripped Reactor.

I (1630)

Stopped RCS cooldown at 430 F and 1500 psig.

(2130)

Leak secured. Started RCS heatup.

i 1591 347

'-26 j

(0415)

Reactor in Hot Shutdown Mode.

(0550)

Started deboration of Reactor Coolant System.

~

1

-3_

(1335)

Reactor critical.

~

(1414)

Reactor at 10 amps.

(1424)

Reactor at 1% power.

(1530)

Reactor at 10% power.

(1600)

Reactor at 12% power.

(2210)

Maintained Reactor at 12% power while processing water to restore the Reactor Coolant Drain System Tank level to sufficient level to allow normal power operation.

11-27 (0100)

Started "A" HPI and secured Makeup Pump due to low oil pressure alarm.

(0800)

Reactor at 12% power.

(1210)

Unit on line (closed OCB's 220 and 230).

(1321)

Reactor at 30P. power (450 M7e) and holding for improved balance.

(1450)

Began increasing Reactor power to 727. for 5-hour hold.

(1553)

, Reactor at 72% power (640 MLe) for 5-hour hold.

(2100)

Holding power - waiting completion of leak rate calculation.

11-28 (0255)

Received acceptable leak rate calculation and began power escalation to 92%.

(0408)

Reactor at 92% (820 MWe) for 2-hour hold.

(0613)

Raising power to 100%.

(0645)

Stopped power.escalatios t 97% power due to inability to place d8 Condtnsate Polisher in service (inlet valve will not open).

11-29 (0000)

Reactor at 90% (820 MRe).

(1228)

Raising Reactor power to 100%.

(1318)

Reactor at 100% (900 MWe).

1591 348

-4 PERSON';EL CHA'*CES REQUIRING REPORTING No personnel changes t' at require reporting in accordance with Technical Specifications Figure 6.9-2 were made in November, 1979.

MAJOR ITEMS OF SAFETY-RELATED MAINTENANCE 1.

Continued inspection / testing of pipe supports; repaired or replaced as necessary to meet the new criteria covered in Bulletin 79-02.

2.

Rebuilt and/or filled three snubbers found low on oil during snubber inspection. (LER 79-16, LER 69-18).

3.

Changed setpoints of over/under voltage protection scheme for the Vital Buses-4.

Repaired weld on stub of Drain Valve SIM-579 line at intersection with HPI Header (23620-4"-CA) on discharge side Makeup Pump (LER 79-19).

SUMMARY

OF CHANGES MADE IN ACCORDANCE WITH 10 CFR 50.59(b) i No chances, tests, or experiments were completed in September, 1979, which constituted a change in a safety analysis report description.

I 1591 349 I

i 0

P00R ORGINAL REFUELI::C I:TCP?.ATIO:* REQUEST Rancho Seco Unit 1 1.

1: ace of Facility:

January 19, 1979 Scheduled da:e for next refueling shutdown:

2.

March, 1979 Scheduled date for restart following refueling:

'3.

Technical Specification change or other license anendment required:

4.

Change to Rod Inder. vs. Power Level Curve (TS 3.5.2) a)

Change to Core I: balance vs. Pouer Level Curve (TS 3.5.2) b)

c) Til: Limits (TS 3.5.2) d) Safety Equip =cnt Testing (TS 3.3.3).

December. 1970 Scheduicd date(s) for sub=itting proposed licensing action:

S.

None Impercent licensing considerations associated with refueling:

6.

7.

Nu,cber of fucl assc=blies:

a) In the core:

177 b) In the Spent Fuel Pool:

112 579 8.

Present licensed spent' fuel capacity:

5rojected date of the last refueling that can be discharged 9.

to the Spent Fuel Fool:

lo87 1591 350 a

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AVERAGE DAILY UNIT POhEI LEVEL 50-312 DOCKET NO.

R UNIT ancho Seco Unit I 79-11-30 DATE CO\\lPLETED BY R. 11 Colombo TELEPliONE 916-452-3211 MONTH

% e-ka.

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL Olhe Set) paye.Ner; I

867 0'

37 2

868 18 333 3

868 19 654 867 4

20 860 21-854 5

865 6

860 863 22 7

865 23 865 8

866 861 24 9

868 93 25 867 10 26 0

863 11 27 231-862 -

12 28 764 863 13 814 29 862 861 14 30 15 3;

16 861 INSTRUCTIONS On this (Or::n:, hst :he nera;c daily un:t power leselin.\\tWe Net for e eh day in the report:ne :n nth. C.>mpure to the nearest whoie megnot:-

1591 351 (9/771 e

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P00R O hNO OPERATING DATA REPORT Ul DOCKET N0 50-312 DATE 79-11-30 CO3fPLETED BY R.

t' Colombo l

TELEPHONE 916-452-3211 OPERATING STATUS

1. Unit Name:

Rancho Seco Unit One Notes Scheduled outage on

2. Reportin; Period:

November 1979 November 17 to inspect-inaccessible snubbers and to

3. Licensed Thermal Power t.'lWts:

2772 initiate the under/over

4. Nameplate Rating IGross SIVe):

963 voltage protection scheme

5. Design Electrical R: ting (Net 31We t:

019 for the vital buses.

6. Staximum Dependable Capacity aGross SIWE):

917 l

7. Sfaximum Dependable Capacity (Net 31Wep:

073

8. If Changes Occur in Capacity Rating (Items Number 3 Through 7) Since Last Report. Gise Reasons:

N/A

9. Power Level To Which Restricted. If Any (Net 31We):

^

10. Reasons For Restrictions. If Any:

N/A This 5!onth Yr.-to.Date Cumulatise

11. Hours in Reporting Period 720 8,016 40,513
12. Number Of Hours Reactor has Critical 691.8 6,258.7 25,329.5
13. Reactor Rewrve Shutdown Hours 0

1,557.7 3,975.1 l4'. Hours Generator On.Line 634.5 6,034.1 24,197.3

15. Unit Resene Shutdown Hours 0

1,199.3 1,210.2

16. Cross Thermal Ener y Generated t>!WH, 1,709,887 16,463,692 61,536,848
17. Gross Electrical Ener; Generated s'.t'Vili 544,771 5,353,130 20,615.930
18. Net Electrica! Ener;> Generated salhHj 514,811 5,075,584 19,474,474
19. Unit Service Factor 88.1 75.3 59.7
20. Unit Availability Factor 88.1 90.2 62.7
21. Unit Capacity Factor iUsing.\\lDC Net) 81.9 72.5 55.1
22. Unit Capacity Factor (Using DER Net 77.9 69.0 52.4
23. Unit Forced Ot. tap Hate 9.0 6.2 32.7'
24. Shutdown > Scheduled Oser Nest 6 Stanths tT pefDate.and Dur:tian of Eachi:

3 Refueling: Januarv 1980-duration approximate 1v 60 days.

25. If Shur Down At End Of Report PericJ. Estimated D.ne of Startup-N/A
26. Units in Test Status. 'rior to Co;nmeresal Operarmn s:

Forecast Achiesed INITIAL CRIT!r \\ LITY

^

INITi \\L ELECTRICITY

__ N/A N/A CO.\\l\\:ERCITL Ol'ER A1 ION 4

s, o 15 91 2 52 (W77:

I UNIT SliUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-312 UNIT NAstE Rancho Seco Unit 1 D.\\10 79-11 '10 REPOltT MON 111_ November. 1979 COMPI.E II:D IlY R. W.

Colombo 1EErPilONE 916-452-3211

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14 79-11-17 S

22.8 B

1

~ N/A N/A N/A Inspected inaccessible snubbers and initiated the new under/over voltage protection scheme for the vital buses.

15 79-11-18 F

1.9 A

1 N/A N/A N/A "B" Reheater Safety Valve lifted and would not rescat.

16 79-11-18 F

2.2 A

1 N/A N/A N/A "B" Reheater Safety Valve lifted and would not resent.

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17 79-11-18 F

2.7 A

1 N/A N/A N/A "B" Reheater Safety Valve lifted and g

would not resent.

Valve repaired.

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18 79-11-19 F

0 A

1-N/A N/A N/A Reduced Reactor power to 10% due to an Electrohydraulic oil leak on #1 Q

Intercept Valve. Valve Trip Solenoid repaired.

19 79-25-79 F

55.9 A

1 79-019/03 L-0 SF PIPEXX Took Reactor to ilSD due to a weld leak O

at intersection of inlet stub of Q

SIM-579 drain 1ine and 4" llPI header.

v o o te vo n n e r,,,1 -

1 2

3 4

F: Forced Itc.non:

Method:

Exhibit G Instructions S: Scheduled A.I'luipment Failure (Explain) 1 Manual for Preparation of Data ll Maintenance or Test 2 Manual Scram.

Entry Sheets for 1.ieensee C Itchiclinr.

3-Automatic Scram.

Event ReporI (LL R) File (NUREG-D.Itcr."Id'"'y itesiriction 4-Ot her (Explain) 01611 I: Operator Training & License Examination F. Adenini.t rative 5

G. Operational Error (Explain)

' (9/77) 11-O her(Explain)

Exhibit I Same Source 9

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