ML19210D799

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Forwards IE Info Notice 79-27, Steam Generator Tube Ruptures at Two PWR Plants. No Response Required
ML19210D799
Person / Time
Site: South Texas  STP Nuclear Operating Company icon.png
Issue date: 11/16/1979
From: Seyfrit K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Eric Turner
HOUSTON LIGHTING & POWER CO.
References
NUDOCS 7911280091
Download: ML19210D799 (1)


Text

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7L C-e UNITED STATES

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w November 16, 1979 In Reply Refer To:

RIV Docket Nos. 50-498/IE Information Notice No. 79-27 50-499/IE Information N3tice No. 79-27 llouston Lighting & Power Company ATTN:

Mr. E. A. Turner, Vice President Power Plant Construction and Technical Services Post Office Box 1700 llouston, Texas 77001 Gentlemen:

The enclosed IE Information Notice provides information with regard to the sequence of events that followed incidents involving steam generator tube ruptures at two PWR units.

Sincerely, f

. b/

A -Karl V.

frit Director

Enclosures:

1.

IE Information Notice 79-27 2.

Recently Issued IE Information Notices 1435 335 7 9112 80 d

SSINS No.:

6870 Accession No.:

7910250488 UNITED STATES NUCLEAR REGULATORY COSD!ISSION OFFICE OF INSPECTION AND ENFORCDIENT WASilINGTON D.C.

20555 IE Information Notice No. 79-27 Date: November 16, 1979 Page 1 of 7 STEAM GENERATOR 'I1JBE RUPTURES AT TWO PWR PI. ANTS Description of Circumstances:

In recent months two incidents involving steam generator tube ruptures have occurred.

In both instances, the units were cooled down and placed in the residual heat removal mode with existing procedures.

Event of June 25, 1979 at the Doel 2 Nuclear Power Plant in Belgium The first event occurred on June 25, 1979, at the Doel 2 nuclear power plant in Belgium. The Doel unit is a 390 Mwe Westinghouse two-loop reactor. The event consisted of a rupture of several tubes in the loop B steam generator. The resultant leakage between the primary and secondary systems was estimated to be 125 gpm.

The event started when the plant was heated up after a shutdown caused by a malfunction of the main steam isolation valve.

At the time of the incident the primary coolant pressure was:

2233 psi and the temperature: 491?F. The reactor remained subcritical throughout the event.

The first indication of abnormal behavior was a rapid decrease of the primary system pressure (approximately:

28 psi / min.).

This was followed by the sequence of events listed below:

Time, min.

1.

Increase of charging flow demand, requiring startup of a second 1.8 charging pump.

2.

Automatic isolation of the CVCS letdown line.

2.4 3.

Shut off of the pressurizer heaters due to low liquid level in the 2.4 pressurizer.

4.

Closing of block valves in the pressurizer relief line.

4.6 5.

Rapid increase of water level The steam generator was isola DUPLICATEDOCUMENh 6.

Startup of the third charging all charging pumps from the C tank.

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