ML19210D787

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Forwards IE Info Notice 79-27, Steam Generator Tube Ruptures at Two PWR Plants. No Response Required
ML19210D787
Person / Time
Site: Bailly
Issue date: 11/16/1979
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Shorb E
NORTHERN INDIANA PUBLIC SERVICE CO.
References
NUDOCS 7911280070
Download: ML19210D787 (1)


Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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...s Docket No. 50-367 Northern Indiana Public Service Company ATTN:

Mr. Eugene M. Shorb Senior Vice President 5265 Hohman Avenue Ham:nond, IN 46325 Gentlemen:

The enclosed IE Information Notice No. 79-27 provides information with regard to the sequence of events that followed incidents involving steam generator tube ruptures at two PWR units.

Sincerely, O-4.

James G. Keppler Director

Enclosures:

1.

IE Information Notice No. 79-27 2.

Recently Issued IE Information Notices cc w/tacls:

Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC Mr. Dean Hansell, Office of Assistant Attorney General 1435 517~

1911289 0 7 6

SSINS No.:

6870 Accession No.:

7910250488 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGT R D.C.

20555 November 16, 1979 IE Information Notice No. 79-27 STEAM GENERATOR TUBE RUPTURES AT TWO FNR PLANTS Description of Circumstances:

In rece.it months two incidents involving steam generator tube ruptures have occurred.

In both instances, the units were cooled down and placed in the residual heat removal mode with existing procedures.

Event of June 25, 1979 at the Doel 2 Nuclear Power Plant in Belgium The first event occurred on June 25, 1979, at the Doel 2 nuclear power plant in Belgium.

The Doel unit is a 390 Hwe Westinghouse two-loop reactor.

The event consisted of a rupture of several tubes in the loop B steam generator.

The resultant leakage between the primary and secondary systems was estimated to be 125 gpm.

The event started when the plant was heated up after a shutdown caused by a malfunction of the main steam isolation valve.

At the time of the incident the primary coolant pressure was:

2233 psi and the temperature:

491 F.

The reactor remained subcritical throughout the event.

The first indication of abnormal behavior was a rapid decrease of the primary system pressure (approximately:

28 psi / min.).

This was followed by the sequence of events listed below:

Time, min.

1.

Increase of charging flow demand, requiring :tartup of a second 1.8 charging pump.

2.

Automatic isolation of the CV 3.

Shut off of the pressurizer h pressurizer.

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