ML19210D778

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Forwards IE Info Notice 79-27, Steam Generator Tube Ruptures at Two PWR Plants. No Response Required
ML19210D778
Person / Time
Site: Midland
Issue date: 11/16/1979
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Howell S
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
NUDOCS 7911280059
Download: ML19210D778 (1)


Text

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Docket No. 50-329 Docket No. 50-330 g,',

Consumers Power Company ATTN:

Mr. Stephen H. Howell Vice President 1945 West Parnall Road Jackson, MI 49201 Gentlemen:

The enclosed IE Information Notice No. 79-27 provides information with regard to the sequence of events that followed incidents involving steam generator tebe ruptures at two PWR units.

Sincerely, 64~

/j:,JamesG.Keppler f Director

Enclosures:

1.

IE Information Notice No. 79-27 2.

Recently Issued IE Information Notices cc w/encls:

Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC Ronald Callen, Michigan Public Service Com:nission Dr. Wayne E. North Myron M. Cherry, Chicago 1435 505 7911ognog9

SSINS No.:

6870 Accession No.:

7910250488 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON D.C.

20555 November 16, 1979 IE Information Notice No. 79-27 STEAM GENERATOR TUBE RUPTURES AT TWO PWR PLANTS Description of Circumstances:

In recent months two incidents involving steam generator tube ruptures have occurred.

In both instances, the units were cooled down and ? laced in the residual heat removal mode with existing procedures.

Event of June 25, 1979 at the Doel 2 Nuclear Power Plant in Belgium The first event occurred on June 25, 1979, at the Doel 2 nuclear power plant in Belgium. The Doel unit is a 390 Mwe Westinghouse two-loop reactor.

The event consisted of a rupture of several tubes in the loop B steam generator.

The resultant leakage between the primary and secondary systems was estimated to be 125 gpm. The event started when the plant was heated up after a shutdown caused by a malfunction of the main steam isolation valve.

At the time of the incident the primary coolant pressure was:

2233 psi and the temperature:

491 F.

The reactor remained subcritical throughout the event.

The first indication of abnormal behavior was a rapid decrease of the primary system pressure (approximately:

28 psi / min.).

This was followed by the sequence of events listed below:

Time, min.

1.

Increase of charging flow demand, requiring startup of a second 1.8 charging pump.

2.

Automatic isolation of the CV Shutoffofthepressurizerhg 3.

pressurizer.

Entire document previously entered into system under:

ANO No. of pages: