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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20065D0491990-09-14014 September 1990 Forwards Operator & Senior Operator Licensing Exam Ref Matl for Exam Scheduled for Wk of 901112,per 900607 Request ML20065D4951990-09-14014 September 1990 Forwards Updated Exam Schedule for Facility,In Response to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule ML20059K4681990-09-14014 September 1990 Provides Supplemental Info Re Emergency Response Data Sys (Erds).Data Transmitted by Util ERDS Will Have Quality Tag of 4 & Point Identification for ERDS Renamed ML20059G2341990-09-10010 September 1990 Provides Response to Request for Addl Info Re Interpretation of Tech Spec 3/4.7.10, Fire Barriers. Interpretation Is Implemented & Unnecessary Compensatory Measures Removed.List of Fire Barriers Inspected on One Side Only Encl ML20059G4961990-09-0606 September 1990 Submits Voluntary Rept of Svc Water HX Testing During Sixth Refueling Outage.Expected Flow Rates Not Achieved.Periodic Tests Developed to Check Efficiency of Containment Air Coolers ML20064A6271990-09-0606 September 1990 Requests That Requirement Date for Installation & Testing of Alternate Ac Power Source & Compliance w/10CFR50.63 Be Deferred Until Completion of Eighth Refueling Outage ML20028G8611990-08-28028 August 1990 Forwards Davis Besse Nuclear Power Station Semiannual Rept: Effluent & Waste Disposal,Jan-June 1990. ML20059D4121990-08-28028 August 1990 Forwards Second 10-Yr Interval Pump & Valve Inservice Testing Program ML20059D5521990-08-24024 August 1990 Forwards Semiannual Fitness for Duty Rept for Jan-June 1990 ML20059B5291990-08-23023 August 1990 Forwards Updated Fracture Mechanics Analysis of Hpi/Makeup Nozzle,Per 900510 Meeting W/Nrc.Util Believes That Addl Analysis to Assess Structural Integrity of Nozzle Using More Conservative Fracture Model Supports Previous Analysis ML20058Q3911990-08-16016 August 1990 Requests NRC Concurrence on Encl Interpretation & Technical Justification of Tech Spec 3/4.7.10, Fire Barriers ML20058P7801990-08-10010 August 1990 Advises of Intentions to Revise Testing Requirements for Fire Protection Portable Detection Sys at Plant & Functional Testing of auto-dialer & Telephone Line Subsys from Daily to Weekly Testing ML20063P9981990-08-0909 August 1990 Submits Supplemental Response to Insp Rept 50-346/89-21. Util Rescinds Denial & Accepts Alleged Violation ML20056A5341990-08-0303 August 1990 Confirms Electronic Transfer of Payment of Invoice I0942 Covering Annual Fee for FY90,per 10CFR171 ML20058M7791990-08-0303 August 1990 Forwards Rev 10 to Industrial Security Plan & Rev 6 to Security Training & Qualification Plan.Revs Withheld ML20058L1821990-08-0101 August 1990 Forwards Davis-Besse Dcrdr Human Engineering Discrepancy Repts 1988 Summary Addendum 1,Vol 1, Per NRC Audit Team Request ML20056A8341990-07-23023 July 1990 Forwards Revised Monthly Operating Rept for June 1990 for Davis-Besse Nuclear Power Station Unit 1 ML20055H4601990-07-20020 July 1990 Discusses Resolution of Draft SER Open Item on Voluntary Loss of Offsite Power.Util Preparing License Amend Request Per Generic Ltrs 86-10 & 88-12 to Relocate Fire Protection Tech Specs & Update Fire Protection License Condition ML20055F9681990-07-17017 July 1990 Forwards Application for Amend to License NPF-3,adding Centerior Svc Company as Licensee in Facility Ol.Change Allows for Improved Mgt Oversight,Control & Uniformity of Nuclear Operations ML20055F8561990-07-17017 July 1990 Discusses Util Planned Activities Re Instrumented Insp Technique Testing Performed at Facility in View of to Hafa Intl.Relief Requests Being Prepared by Util for Sys on Conventional Hydrostatic Testing ML20044B3001990-07-12012 July 1990 Provides Written Confirmation of Util Electronic Transfer of Funds to NRC on 900711 in Payment of Invoice Number I1050 ML20044B1841990-07-10010 July 1990 Requests Approval of Temporary non-code Repair & Augmented Insp of Svc Water Piping,Per 900626 Telcon ML20055D9701990-06-29029 June 1990 Provides Written Confirmation of Util Electronic Transfer of Funds for Payment of Invoice 0111 Covering Insp Fees for 890326-0617 ML20043H5291990-06-14014 June 1990 Forwards Plans Re Reorganization & Combining of Engineering Assurance & Svc Program Sections ML20055C7521990-06-14014 June 1990 Responds to NRC Bulletin 89-002, Potential Stress Corrosion Cracking of Internal Preloaded Bolting in Swing Check Valves & Justification for Alternate Insp Schedule for One Valve. No Anchor Darling Swing Check Valves Installed at Plant ML20055F2261990-06-14014 June 1990 Forwards 1990 Evaluated Emergency Exercise Objectives for Exercise Scheduled for 900919 ML20043G5661990-06-14014 June 1990 Forwards Rev 9 to Industrial Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043G7811990-06-12012 June 1990 Forwards Info Re Implementation of NUREG-0737,Item II.F.2, Inadequate Core Cooling Instrumentation, Per NRC 900214 Safety Evaluation.Item II.B.1 Issue Re Reactor Vessel Head Vent Also Considered to Be Closed ML20043F6091990-06-11011 June 1990 Forwards Util Comments on NRC Insp Rept 50-346/90-12, Per 900601 Enforcement Conference Re Core Support Assembly Movement & Refueling Canal Draindown.Refueling Canal Draindown Procedure Provides Specific Draining Instructions ML20043E1301990-06-0101 June 1990 Withdraws 870831 & 890613 Applications to Amend License NPF-3.Changes Requested Addressed by Issuance of Amend 147 or Can Now Be Made as Change to Updated SAR Under 10CFR50.59 ML20043D5601990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,revising Tech Spec 3/4.6.4.1, Combustible Gas Control - Hydrogen Analyzers. Request Consistent W/Nrc Guidance,Generic Ltr 83-37,dtd 831101,NUREG-0737 Tech Specs & Item II.F.1.6 ML20043D5691990-05-31031 May 1990 Forwards Application for Amend to License NPF-3,requesting Extension of Expiration Date of Section 2.H to Allow Plant Operation to Continue Approx 6 Yrs Beyond Current Expiration Date ML20043D1451990-05-31031 May 1990 Forwards Rev 11 to Updated SAR for Unit 1.Rev Updates Table 6.2-23 Re Containment Vessel Isolation Valve Arrangements ML20043D1621990-05-29029 May 1990 Documents Util Understanding of NRC Interpretation of Plant Tech Spec 3.7.9.1,Action b.2 Re Fire Suppression Water Sys, Per 891206 Telcon.Nrc Considered Electric Fire Pump Operable Provided Operator Stationed to Open Closed Discharge Valve ML20043C2331990-05-25025 May 1990 Forwards Summary of 900510 Meeting W/B&W & NRC in Rockville, MD Re Hpi/Makeup Nozzle & Thermal Sleeve Program.List of Attendees & Meeting Handout Encl ML20043B1701990-05-18018 May 1990 Forwards Revised Exemption Request from 10CFR50,Section III.G.2,App R for Fire Areas a & B,Adding Description of Specific Limited Combustibles That Exist Between Redundant Safe Shutdown Components in Fire Area a ML20043A5441990-05-16016 May 1990 Discusses Status of Safety & Performance Improvement Program Portion of B&W Owners Group EOP Review Project ML20043A2311990-05-11011 May 1990 Responds to Violation Noted in Insp Rept 50-346/90-08. Corrective Actions:Results of Analysis of Radiological Environ Samples & Radiation Measurements Included in 1989 Annual Radiological Environ Operating Rept ML20043A4901990-05-10010 May 1990 Forwards Summary of Differences Between Rev 5 to Compliance Assessment Rept & Rev 1 to Fire Area Optimization,Fire Hazards Safe Shutdown Evaluation, Vols 1-3.Rept Demonstrates Compliance W/Kaowool Wrap Removal ML20042F9801990-05-0404 May 1990 Provides Written Confirmation of Util Electronic Transfer of Payment of Invoice Number 10716 to Cover Third Quarterly Installment of Annual Fee for FY90 ML20042F5781990-05-0303 May 1990 Provides Status of Hpi/Makeup Nozzle & Thermal Sleeve Program.Nrc Approval Requested for Operation of Cycle 7 & Beyond Based on Program Results.Visual Insp of Thermal Sleeve Identified No Thermal Fatique Indications ML20042F0951990-04-30030 April 1990 Responds to Violations Noted in Insp Rept 50-346/90-02. Corrective Actions:Maint Technician Involved in Tagging Violation Counseled on Importance of Procedure Adherence W/ Regard to Personnel Safety ML20042F0841990-04-27027 April 1990 Responds to Violations Noted in Insp Rept 50-346/89-201 for Interfacing Sys LOCA Audit on 891030-1130.Corrective Actions:Plant Startup Procedure Will Be Revised Prior to Restart from Sixth Refueling Outage ML20042E7311990-04-27027 April 1990 Forwards Application for Amend to License NPF-3,deleting 800305 Order Requiring Implementation of Specific Training Requirements Which Have Since Been Superseded by INPO Accredited Training Program ML20042F1961990-04-27027 April 1990 Informs of Adoption of Reorganization Plan Re Plants on 900424.Reorganization Will Make No Changes in Technical or Financial Qualifications for Plants.Application for Amends to Licenses Adding Company as Licensee Will Be Submitted ML20043F7261990-04-20020 April 1990 Requests Exemption from 10CFR55.59(a)(2) to Permit one-time Extension of 6 Months for Reactor Operators & Senior Reactor Operators to Take NRC 1990 Requalification Exam. Operators Will Continue to Attend Training Courses ML20042E7091990-04-17017 April 1990 Forwards Annual Environ Operating Rept 1989 & Table 1 Providing Listing of Specific Requirements,Per Tech Spec 6.9.1.10 ML20012F5091990-04-0303 April 1990 Forwards Completed NRC Regulatory Impact Survey Questionnaire Sheets,Per Generic Ltr 90-01 ML20012F6001990-04-0202 April 1990 Submits Supplemental Response to Station Blackout Issues,Per NUMARC 900104 Request.Util Revises Schedule for Compliance W/Station Blackout Rule (10CFR50.63) to within 2 Yrs of SER Issuance Date ML20012E0181990-03-22022 March 1990 Forwards Application for Amend to License NPF-3,changing License Condition 2.C(4) Re Fire Protection Mods to Fire Extinguishers,Fire Doors,Fire Barriers,Fire Proofing,Fire Detection/Suppression & Emergency Lighting 1990-09-06
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Docket No. 50-346 Totsoo License No. NPF-3 Serial No. 559 LOWELL E. ROE November 21, 1979 7,,7,','$',",*,,,,
[4191 259-5242 Mr. Harold R. Denton, Director Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D. C. 20555
Dear Mr. Denton:
Toledo Edison indicated its intent to comply with your staf f's short term lessons learned recommendations from the ihree Mile Island, Unit 2 (TMI-2) incident of March 28,1979. Our letter of October 23, 1979 (Serial No. 546) identified pre-liminary schedules and some basic information about our implementation of the recommendations at the Davis-Besse Nuclear Power Station Unit 1 (DB-1) . We identi-fled them, and reiterate now, that we consider the established design of the Davis-Besse Station combined with the modifications and procedural changes made in recent months adequate to ensure there be no undue risk to public health and safety.
Your generic letter of October 30,1979 (Log No. 454) identifies concern over implementation schedules of utilities for items recommended to be implemented by January 1, 1980. Additionally, it identifies new, more detailed recommendation criteria. The schedule concern was reinforced during a telephone conversation between our staffs on November 9, 1979. Toledo Edison has been reviewing and further defining our projected activities in this area and have gone back and reassessed all our pending activities in light of your concern. The result has been a prioritization process that delays several non-related ongoing regulatory activities and therefore allows e::paditing of the subject tasks by our personnel as well as our vendors and consultants. We will attempt to minimize the impact on other TMI-2 related items being pursued in the bulletins and orders and emergency preparedness areas.
~
The results on short term lessons learned of our reassessment are provided here.
The items attached only include those schedule items whose projected implementation dates have been revised or justified and those whose implementation methods or de-tailed information modify our letter responses of October 23, 1979.
7911270 3 7 ) l P t THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISCN AVENUE TOLEDO. OHIO 43652
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Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Page Two These projected dates are reficceed as realistic and are based on aggressive schedules for Toledo Edison, its vendors and consultants considering all regulatory activities currently defined. As a result, these dates will be impacted by each new higher priority request of your staff. As the activities progress we will continue to expedite and improve schedules when possible. Those items requiring outages have been scheduled concurrent with presently planned outages. Installation may be completed during an earlier outage of sufficient duration af ter the equipment is available and installation engineering complete. As always, we are available, at your request to discuss any aspect of our submittal.
Very truly yours,
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Docket No. 50-346 License No. NPF-3 Serial No. 559 No*/ ember 21, 1979 TOLEDO EDISON RESPONSE TO NRC LETTER OF OCTOBER 30, 1979 FOR DAVIS-BESSE NUCLEAR POWER STATION UNIT 1 (DB-1) 3x99 050
Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Toledo Edison Response to NRC letter dated October 30, 1979 NOTES: 1) All schedule dates are projections and subject to change based on outcome of reviews under 10CFR50.59, hardware availability and support manpower availability.
- 2) Items in the attachment correspond to the identification schemes of the September 13 and October 30, 1979 NRC letters and NUREG 0578.
Task number designations are for administrative cross-referencing within Toledo Edison.
Letter Items:
Item d Three additional instrumentation requirements for short-term action were developed during the ACRS review of NUREG 0578. These items relate to containment pressure, containment water level and containment hydrogen monitors designed to follow the course of an accident. (Task Nos. 37 - 39)
Response
CONTAINMENT PRESSURE - Safety grade control room indication for an extended range of containment vessel pressure will be provided at Davis-Besse Unit 1. The revised projected schedule identifies installation by Janu'ary 1,1981.
CONTAINMENT WATER LEVEL - Safety grade control room indication of narrow and wide range containment water level will be provided at Davis-Besse Unit 1.
Several options to provide this level are currently being evaluated. For commitment purposes, the most schedule restrictive option requires instrument installation inside the containment building. The planned outage when the equipment would be available for installation and testing is the Spring 1981 refueling outage. If a design is selected that does not require containment entry for full or. partial implementation, the schedule may be accelerated.
CONTAINMENT HYDROGEN - Safety grade control rcom indication of 0 - 10% hydrogen con-centration will be provided at Davis-Besse Unit 1. The revised projected schedule identifies installation by January 1,1981.
1]) 0 Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Item e An additional requirem. following issuance of NUREG 0578, which concerned a remotely operable high soint vent for gas from the reactor coolant system, was developed (high point and vessel head vents, Task No. 40)
Response
A generic design effort is underway by B&W to provide a functional description of the construction, location, size and appropriate power supply for reactor coolant system high point vents. Appropriate safety analyses and reviews considering the effects of such vents are also being pursued concurrently. Additionally, an evaluation of the necessity of a reactor vessel head vent on the B&W nuclear steam supply system is being performed. It is presently projected that a preliminary design of the pro-posed venting system should be completed and forwarded to you for review and conceptual approval by January, 1980.
Provided the evaluations are completed as expected and no potential unreviewed safety issues are identified, these vents could be installed during the planned Spring outage of 1981. This is contingent upon NRC approval and qualified equipment availability within the time frame between NRC approval and the 1981 outage.
Item f NUREG 0578 recommendations as modified by the errata of Enclosure 5.
(Note that recommendations are numbered consistent with NUREG 0578).
Recommendation 2.1.1 - Emergency Power Supply Requirements for Pressurizer Heaters, Power Operated Relief Valves and Block Valves, and Pressurizer Level Indicators in PWRs. (Task No. 001 - 005).
Response
PRESSURIZER HEATERS - The current Davis-Besse design provides manual loading of 126 kw of pressurizer heater capacity to each emergency diesel. Procedures are already in place covering the manual loading of these electrical loads. All actions to energize these heaters from the emergency diesel generators are in the control room and are made by the control room operator. Davis-Besse currently meets this recommendation.
No further action is required.
PILOT OPERATED RELIEF VALVE (PORV) - The current Davis-Besse design has its non-safety related pilot operated relief solenoid valve and control circuitry powered from a
. 125 vDC bus supplied by a safety grade battery system. A safety grade battery charger is provided to this DC system. The valve position indication is provided from the station battery ria a 250 vDC to 120 vAC inverter. Isolation of safety grade buses from non-safety grade devices is provided by qualified devices at the motor control c ent er s. Davis-Besse meets the emergency power recommendation. No further action is required.
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Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 PILOT OPERATED RELIEF VALVE BLOCK VALVES - Davis-Besse will provide an AC safety grade motive and control power source to the PORV block valve. The power source will,be appropriately isolated from non-safety grade portions of the system. The current schedule projects this modification will be completed by January 1,1980.
PRESSURIZER LEVEL INDICATORS - The current Davls-Besse design has two channels of safety grade pressurizer level indication on a safety grade power supply. Davis-Besse currently meets this recommendation. No further action is requirsd.
Recommendation 2.1.3a - Direct Indication of Power Operated Relief Valve and Safety Valve Position for PWRs and BWRs. (Task No. 7)
Response
Toledo Edison will provide positive primary system safety "alve and PORU position indication by the use of an acoustic monitoring system. Discussions with vendors supplying these devices indicate that the system can be powered from a safety related power supply with sensors that are seismically and environmentally qualified. However, the entire system will not meet safety grade requirements. Due to projected equipment delivery and installation engineering requirements this system will be installed and tested prior to start-up af ter the Spring refueling outage currently scheduled to start in March 1980. Davis-Besse currently utilizes quench tank level, quench tank pressure and PORV electrical position indication to aid in operator diagnostics. These methods are currently discussed in the DB-1 emergency procedures. Toledo Edison's current procedures and operator training are adequate to provide diagnostic informa-tion for the operator and will be utilized as a backup to the acoustic system when installed.
Recommendation 2.1.3b - Instrumentation for Detection of Inadequate Core Cooling in BWRs and PWRs. (Task Nos. 8 - 10).
Response
Toledo Edison is participating with B&W in the development of procedural guidelines for operator recognition of inadequate core cooling under the conditions identified in Section 3 of recommendation 2.1.9 (NUREG 0578, page A-44) . These guidelines are currently being pursued with the NRC Bulletin and Orders Task Fo ce. Inadequate core cooling for the refueling and loss of inventory cases will be submitted by January 1, 1980.
The design of any new instrumentation, if deemed necessary by a joint B&W Owners evaluation, would be submitted for NRC review and approval in April 1980. A scheduled installation date for any such instrumentation will be provided along with the April 1980 proposal.
DB-1 will install a primary c )olant saturation meter which will provide on-line control room Ladication of coolant saturation condition. The lack of wide range safety grade temperature inputs available is currently under review, as well as the quality assurance program to which the system is built. This will identify if the overall system can qualify as fully safety grade. Due to expected projected equipment delivery and installation engineering requirements the system will be installed during the Spring refueling outage currently snheduled to start in March, 1980. The following pages contain additional information On this subcooled meter.
1x99 053
. , , Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 INFORMATION ON THE SUBC00 LING METER Display Infomation Displayed (T-Tsat, Tsat, Press, etc.) AT = (Tsat - Th)
Display Type (Analog, Digital, CRT) . Digital continuous for selected Continuous or on Demand parameter Single or Redundant Display single Location of Display Control Room Area klarms (include setpoints) A T450 F Overall uncertainty (*F, PSI) Note (1)
Range of Display Note (1)
Qualifications (seismic, environmental, IEEE323) Note (1)
Calculator -
Type (process computer, dedicated digital or analog calc.) Dedicated Digital If process computer is used specify availability. (% of time) N/A Single or redundant calculators single Selection Logic (highest T., lowest press) Note (1)
Qualifications (seismic, environmental, IEEE323) Note (1)
Calculational Technique (Steam Tables, Functional Fit, ranges) steam Tables Inout Temperature (RTD's or T/C's) RTDs Temperature (number of sensors and locations) 2 (1/ Hot leg)
Range of temperature sensors Note (1)
. ;299 n64
Docket No. 50-346 .
Licence No. NPF-3 Serial No. 559 November 21, 1979
?
Uncertainty
- of temperature sensors (*F at 1 ) Note n3 Qualifications (seismic, environmental, IEEE323) Note n)
Pressure (specjfy instrument used) Note (1)
Pressure (numoer of sensors and locations) Note (1)
Range of Pressure sensors Note (1)
Uncertainty
- of pressure sensors (PSI at 1 ) Note (1)
Qualifications (seismic, environmental, IEEE323) Note (1)
Backup Capability Availability of Temp & Press yes Availability of Steam Tables etc. Yes Training of operators Yes Procedures Yes
- Uncertainties must address conditions of forcea flow and natural circulation NOTE (1) The selection of specific equipment is still under review.
Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Davis-Besse currently provides operator saturation curves mounted in the control room as well as in the station's emergency procedures. Additionally there is a computer alarm point for approach i.o saturation conditions. Toledo Edison's current procedures and extensive operator training in the area of reactor coolant saturation concerns provide an adequate diagnostic cool to reactor operators and will remain available after the saturation meters are installed.
Recommendation 2.1.5a - Dedicated Penetrations for External Recombiners or Post-Accident Purge Systems (Task No. 13).
Response
Davis-Besse utilizes the concainment hydrogen dilution system for post-accident combustible gas control. This is a dedicated, safety grade, accident mitigation system whose penetrations meet redundancy and single failure criteria. Davis-Besse complies with this recommendation. No further action is required.
Recommendation 2.1.6a - Integrity of Systems outside Containment likely to Contair Radioactive Materials (Engineered Safety Systems and Auxiliary Systems) for PWRs and BWRs (Task No.15) .
Response
A leakage reduction program, including an initial effort as well as an ongoing pre-ventive maintenance effort, is being developed for DB-1. By January 1,1980 we will provide a summary description of this program. This summary will include a list of the systems involved and identification of testing methods. Currently we expect difficulty in the area of gaseous systems testing if helium leak detection methods are utilized. Alternate methods are being evaluated.
Recomendation 2.1.6b - Design Review of Plant Shielding of Spaces for Post-Accident Operations ( Task No. 16).
Response
Toledo Edison's consultant is providing a preliminary analysis of current plant shielding effectiveness of sampling, letdown and accident mitigation systems under the assumed source terms in your letter b January 1,1980.
These results will then be evaluated based on area accessability requirements. Any proposed design modifications would be provided with an implementation schedule by February 20, 1980.
9 1T99 056 Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Recommendation 2.1.7b - Auxiliary Feedwater (AFW) Flow Indication to Steam Generators for PWRs (Task No. 18).
Response
DB-1 has installed control grade AFW flow indicators as described in Toledo Edison's letter Serial No. 507, dated May 22, 1979. Additionally, DB-1 currently has safety grade steam generator level indication which provides the primary means to detect if the auxiliary feedwater systea is working properly. The flow indicators provide a backup to meet the single failure criteria.
With these indications, DB-1 complies with the January 1,1980 control grade instru-mentation recommendation.
Toledo Edison will install cae safety grade AW flow indicator per steam generator to provide a inckup indication of AW flow for the existing safety grade steam generator level. The safety grade AFW flow indicators are projected to be installed prior to January 1, 1981.
Recommendation 2.1.8a - Improved Post-Accident Sampling Capability (Task Nos. 19 - 21).
Response
DB-1 will review appropriate techniques to assure the feasibility of promptly sampling and analyzing reactor coolant and containment atmosphere under accident conditions.
In the short term, guidelines will be provided to the station by January 1,1980 for the drawing of highly radioactive reactor coolant liquid and containment vessel gaseous samples. These sampling techniques will be consistent with the current plant design capabilities which limit sample points to the reactor coolant letdown line and the pressurizer liquid. Guidelines will be provided by January 1, 1980 for on-site radiological analysis of reactor coolant samples as well as radiological and hydrogen analysis of the containment atmosphere.
The capability of on-site chemical analysis of reactor coolant is still under review.
DB-1 b9ing a fresh water site, need rot require chloride analysis. Orre area of concern in liquid chemical analysis is the dissolved gases evaluation. Due to current uncertainties in this area we cannot commit to prompt on-site chemical analysis of highly radioactive reactor coolant. Offsite laboratory analysis provides a short term alternate to this capability.
For the long term, a design review identifying plant modifications that will enhance the onsite sampling and analytical capability for highly radioactive reactor coolant and containment vessel gases will be completed in January,1980. The results of this review, a description of any planned modifict tions and a proposed schedule for implementation of these will be submitted to the NRC by January 25, 1980. ,
1799 057
Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 Recommendation 2.1.8b - Increased Range of Radiation Monitors (Task Nos. 22-24) .
Response
Toledo Edison is developing guidelines that will be available by January 1,1980 as an interim method of quantifying high level radioactive releases. Emergency power, independent of off-site power, will not be available until af ter the refueling outage, which is presently scheduled for Spring 1980. These guidelines sre being developed to utilize currently existing and/or portable equipment. Where control room readout capability is not available, communication with the control room will be provided.
Equipment related and procedural details will be addressed in the guidelines.
For the long termja design review identifying plant modifications to enhance this monitoring capability will be completed in January, 1980. The results of this review, a description of any planned modifications and a proposed schedule for implementation will be submitted to the NRC by January 31, 1960.
Recommendation 2.1.8c - Improved In-Plant Iodine Instrumentation (Task No. 25)
Response
Toledo Edison is developing the capability to detect the presence of iodine. Several options are currently being evaluated in sa area of interest following a radiological release. This capability will be available by January 1,1980. A review of planned design modifications to enhance the DB-1 capabilities in this area is underway. The results of the review, including a schedule of any design modifications will be submitted to the NRC by January 31,1980.
Recommendation 2.2. lb - Shif t Technical Advisor (Task No. 31)
Response
Toledo Edison is proposing a separation of the functions described in enclosure 2 of your September 13, 1979 letter. ,
The Shif t Technical Advisor (STA) will fulfill the function of accident assessment.
The specific details of how this individual is to administratively function is pre-sently dependent on manpower availability, further corporate direction and facility changes in progress. As a minimum, a designated individual will be available 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> a day whenever nue. lear safety systems are required to be operable beginning January 1, 1980. S2ation personnel will be required by procedure to notify the Shift Technical Advisor La the event of:
- 1. Any anticipated power transient
- 2. Any reactor trip or load run backs
- 3. Any loss of safety system function or offsite power supply The STA will be capable of reaching the control room within 10 minutes of receiving a call.
29o, nR8 -
Docket No. 50-346 License No. NPF-3 Serial No. 559 November 21, 1979 The second function, operating experisnce assessment, will be provided by a non-shif t oriented review group within the Toledo Edison organization. By January 1,1980, this function will be provided and its administration documented in procedures.
By January 1,1981, the Shift Technical Advisors will have completed training in the areas of reactor operations, as well as, transient and plant accident response. Additionally, a program will be implemented to expand the general technical edc: Lion level of any Shif t Technical Advisor that does not have a college level education in a scientific or engineering discipline. Completion of this part of the program may not be a prerequisite for Shif t Technical Advisor based on the individuals prior experience and an evaluation of his capability by the Toledo Edison Company. This evaluation will be subject to review by the Vice President of Energy Supply and his staff.
Recommendation 2.2.2b - On-site Technical Support Center (Task No. 34)
Response
As a part of an ongoing review of plant response to emergencies, Toledo Edison is reviewing the requirements of the or. site technical support center. By January 1,1980, an interim center will be established. This center will be in close proximity to the control room, have plant reference documents easily available and will have a communication link to the control room. A permanent location for this center is currently under review and will be determined by the results of an overall evaluation of emergency plant response facilities. The preliminary design of the permanent technical support center (PTSC) will be available by January 1,1980. The projected implementation schedule of the PTSC will be provided with the preliminary design.
e