05000324/LER-1979-087-03, /03L-0:on 791029,containment Valve Would Not Operate During Core Auxiliary Cooling Sys Component Test. Caused by Travel Stops Out of Adjustment.Travel Stops Correctly Set

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/03L-0:on 791029,containment Valve Would Not Operate During Core Auxiliary Cooling Sys Component Test. Caused by Travel Stops Out of Adjustment.Travel Stops Correctly Set
ML19210D279
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/29/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D274 List:
References
LER-79-087-03L-01, LER-79-87-3L-1, NUDOCS 7911260223
Download: ML19210D279 (1)


LER-1979-087, /03L-0:on 791029,containment Valve Would Not Operate During Core Auxiliary Cooling Sys Component Test. Caused by Travel Stops Out of Adjustment.Travel Stops Correctly Set
Event date:
Report date:
3241979087R03 - NRC Website

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60 6l DOCK ET NUV8ER 68 69 EVEn.T 0 ATE 74 75 REPORT DA.TE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l"OT21 l While performing PT 16.1.1. CAC System Comoonent Test. CAC-V5 containment I

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