05000334/LER-1979-043-03, /03L-0:on 790301,during Period Mar-Sept 1979, Analysis of Diesel Fuel Not Completed within Specified Time. Caused by Incomplete Instructions for Modes 5 & 6.Chemistry Manual Revised to Clarify Sampling

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/03L-0:on 790301,during Period Mar-Sept 1979, Analysis of Diesel Fuel Not Completed within Specified Time. Caused by Incomplete Instructions for Modes 5 & 6.Chemistry Manual Revised to Clarify Sampling
ML19210D133
Person / Time
Site: Beaver Valley
Issue date: 11/15/1979
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19210D127 List:
References
LER-79-043-03L, LER-79-43-3L, NUDOCS 7911200570
Download: ML19210D133 (1)


LER-1979-043, /03L-0:on 790301,during Period Mar-Sept 1979, Analysis of Diesel Fuel Not Completed within Specified Time. Caused by Incomplete Instructions for Modes 5 & 6.Chemistry Manual Revised to Clarify Sampling
Event date:
Report date:
3341979043R03 - NRC Website

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NRC FORM 366 U. S. NUC' EAR REGULATORY COMMISSION (7 77)

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60 61 COCKET Nuv8ER h4 63 EVENT DATE 14 7b REPORT D ATE 80 EVENT OESCRIPTION AND PROS A8LE CONSEQUENCES h o 2 lDuring a routine audit of Chemistry records on 10/22/79, it was observed that I

[TTT1 I samples of diesel fuel from the fuel storage tank for the emercency diesel I

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lcencrators were beine taken as required hv the Technical Snecifications.

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o s Iduring the period March through September, 1979, there were several occasions when

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l E Ianalysis of the samples was not connleted within the required time.

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33 03 36 31 40 41 42 4J 44 47 CAUSE OESCRIPTION ANO CORRECTIVE ACTIONS l Chemistry personnel failed to analyze the samples within the allowable time limits l

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g ]because of incomplete instructions in the Chemistry manual for Modes 5 and 6.

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m ] Chemistry manual was revised to clarify Technical Specification sampling and l

g l analysis requirements. Chemistry personnel were issued letters stressing the l

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