05000366/LER-1979-104-03, /03L-0:on 790915,oxygen Bottle Providing Reagent Gas for Hydrogen Analyzers Found Empty,Resulting in Inoperative Analyzers.Standing Order Issued to Monitor Use of Bottles for Determining Change Frequency

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/03L-0:on 790915,oxygen Bottle Providing Reagent Gas for Hydrogen Analyzers Found Empty,Resulting in Inoperative Analyzers.Standing Order Issued to Monitor Use of Bottles for Determining Change Frequency
ML19209B745
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 10/03/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B741 List:
References
LER-79-104-03L, LER-79-104-3L, NUDOCS 7910100387
Download: ML19209B745 (2)


LER-1979-104, /03L-0:on 790915,oxygen Bottle Providing Reagent Gas for Hydrogen Analyzers Found Empty,Resulting in Inoperative Analyzers.Standing Order Issued to Monitor Use of Bottles for Determining Change Frequency
Event date:
Report date:
3661979104R03 - NRC Website

text

.C F Of'." 36G 771 LICEtjSEE QVENT REPORT

, CON THOL uLOCK: l l

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lh (PLE ASE FHINT OR TYPE ALL REQUIRED INFCRMATION) 8 I c 1 A i e I r I n l 2j@l n in lo Io lo ldn._la i o I n I al@L4 I i I i I t I i l@l i

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64 63 EVENT CATE 14 73 REPQHT D ATE 83 8

60 El COCKE T NuvaEsi EVENT OESCRiPTION AND PrtO9 ABLE CONSEQUENCES h TIT]l The o.:vgen bottle providing the source of reatent gas for the hydrogen analyzers o

, 3 l (2P33-P001A and 2P33-P001D) was found to be empty. The empty bottle resulted in---

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4 l the analyzers being inoperative. There was no effect'on the environs. There have l

, 3 l been no similar occurrences of this type.

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l 80 COMP.

VALVE SYSTEM CAU55

CAUSE

COCE COJE SUSCCOE CC*APONENT CODE SU8 CODE SU8CCCE lS !E lh W@ l Xlh l II Nl SITlRIUlh W h [Z_] h o

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9 to it ti 13 18 19 20 SEcuE N TI A L OCCUR R Ef 4CE REPORT REVISION LE R/Ro EVE NT YE A R REPORT NO.

CCOE TT PE No.

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21 22 23 24 26 27 28 29 30 38 32 QN C PLANT MET O Hour 3 SE 1 FOR1 8.

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40 48 42 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h [The analyzers were inoo because thev bad no rew mt gn flou to the hydrogen cells. _A_j

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i new bottle or gas was installed and the analvzers returned to operable status.

7TTl I standing order has been written to survev the usage of the reagent gases to determine _,_,J i

3 i the frequency needed for replacing gas bottles. Procedure HNP-?-1060, Daily Rounds, l

I will be revised to include frequent checks of gas pcessure. The Unit I system was l

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8 9 10 11 44 45 PERSONNEL EXPC0VdE5 NUf.t P E R TYPE DESCRIPflotl l

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8 9 IC 912-367-7781 R. T. Nix PHC -L NAME OF PREPARER

Ccorgia Power Company' Plant E. 1. llatch Baxley, Georgia Reportable Occurrence Report No. Su-366/1979-104 s

Cause Description and Corrective Actions (cont.)

checked and found not to operate on bottled reagent gas.

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