ML19209B745

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LER 79-104/03L-0:on 790915,oxygen Bottle Providing Reagent Gas for Hydrogen Analyzers Found Empty,Resulting in Inoperative Analyzers.Standing Order Issued to Monitor Use of Bottles for Determining Change Frequency
ML19209B745
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 10/03/1979
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B741 List:
References
LER-79-104-03L, LER-79-104-3L, NUDOCS 7910100387
Download: ML19209B745 (2)


Text

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LICEtjSEE QVENT REPORT (PLE ASE FHINT OR TYPE ALL REQUIRED INFCRMATION)

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8 60 El COCKE T NuvaEsi EVENT OESCRiPTION AND PrtO9 ABLE CONSEQUENCES h TIT]l The o.:vgen bottle providing the source of reatent gas for the hydrogen analyzers o in--- l

, 3 l (2P33-P001A and 2P33-P001D) was found to be empty. The empty bottle resulted l

3 4 l the analyzers being inoperative. There was no effect'on the environs. There have l

, 3 l been no similar occurrences of this type.

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l a d l 80 CAUSE COMP. VALVE SYSTEM CAU55 SU8 CODE SU8CCCE COCE COJE SUSCCOE CC*APONENT CODE o 9 8

lS !E 9 to lh W@ l Xlh l II Nl SITlRIUlh W h [Z_] h it ti 13 18 19 20 REVISION SEcuE N TI A L OCCUR R Ef 4CE REPORT REPORT NO. CCOE TT PE No.

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. i o [The analyzers were inoo because thev bad no rew mt gn flou to the hydrogen cells. _A_j A I t i i i new bottle or gas was installed and the analvzers returned to operable status.

7TTl I standing order has been written to survev the usage of the reagent gases to determine _,_,J l

i 3 i the frequency needed for replacing gas bottles. Procedure HNP-?-1060, Daily Rounds, l

.i 4 I will be revised to include frequent checks of gas pcessure. The Unit I system was Sa 8 9 " #

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ISSU E C SCRIPTION

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  • R. T. Nix PHC -L 912-367-7781 NAME OF PREPARER

Ccorgia Power Company' -

Plant E. 1. llatch Baxley, Georgia Reportable Occurrence Report No. Su-366/1979-104 s

Cause Description and Corrective Actions (cont.)

checked and found not to operate on bottled reagent gas.

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