ML19209B474

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IE Insp Rept 50-313/79-15 & 50-368/79-13 on 790708-0809. Noncompliance Noted:No Requalification Training Schedule for Licensed Operators
ML19209B474
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 08/22/1979
From: Johnson W, Spangler R, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19209B467 List:
References
50-313-79-15, 50-368-79-13, NUDOCS 7910090768
Download: ML19209B474 (15)


See also: IR 05000313/1979015

Text

.

.

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEfiENT

REGION IV

Report Nos. 50-313/79-15

50-363/79-13

Docket Nc.

50-313

License No. DPR-51

50-358

License No. NPF-6

Licensee:

Arkansas Fr er ar.d Light Company

,

P. O. Box 551

Little Roc' , Arkansas 72203

<

Facility .are:

Arkansas Nuclear One (AN0), Units 1 and 2

Inspection At:

ANO Site, Russellville, Arkansas

Inspection Conducted: July 8 - August 9,1979

Inspectors:

7 _. I. M I' = - w

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B/SV79

W. D. Johnson, Resident Reactor Inspector

Date

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R: G. Spangler, Refctor Inspector

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G. f . p)'erduzco, Reactor' Inspector

Date

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Sv. R. Dean,RepctorInspector

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R. Smith, Reactor Inspector

Date

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E. A. Cupp, Reactor Insp'ector

Date

Approved By:

7'[<

9/a 2/79

T. F. Westerman, Chief, Reactor Projects Section

Date

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.

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Inspection Summary

Ins ~ ection conducted during period of July 8 - August 9,1979 (Report No. 50-313/

p

79-15)

Areas Insoscted:

Routine, announced inspection of training, requalification

training. surveillance of pipe support and restraint systems, refueling mainten-

ance, :15c: coerations, followup on previously identified item.s, isothermal

tencera ure coefficient of reactivity measurement, and on-site review committee

activiti es .

The inspection involved 243 inspector-hours on-site by six (6) NRC

inspect:rs.

Results:

aithin the eight areas inspected, one item of noncompliance was

identriec (Infraction - requalification training, paragraph 3).

Inspection conducted during period of July 8 - August 9,1979 (Report No. 50-36C{

79-13)

Areas Insoected:

Routine, announced inspection of plant conditions, training, requal-

ification trafiiing, startup testing, 20% testing plateau data review. The inspection

involved 103 inspector-hours on-site by six (6) NRC inspectors.

Results: Within the four areas inspected, no items cf noncompliance were identified.

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DETAILS

1.

Persons Contacted

J. P. O'Hanlon, ANO General Manager

G.

H. Miller, Engineering & Technical Support Manager

L.

Jexander, QC Engineer

B. '

Eaker, Operations Superintendent

7. i. Cogburn, fluclear Engineer

E. C. Ewing, Production Startup Supervisor

!- w . coma, Scheduler

S. 2 Tenvilliger, Operations and Maintenance Manager

S. Pe rel, Licensing Engineer

F. Foster, Plant Administrative Manager

M. Stroud, Electrical Maintenance Supervisor

R. Eider, I&C Supervisor

J. McWilliams, Planning & Scheduling Supervisor

J. Vandergrift, Training Supervisor

T. Green, Training Coordinator

D. Trimble, Licensing Manager

C. Shively, Plant Performance Engineer

D. Barton, Training Coordinator

The inspectors also contacted other plant personnel, including operators,

technicians and administrative personnel.

2.

Inspector Followup on Previously Identified Items

(Closed) Unresolved Item 313/7703-14 (Inspection Reports 77-03 and 77-18,

paragraph 2):

Perfomance of local leak rate testing of six valves in the

reverse direction.

The inspector reviewed the completed job orders shown below and determined

that the six valves in question had been leak tested in the accident

direction prior to plant startup following the last refueling outage (R3):

Valve No.

Penetration No.

Job Order

SF 44; SF 43

19

7512

.,

CV-1053

70

7540

CV-4446

68

7538

CV-1214; CV-1216

14

7511

(Closed) Unreselved Item 313/7907.-02, 368/7907-02 (Inspection Report 79-07,

paragraph 7A):

Consideration of explosive atmospheres in Procedure 1005.18,

Control of Combustibles.

Revision 1 to Procedure 1005.18, in paragraph 5, requires that the recomen-

dations of NFPA 327-1975 be followed for welding, cutting, grindings, -ets . ,

in an explosive atmosphere.

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$

(Closed)UnresolvedItems 313/7907-05, 368/7907-05 (Inspection Report 79-07,

paragraph 7D):

Define the applicable portions of the QA topical applicable

to the Fire Protection Program.

The "nspector and the senior QC Engineer on site concluded that all portions

of the QA topical, with the exception of vendor qualification criteria and

the annual generic review of the fire protection program, apply to Technical

Sce:ification fire protection hardware and related v;ork. The Safety Review

Ccmittee (SRC) will do the annual generic review of the program rather than

ACSL CA organization.

(Cl sec) Unresolved Items 313/7902-04, 368/7902-13 (Inspection Report 79-02,

paragrapn 4):

Failure of Procedure 1 '4.14 to provide for documentation of

work cescription and post-maintenance

2ckout.

Revision 2 to Procedure 1004.14 implements a revised Job Order form and

includes instructions for its use that specifically addresses the require-

ments of ANSI 18.7.

(Closed) Unresolved Items 313/7822-02; 313/7822-03 (Inspection Report 78-22,

paragraph 4): Operator Errors in the evolution for the recirculation of

tank T-10.

The inspector reviewed the disposition of the licensee's nonconformance report

number 78.

(Closed) Unresolved Item 313/7'"2-22 (Inspection Report 78-12, paragraph 13):

Quorum approval by SRC.

Based on a management meeting between IE Region IV mar gement and AP&L manage-

ment conducted on February 9, 1979, this matter is considered resolved.

(Closed) Open Items 313/7902-02; 368/7902-09 (Inspection Report 79-02,

paragraph 4): The role of the Planning and Scheduling Division in the

issuance and processing of job orders was not called out by procedure.

Procedure 1004.14, Revision 2, Issuance and Processing of Job Orders, now

defines the role of Planning and Scheduling Division with regard to processing

job orders.

(Closed) Open Item 313/7902-01 (Inspection Report 79-02, paragraph 5): Test

and calibration of the Unit 1 Inverter Static Switches.

The inspector reviewed the completed job orders 5849, 5850, 5851, 5852, 5853

and 5054.

These job orders implemented for each inverter static switch TC-1

to procedure 1304.85 which reset the instantaneous overcurrent transfer point

to maximum and the undervoltage transfer point to a minimum.

Each inverter

static switch was tested to ensure that the switch would not transfer for

load increases to 150% and that the undervoltage transfer set point was

approximately 80 volts.

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(Closed) Open Item 313/7909-16 (Inspection Report 79-09, paragraph 9E):

Load analysis of DG-1 with P78 loading.

This analysis was submitted to NRR by AP&L letter dated December 3,1973.

(Clesed) Open Item 313/7909-01 (Inspection Report 79-09, paragraph 6):

Review of acceptance test and environmental qualifications of engineered

safaty features switchgear room chiller units.

The Ms:ector reviewed the startup testing conducted under work plan 71

wnicn was completed Fay 4-5, 1979.

No problems were identified.

AP&L

Lic2rsing and NRR are corresponding to resolve the questions of environ-

mer. ai ;_alificati ns for the chillers.

IE plans no further followup in

this area unless recuested by NRR.

(Cicsec) Open Item 313/7822-05 (Inspection Report 78-22, paragraph 4):

Operations logs da not show Technical Specification safety limits for

apprcpriate parameters.

The operations log sheets have been reissued to show Technical Specification

limits on the appropriate parameters.

(Closed) Open Item 313/7909-02 (Inspection Report 79-09, paragraph 7):

Improper isolation valve numbers on attachment D to 1104.29, page 5/5.

Permanent change 6 to revision 4 of 1104.29 corrects the isolation valve

numbers for RE 3810.

(Closed) Open Item 313/7909-08 (Inspection Report 79-09, paragraph 7):

Improper realignment steps in procedure 1104.36, supplement 1.

Revision 3 of 1104.36, Diesel Generator Operability, contains the proper

realignment steps to ensure that the Diesel Generators are returned to ESF

standby following surveillance testing.

(Closed) Open Item 313/7909-14 (Inspection Report 79-09, paragraph 7):

Addition of a caution statement in procedure 1004.19 to avoid hanging tags in

a manner which could obscure control board indication.

Permanent change 1 to 1004.19, Caution and Hold Card Tagging, wad the

appropriate caution statement to the procedure.

(Closed) Item of Noncompliance (Inspection Report 313/79-02, paragraph 4):

Failure to perform surveillance testing on P34A (low pressure safety

injection pump) prior to removing P34B from service.

The inspector reviewed Operations iiemorandum 34, dated February 15,1979, and

conducted discussions with two Shift Supervisors and determined that they

were aware of the incident. This completes the followup for the licensee

response.

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(Closed) Open Item 313/7910-07 (Inspection Report 79-10, paragraph 8):

Drawing errors - M402 and M204.

The drawing errors noted in the referenced inspection report have been

Cor*ected.

3.

Tri+c and Recualification Training (Units 1 & 2)

The wroose of this inspection was to evaluate the licensed operator and

Dair:er.arce personnel training program and determine if the training program

was " ccnformar:ce with the regulatory requirements and requalification

trair"ng program approved by fiRC.

The inspector's review included the following points:

The inspector reviewed records for ten licensed operators (RO) of

.

which four were senior operators (SRO).

Annual requalification exams and grades - January through June 1978

.

exams and part of the exams for 1979.

These are presently being

graded and evaluated. The RO's are graded. The SR0's are not

graded.

Records of requalification lecture attendance.

.

Records of on-the-job training, including reactivity manipulations.

.

Records of self-study requalification program topics.

.

Annual operator evaluations and evaluation of actions taken on actual

.

and simulated abnormal and emergency conditions.

Reviewed three lecture lesson plans for Unit 1, and two lecture lesson

.

plans for Unit 2.

Interviewed selected operators from the group of records reviewed.

.

Reviewed requalification program for changes since last f1RC review.

.

Reviewed on-the-job training records for selected maintenance personnel.

.

The inspector reviewed the 1978 annual requalification exams for SR0 and R0's

to determine if the subsequent training program lectures had been scheduled

and conducted for areas where the operators had made a score of less than 80%.

This requalification program is required by 10 CFR 55, Appendix A.

Appendix A, Section 1, states in part that, " Schedule - The requalification

program shall be conducted for a continucus period not to exceed two years,

and upon conclusion shall be promptly followed, pursuant to a continuous

schedule, by successive requalification programs." Section 2 of Appendix A

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further states that the requalification program shall include preplanned

lectures on a regular and continuing basis throughout the license period

in those areas where annual operator and senior operator written exam-

ination indicate that emphasis in scope and depth of coverage is needed.

Ap.cendix A, Section 4.C, requires eko that systematic observation and

evihation of performance and competency of licensed operators and senior

c era: rs by supervisors and/or training staff members, including evaluation

of a:: uns taken, or to be taken during actual or simulated abnormal and

em-rgency conditions. Section 4.2.5 of the requalification program for

Uni: 1. and Secticr 13.2.1 of the Unit 2 FSAR further amplifies the require-

men:: cf the CFR above.

Cen rary to these requirements, a schedule was not provided for these

lectures and requalification programs resulting in lectures not being given

to three licensed operators in areas where weaknesses were noted in the

annual requalification exams. The inspector also found one operator of the

group reviewed that did not have a performance evaluation.

In discussion

with the licensee training coordinator, it was detennined that the perfor-

mance evaluation was not completed. Also, the. training coordinator found

that two additional operators had not had the performance evaluation.

This is considered an item oi .;oncompliance.

(313/7915-05)

,

4.

Pipe Supports (Unit 1)

The inspector examined selected safety-related piping supports and restraints

as well as relevant procedures and records to ascertain whether surveillance

of restraints and supports is being conducted as required by Technical

Specifications, licensee commitments, and approved programs and procedures.

The following procedures were reviewed:

1304.82, Rev.1, 4/4/79, Functional Tes and Calibration ( f

.

Suppressors

1304.84, Rev. 4,1/18/79, Hydraulic Shock Suppressors Visual

.

Inspection

1304.99, Rev. O, 4/7/79, Pipe Hanger Preventive Maintenance

.

Procedure 1304.84 is not considered adequate in that:

a.

The procedure presently includes acceptance criteria but has no

,

operability statement.

b.

The procedure data sheet should direct specific attention to the

condition of the bleed hole, clevis, fasteners and seals, as well as

reservoir level. The data sheet of 1304.84, Rev. 3, included these

observations, but Rev. 4 eliminated them.

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Procedure does not assign specific responsibility for a review of

c.

the snubber visual inspection findings.

Items a. through c. above are considered an open item and will be re-examined

on a subsequent inspection.

(313/7915-01)

Rexrds of snubber visual inspections conducted April 9,1979 and June 19,

1979 w-r3 reviewed.

No items of noncompliance or deviations were

icentified.

The results of the April 1979 functional testing of the following snubbers

were eviewet

r!S-15

55-68

HS-31

HS-69

HS-70

H-C-2

HS-21

HS-49

Acceptance criteria, including lock-up ard bleed velocities, were met in

all cases.

Inspection frequency and sample size were consistent with

'echnical Specification requirements.

The following snubbers were directly examined by the inspector:

HS-1

HS-2

HS-5

HS-7

HS-49

HS-50

HS-82

HS-82 and HS-7 were found to have reservoir levels below 50%.

Further, HS-82

was leaking at the control block and the clevis area had no evidence of

lubrication. The remaining snubbers were in satisfactory condition. This

is an open item.

(313/7915-02)

During the course of the inspection, numerous spring hangers were examined

by the inspector. All were found to be mechanically sound and loaded to

their correct value.

5.

Maior Maintenance Activities (Ilefueling) (Unit 1)

The inspector reviewed the following maintenance activity conducted during

the refueling outage:

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P00RORIBNL

Small ECCS Redesign

This maintenance activity involved cross-connection of HPSI discharge flow

paths to mitigate a small break LOCA coincident with loss of off-site power,

and the failure of one ESF bus, without operator action.

Tne inspector reviewed the Design Change Request (DCR 79-100), the purchase

creers , ard traterial receiving reports concerning the work activities. The

inspector also re,iewed the completed flow test documentation.

(Work Plan 69)

No ': ems of nonccccliance or deviations were identified.

6.

Revis of Plant Operations (Unit 1)

ine inspector reviewed plant logs and records to verify confomance to plant

procedures and to confirm that Technical Specifications were met.

The

inspector also conducted a plant tour of accessible areas to observe general

housekeeping and to verify selected component configurations.

In addition,

the inspector reviewed the licensee's conduct of fire protection inspections.

T:.a following logs and records for June 1979 were reviewed:

RPS Log

NSS Data Point Log

Waste Control Log

ESAS Log

NSS and Safeguard Auxiliary Log

Auxiliary Log, Outside

NSS Hourly Log (Computer)

Station Battery Daily Check

Station tog - Operations

Daily Hot Lab Water Report

Radiochemistry Log

Shift Turnover Log

Jumper and Bypass Log

Caution Tag Log

Hold Card Log

Trouble Tickets

Standing Orders

The inspector noted that there were five (5) outstanding trouble tickets on

the fire detection system and that during the entire week of July 16, 1979,

one of the #1 DG room alarns was in an alarm condition. The licensee

cortmitted to an immediate effort to correct the problems with this system.

(0 pen Item 313/7915-03)

The inspector selected several entries in the Jumper and Bypass Log and the

Tag Logs and with a licensee representative observed those selections to

verify installation was in agreement with the logs.

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The following general observations were made during the plant tour:

No excessive fluid leaks or piping vibrations were observed.

Selected valves were observed to be in the required positions.

.

Selected equipment caution and hold tags were verified to be

.

carrect.

Centrol room operators were knowledgeable in annunciator status.

Zeiected recorders were recording properly.

.

.

?.adiation controls were observed to be established properly.

Control room manning was in accordance with Technical Specifications.

.

Cleanliness was satisfactory.

.

Fire extinguishers were unebstructed and had been currently inspected.

.

Shift turnover was conducted satisfactorily.

.

No items of noncompliance or deviations were noted.

7.

Review of Plant Operations (Unit 2)

The inspectors reviewed plant logs and records to verify conformance to

plant procedures and to confirm that Technical Specifications were met. The

inspectors also conducted a plant tour of accessible areas to observe general

hcusekeeping and to verify selected component configurations.

In addition,

the inspectors reviewed the licensee's conduct of fire protection inspections.

The following logs and records for June 1979 were revieweh

Station Battery Daily Check Log

Station Log - Operations

Auxiliary Operator's Outside Log

CPC/CEAC Auto Restart and Sensor Failure Log

CEA Position Log

Daily Shift Containment Sump Discharge Log

Shutdown Log (Modes 5 and 6)

Control Room Log

Daily Hot Lab Water Report

Radiochemistry Log

Shift Turnover Log

Jumper and Bypass Log

Caution Tag Log

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Hold Card Log

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Trouble Tickets

Standing Orders

.

.

j

The inspector selected several entries in the Jumper and Bypass Log and

the Tag Logs and with a licensee representative observed these selections

to verify installation was in agreement with the logs.

The following general observations were made during the plant tour:

' c excessive fluid leaks or piping vibrations were observed.

.

Seismic restraints and pipe hangers appeared to be in satis-

.

factory condition.

Selected valves were observed to be in the required positions.

.

Selected equi;=ent caution and hold tags were verified to be

.

correct.

Control recm operators were knowledgeable in annunciator status.

.

Selected recorders were recording properly.

.

Radiation controls were observed to be established properly.

.

Control room nanning was in accordance with Technical Specifications.

.

Fire extinguishers were unobstructed and had been recently inspected.

.

Shift turnover vias satisfactory.

.

In general, plant cleanliness was satisfactory.

However, the inspector noted

two (2) opened quart cans of oil and a closed 55 gallon barrel of Mobil 445

in the north diesel generator room and one (1) opened quart of oil in the

south upper penetration room.

Upon notification, the licensee corrected these

problems.

Unit 2 has a permanent fire watch (security guard) stationed in the 372-foot

level hallway which also includes the entrance to the cable spreading room.

This station will be maintained until the fire protection system is in full

operation.

No items of noncompliance or deviations were noted.

8.

Followup on Licensee Event Reports (Unit 1)

The inspector reviewed the design change packages and work plans associated

with the design changes engineered to correct deficiencies identified in

the following licensee event reports (LER's):

77-19

Inadequate Chiller Units for Engineered Safety Features

Switchgear Rooms

78-09

Possible Inadequacy of HPI Flow for Certain Size Small

Breaks in the RCS

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9.

Review of Isott;ernal Temperature Coefficient of Reactivity Measurement

(Unit 1)

The purpose of this inspection effort was to review the procedures and

results for the measuring of the Isothermal Temperature Coefficient of

Reactivity.

Tre %:cector reviewed Procedure 1302.16, Isotherma? Tempertture Coefficient

Of hea :ivity Measurement.

Data reviewed was that of the latest test con-

cu :ed by the licensee for the above procedure. The inspector noted that

cur'n; the perfcrmance of the Isothermal Temperature Coefficient of Re-

at:te":y test, the controlling rod group was moved in order to increase

raa::cr power within the intermediate range. Although not specifically

pr:nicitea by the above procedure, control rod movement during Temperature

Ccefficient of Reactivity Measurements necessitates that reactivity

associated with rod movement be mathematically accounted for in data

at:alysis. Thus, the rrsults achieved may not be as accurate as is possible

had rod covement and r2 actor power been adjusted prior to the controlled

data runs. A licensee representative indicated that a review of the

procedure would be done to consider these concerns.

fic items of noncompliance or deviation were found.

10.

Followuo to IEB 79-02 (Unit 1)

On May 25, 1979 an inspector observed the torque tests performed by the

licensee for the following supports:

Sucoort

Sketch

HBD-21-H102

12-2178

HSD-14-SW20

12-1457

HBD-14-SWl8

12-1455

HBD-21-H52

12-2161

HBD-21-H60

12-2164

This work was performed according to procedure 11406-276-5.

flo items of

noncompliance or deviations were noted,

11.

Review of 20% Power Plateau Data (Unit 2)

The inspector reviewed the completed test data for 2.800.01, Appendix U,

Unit Load Transient Test, to verify that the licensee had properly evaluated

and approved the test results.

The inspector also reviewed the licensee's evaluation of the 20% power

plateau test results and his authorization to proceed to the next test

plateau. The Plant Safety Conuittee (PSC) and the Test Working Group (TWG)

met jointly on June 12, 1979. At this meeting, the 20% poser plateau test

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results were reviewed and found to be acceptable. The PSC Chairman, the

TWG Chaiman and the General Manager signed Step 7.6.6 of Procedure

2.800.01, Power Ascension Test, giving authorization to proceed to the

50.',' power test plateau.

No items of noncorpliance or deviations were identified.

12.

Insrector Witness of Power Ascension Testing (Unit 2)

Th2 in cacter witnessed the performance of an NSSS Calorimetric at the 50%

pcser alateau. The test was performed in accordance with Procedure 2.800.01,

A::crdix I.

This tect determines core thermal powar by means of a secondary

hec: :c!ance ar.d verifies the COLSS thermal power calculations.

Tbc

.spector witr.essed portions of the performance of the isothermal

tem erature coefficient and power coefficient test at the 50% power plateau.

The as was perfcrned in accordance with Procedure 2.800.01, Appendix R.

The irspector witnessed portions of the perfornance of the unit load transient

test at the 50% power plateau. The test was performed in accordance with

Procedure 2.800.01, Appendix U.

The inspector also witnessed portions of the performance of the shape

annealing matrix and boundary condition measurement at the 50% power plateau.

This test was performed in accordance with Procedure 2.800.01, Appendix W.

The inspector noted that during this test, power varied by more than the

+ 0.2% specified by Step W.2.8 of the Procedure. A licensee representative

agreed to evaluate this matter to determine if it could affect test results.

(0 pen Item 368/7913-01)

During the above tests, the inspector verified the following items:

Latest procedure revision in use

.

Minimum crew requirements net

.

Test prerequisites and initial conditions met

.

Procedure is adequate

.

Crew action correct and timely

.

Adequate test coordination

.

Trial data assembled

.

Acceptance criteria met

.

Licensee's preliminary evaluation is adequate

.

The tests were observed to have been adequately conducted.

No items of non-

compliance or deviations were identified.

13.

Onsite Review Comnittee (Units 1 and 2)

The inspector reviewt

the activities of the Plant Safety Committee (PSC) in

order to ascertain whether the Conmittee's review functions are being con-

ducted in accordance with Sections 6.5.1 of the Unit 1 and Unit 2 Technical

Specifications. These sections state the membership, meeting frequency,

quorum, review and record keeping requirements for the PSC.

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The inspector's findings are described below.

a.

The plant Procedure which governs the PSC activities is 1005.01, the

Administrative Controls fianual.

The current revision of this Procedure

(Revision 3, dated January 31,1977) is outdated with respect ta the

description of the PSC Chairman and the titles of the other mmbers.

At the time of this inspection, a revision to this Procedure was in

reparation. This Procedure was identified as being outdated in a

previcus ir.spection report.

Open items 313/78-22-01 and S63/78-29-01

remain open pending revision of this procedure.

5.

?e preser.t membership and qualifications of the PSC are as required

M the Technical Specifications.

The meeting frequency of the PSC exceeds the Technical Specification

c.

required frequency.

d.

The inspector verified, for selected reviewed items, that those who

participated in the reviews included persons who constituted a quorum

and who possessed expertise in the areas reviewed.

e.

The inspector verified for a selected sample that the items listed in

lechnical Specification 6.5.1.6a through 6.5.1.6j were reviewed by the

PSC as required. The inspector noted that the PSC does not have an

administrative system to assure that the Security Plan and the

Emergency Plan are periodically reviewed as required by the Technical

Specifications.

The Operations and flaintenance !!anager infonned the

inspector that a procedure defining the activities 6nd responsibilities

of the PSC was being developed.

(0penItems 313/7915-04; 368/7913-02)

14.

Containment Purging During flormal Plant Operation (Units 1 & 2)

a.

Unit 1

The licensee received the f1RC letter af fiovember 29, 1978, concerning

containment purging. The licensee's first response to this ietter was

dated January 30, 1979. Thir letter stated an intention to propose a

Technical Specification which will limit purging during operation to

90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year and ccamitted to limit purging during operation to

90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year pending review and approval of the proposed Technical

Specification.

This letter further stated that the licensee's review

of safety actuation signal circuitry has not revealed any manual override

features which unintentionally disables additional safety actuation

signal circuits.

The licensee's second response to the above f!RC letter

was dated April 2,1979. This letter proposed a Technical Specification

which would limit containment purging to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year during plant

operation.

The types of problems described in the tiRC letter of flovember 29, 1978,

relating to potential failures of automatic isolation of the containment

purge isolation valves during power operation do not apply to Af;0, Unit 1.

The Engineered Safeguards Actuation System does not include inputs from

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containment radiation monitors.

The containment purge isolation

valves are closed by Engineered Safeguards channels 5 and 6, which

are actuated by high reactor building pressure. Thus, the problem

of overriding a safety actuation closure signal does not arise at

ANO, Unit 1.

b.

Unit 2

The Technical Specifications of this Unit do not permit opening the

contairnent purge supply or exhaust isolation valves in modes 1, 2,

3 or 4.

Inus, the issue of containment purging during normal plant

cDera:icn dass not apply to this Unit.

15.

IE5/IAL Followuo (Unit 1)

I:2 77-04, Calculational Error Affecting the Design Performance of a System

fcr Controlling pH of Containment Sump Water Following a LOCA:

The Safety Evaluation issued by the Office of fluclear Reactcr Regulation

supporting Amendment tio. 39 to Facility Operating License No. DPR-51

concludes that the licensee's nethodology of pH control is acceptable.

This completes the IE followup for this Bulletin.

16.

Exit Interviews

Exit interviews were conducted at the end of various segments of this

inspecticn with Mr. J. P. O'Hanlon (Plant General Manager) and other

members of the AP&L staff.

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