ML19209A395

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IE Insp Rept 50-312/79-11 on 790612-0712.No Noncompliance Noted.Major Areas Inspected:Operator Training Pertaining to TMI Incident,Design Changes,Procurement & Reactor Operations & Licensee Response to IE Bulletins & LERs
ML19209A395
Person / Time
Site: Rancho Seco
Issue date: 08/20/1979
From: Bagaglio M, Canter H, Faulkenberry B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML19209A393 List:
References
50-312-79-11, NUDOCS 7910030784
Download: ML19209A395 (6)


See also: IR 05000312/1979011

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U.S. fiUCLEAR REGULATORY COMMISSION

OFFICE OF If1SPECTION AND ENFORCEliEfiT

Region V

Report No.

50-312/79-11

Docket flo.

50-312

License fla.

DPR-54

Safeguards Group

Licensee:

Sacramento Municipal Utility District

P. O. Box 15830

Sacramento, California 95813

Facility Name:

Rancho Seco

Inspection at:

Clay Station, California

Inspection Conducted:

, June 12 - July 12,1979

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Inspectors:

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A. D. Jo nso (, Reactor Inspector

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P. H. Joh son, Reactor Inspector

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J. D. Carlson, Reactor InspEtor

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. B. 76etziW, Reacto Inspector

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f. J. Morrill, Reactor Inspector

Date Signed

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Approved By:

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B. H.iFaplkenberry, Chief, Reactor Projects Section 2

'Date Signed

Keactor Operations and fluclear Support Branch

Summary:

Areas Inspected: Operator training pertaining to "Three Mile Island" incident,

IE Bulletins, Licensee Event Reports, tpecial tests, design changes, procurement

and reactor operations. The inspection involved 252 inspector hours onsite by

nine NRC inspectors.

Resul ts :

fio items of noncompliance or deviations were identified.

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DETAILS

1.

Persons Contacted

  • R. Rodriguez, Manager, Nuclear Operations
  • F. Oubre, Plant Superintendent
  • G. Coward, Maintenance Supervisor
  • R. Colombo, Technical Assistant
  • R. Miller

W. Ford, Operations Supervisor

R. Wichert, Plant Mechanical Engineer

J. Mau, Training Supervisor

H. Heckert, Engineering Technician

J. McColligan, Supervisor, Engineering and Quality Control

2.

Auxiliary Feedwater System Tests

The inspectors examined the approved test procedures and results of

the auxiliary feedwater system tests to verify system performance

STP-070, Auxiliary Feedwater Flow verification test,

capabilities.

verified:

that using either auxiliary feedwater pump, adequate flow

a.

would be supplied to each steam generator;

that with the ICS overridden, auxiliary feedwater flow was

b.

capable of being manually controlled;

that upon loss of both main feedwater pumps, auxiliary feedwater

c.

flow would be initiated; and

that upon loss of air pressure, the auxiliary feedwater control

d.

valves can be manually closed.

STP-071, Auxiliary Feedwater Pump Endurance Test, verified the

endurance capability of the auxiliary feedwater pumps by continuous

operation of each for forty hours.

In addition to performing the above examinations the inspectors witnessed

those portions of the tests described in STP-070 a. and b. and a

portion test described in STP-071.

No items of noncompliance or deviations were identified.

  • Denotes those attending exit interview.

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3.

IE Bulletins

The inspector confirmed the information submitted by the licensee in

response to IE Bulletins 79-03, 79-04, 79-07, 79-09 and 79-10 thru

discussion with licensee representatives and by examination of

pertinent documents.

4.

Licensee Event Reports

The inspector confirmed the information contained in Licensee Event

Reports (LER's) f40s 79-03 and 79-04.

5.

Operator Retraining (Inspection Report _ 50-312/79-10)

A representative of General Physics Corporation provided training

to licensed operators at Rancho Seco durIng the weak of June ll, 1979.

This training emphasized small break procedures, the sequence of

events at and lessons learned from Three Mile Island, and other

changes in plant design and procedures made during the recent

shutdown period.

Portions of this training were audited by the

inspectors.

Following the training a General Physics auditor

conducted oral interviews with the operators to verify that they

understood the materials presented and discussed.

An f1RC inspector

also interviewed approximately 50% of the licensed operators

on June 17-18, 1979. These interviews confirmed the effectiveness

of the training and audit program provided by the licensee.

6.

Reactor Trip

A reactor trip occurred on July 12, 1979 while an inspector was at

the site.

Erratic operation of the turbine intercept valves led

to a turbine trip, which tripped the reactor by means of the direct

trip function installed during the recent shutdown. All safety-

related equipment operated as required.

Following evaluation and

trouble-shooting of the turbine control system the plant returned to

power with a brush recorder connected to system parameters of interest.

These parameters showed further instability at a power output of

approximately 200 MWe, and portions of the "D" reheater pressure

transmitter were replaced. Further intercept valve instability

was experienced on July 14, 1979, although a plant trip did not

occur. The licensee replaced the complete "D" reheater pressure

transmitter following this transient, and further difficulties were

not observed.

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7.

Procurement

The inspector examined the following Quality Assurance Procedures

(QAP's) to verify that administrative controls exist relating to

the procurement of safety-related equipment:

QAP-4

Procurement Document Control

QAP-5

Supplier Quality Assurance

QAP-10

Receiving Inspection

QAP-15

Handling, Storage, Shipping and Preservation

QAP-17

Nonconforming Material Control

For selected components in the following listed systems the inspector

verified that procurement specifications contained proper approval

signatures, quality control inspection requirements, and quality

record requirements. The inspector also verified that the items

were inspected upon delivery, handled and stored in accordance with

the plant procedures, and purchased from approved venders. The

inspector toured the warehouse areas and examined the storage

conditions.

Reactivity Control and Power Distribution

Instrumentation

Reactor Coolant System

Emergency Core Cooling System

Containment System

Plant and Electrical Power Systems

No items of noncompliance or deviations were identified.

8.

Design, Design Changes, and Modifications

The inspector reviewed the licensee's program for handling design

changes and modifications.

In addition to the program review,

the inspector examined the documentation for the NRC required

modifications resulting from the Three Mile Island incident.

The

modifications examined were:

Keyswitch cutout of the loss of feedwater and turbine trip

a.

(used for startup and shutdown of the unit.)

b.

Loss of feedwater and turbine trip - reactor trip.

c.

Auxiliary feedwater flow indication.

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d.

Condensate storage tank low level alarm.

No items of noncompliance or deviations were identified.

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9.

Management Interview

The inspectors met with licensee representatives at the conclusion of

the inspection and reviewed the scope and findings of the inspection.

The inspectors inforr.ed the licensee that no items of noncompliance

or deviations were identified during the course of the inspection.

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