ML19209A261
| ML19209A261 | |
| Person / Time | |
|---|---|
| Site: | Perry |
| Issue date: | 09/13/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Davidson D CLEVELAND ELECTRIC ILLUMINATING CO. |
| References | |
| NUDOCS 7910030242 | |
| Download: ML19209A261 (1) | |
Text
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'o UNITED 0TATES
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NUCLEAR REGULATORY COMMISSION 3,,
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,E REGION ll!
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o, 799 ROOSEVELT ROAD t TN ELLYN. RLINOIS 6o137 Docket No. 50-440 SEP 1319I3 -
Docket No. 50-441 The Cleveland Electric Illuminating Company ATTN:
Mr. Dalwyn R. Davidson Vice President - Engineering P. O. Box 5000 Cleveland, OH 44101 Gentlemen:
The enclosed IE Circular No. 79-19, is forwarded to you for informatica.
No written response is required. Should you have any questions related to your understanding of this matter, please contact this office.
Sincerely, g Tames & &'eppYer G_,
0..
G. K Director
Enclosures:
1.
IE Circular No. 79-19 2.
List of IE Circulars Issued in the Last 6 Months cc w/enu:
Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local ?DR NSIC TIC Harold W. Kohn, Power Siting Commission Mr. Daniel D. Wilt, Attorney u)S7 U4 IO10 08 0 2
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SSINS:
6830 Accession No: 7908220111 UNITED STATES i
NUCLEAR REGULATORY CCMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D. C.
20555 E
September 13, 1979 IE Circular No. 79-19 s
LOOSE LOCKING DEVICES ON INGERSOLL-RAND PUMP IMPELLERS Description of Circumstances:
Three reports have been submitted to the NRC regarding the loosening of locking devices on the impellers of pumps manufactured by the Ingersoll-Rand Company.
p The first report was submitted at a sigrificant deficiency (10 CFR 50.55[e])
by Arkansas Power and Light Company in letters of March 17, 1978 and May 9, r
1978. The licensee reported excessive noise and vibrations in both Low Pressure Safety Injection (LPSI) pumps during the preoperational test program on Unit 2 of Arkansas Nuclear One (ANO).
It was discovered that the washers, jam nut and cap nut used to retain the impellers were missing on both pumps (Ingersoll-Rand Type 8X20WD).
The licensee's corrective action involved the installation of a tab washer.
This corrective action was, also, taken on the containment spray pumps (Ingersoll-Rand Type 6X23WD) because of similarity of design.
E The second report was submitted by Duke Power Company in a licensee event l
report (LER 50-287/78-23) dated January 24, 1979.
The symptoms were similar i
to those observed at AND Unit 2 in that high vibration was detected in a reactor building spray pump (Ingersoll-Rand Type 4X11A) for Oconee Unit No. 3.
The licensee found that the impeller had worked loose. The corrective action included a revision to the mainteinance procedure to specify torque requirements.
The third report was 10 CFR 21 Report No. 79-01 submitted by Portland General Electric Co. on April 16, 1979. This report identified a deficiency that may i
exist in the Trojan Nuclear Plant containment spray pumps (Ingersoll-Rand Type 6X23WD) in that there is a potential for the impeller lock nut to loosen.
The potential deficiency was identified because of the similarity of the containment
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e spray pumps design to the residual heat removal (RHR) pumps (Ingersoll-Rand Type 8X20WD) and the discovery of a loose lock nut on an RHR pump during pump maintenance. The corrective action was to provide a positive mechanical lock on the impeller nut.
Westinghouse Nuclear Service Division has i: sued a Technical Bulletin to Westing-house plant owners on looso lock nuts on Ingersoll-Rand Types W, WD, and WDF pumps.
Excerpts from that Technical Bulletin are in Enclosure No. 1.
Combustion Engineering, Inc. has, also, informed the NRC of their actions relative to the same problem in a letter dated March 13
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