ML19208B468

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Ro:On 790517,local Leak Rate Test of RHR Pump B Suction Torus Isolation Valve E11-F004B Showed Valve to Be Leaking in Excess of Specified Criteria.Valve Motor Operator Adjusted
ML19208B468
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 08/29/1979
From: Manry M
GEORGIA POWER CO.
To:
References
PM-79-801, NUDOCS 7909200372
Download: ML19208B468 (4)


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accrgia Power August 29, 1974 PM-?Q-801 PLANT E.

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HATCH Docket No. 60 7?1 Special Renort on RHR Puno Suction Torus Isolation Valve E11-F004B Mr. James P.

O'Reilly Director of Inspection and Enforcement O p' p' D

Region II

'h Suite 3100 bdj 101 Marietta Street Atlanta, Georgia 30302 p[D),- @

T, wUlt;0 L b

Dear Sir:

On May 17, 1979, with the reactor in re fue li ng, a Local Leak Rate Test (LLRT) of the RHR nuno "B"

suction t o rta s isolation valve E11-F0048 was performed per HNP 1 105?.

This test shoued the valve to be leaking in excess of specified criteria frefer to LER 50-321/1070 033).

Following cor-ective action (lapped seat

eings, laoped
gate, and adjusted the valve's motor operator see MR
  1. 1 79-2423),

the valve was satisfactorily retested on July 26, 1979.

On August 12,

1070, the " B loop of the RHR svstam was placed in service in the shutdown cooling mode of operation, and the

. reactor vessel level was observed to staat dropoing.

Investication showed that if the E11-F065n valve was closed, then the reactor vessel water level vould stabilize.

Thus, the E11-F0049 and/or the E11-F0309 valves were leaking.

On August 13, 1079, the "B"

RHR pumo was run torus to torus in an attempt to flush the seat of the E11-F00hB valve;

however, this had no a p p re c i.a b l e effect on the leakage.

On August 14,

1979, the E11-F0309 (relief valve) was removed and bench-tested satisfactorily.
Thus, the E11-F004R valve was determined to be leaking.

The LLRT performed on the E11-F00hB valve on July 26,

1079, was performed in the direction that it would have to prevent leakage post-LOCA, f.e.,

fron the inside of primary containcient outward; the 1.eaka.ge now exisiting for the E11-F00h9 valve is in the occosite direction, i.n.,

back towards contat.nnent.

This leakage oath f"om the reactor vessel to the nucoression chamber / torus) oniv exists when the "B"

RHR oump is in the shutdown cooling m o(i e of operation.

Thut. it was decided that the leakage or the valve represented no condition that would oreclude normal ocaration.

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he decision w19 then nad.

to peaform a

new LLRT on the 311-F0039 valve in order to ensure that the crimary containment l a t e r,"i t y of the valve still existed.

Thus, on August 14, 1970, a LLRT of the valve was performed.

The a e s u '. t s of this test showed the valve to be Icaking less than the accentance criteria soecified by the Technical Specification a ntf: 10CFR50 accendix J

(.60La overall l e a'c a g e for all tvoe 9 and type C LLRTs, and the leakage of the valve shall b'e 109 enou'dh such that the seal. water inventory of the valve is sufficient for 30 days - the seal water inventorv for the E11-F00hB valve is the torus).

However, the valve leak rate was judged to be excessive by plant personnel and a

deviation "coort

(#1 70 126) was waitten saying that the E11-F00h8 valve had failed the LLRT.

It was determined by the Plant 9eview Board that a

Licensee Event Reco"t was not requiaed since the applicable Technical Specification and 10CFR50 apoendix J

aceeotance criteria had been satisfied; houever, it was decided that a special reoort be written due to the sequence of events.

F o l. l ow i n st maintenance on the valve (tightened fou" bolts on the valve's notor ooerator - MR #1-70 h741),

a satisfactory LLRT was performed on August 16, 107o.

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