05000368/LER-1979-063-03, /03L-0:on 790806,containment Atmosphere Sample Reactor Bldg Penetration Outside Isolation Valve 2SV-8263-2 Would Not Indicate Closed During Stroke Test.Caused by Limit Switch Being Out of Adjustment.Limit Adjusted

From kanterella
(Redirected from ML19208A739)
Jump to navigation Jump to search
/03L-0:on 790806,containment Atmosphere Sample Reactor Bldg Penetration Outside Isolation Valve 2SV-8263-2 Would Not Indicate Closed During Stroke Test.Caused by Limit Switch Being Out of Adjustment.Limit Adjusted
ML19208A739
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/31/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19208A735 List:
References
LER-79-063-03L, LER-79-63-3L, NUDOCS 7909170395
Download: ML19208A739 (1)


LER-1979-063, /03L-0:on 790806,containment Atmosphere Sample Reactor Bldg Penetration Outside Isolation Valve 2SV-8263-2 Would Not Indicate Closed During Stroke Test.Caused by Limit Switch Being Out of Adjustment.Limit Adjusted
Event date:
Report date:
3681979063R03 - NRC Website

text

,

f NRC FORM 366 U S NUCLE AR REGUL ATORY COMMISSION (7 77)

LICENSEE EVENT REPORT EXHIBIT A ccNTRot stock l l l l l } l@

(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION)

AIR l Al Nl b l2 lgl 0 l0 l - j0 0 l 0] Oj 0 l-0 l0 lgg l1 l 1l1 j 1lgl j Jg i

o i

7 8 9 LICENSEE CODE to 15 UCENSE Nuveth 25 2f.

Lut%g twrt Jo 57 C A T St CON'T sC% LLJ@l0 I s p 10 i 0131618 GI0 S l0 617 I9 @ l0}8 13[ 117 l9l@

o 8

60 6'

DOCnET NUvSER td 6

EVENT DATE 28 M PON1 O ATE PC EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES b10 o

2 I During Mode 1 operation, the Cohtainment Atmosphere Sample Reactor 1 Building penetration outside isolation valve, 2SV-8263-2, would not i

o a

lindicate closed during a stroke test.

The inside valve, 2SV-8265-1, at i

o 4

e!s IPenetration 2P58, was verified operable. This occurrence is similar to i

e o i LER 50-368/79-044,79-060, and 79-061.

a i,! i 0ccurrence is reportable per T.S.6.9.1.9.b.

l l

O e

n h*C ilU C A w.,E LAUM f. o* '

..t.t

.A CCDE d CE We t C,(

( j.w nNE NT (:>ut s u

.cgE I, - I N I IS IDl @ L,,Ej @ @ @ lV lA L V j0 PG gg gg i-m 2

6."(gg,ug3%ENTvE4A s, s p~

1 l.17 I 91 L--J 1 0 f6lJ J M

IJ l 3 i LL_J L--J [0j

_4

J 24

, s.

a
i 10 IUib lf h'0 lg JJ

'f 4 JD u

J' 40 di di 42 se a;

cusE os scR.<' icN ANo CcRR EC flVE ACTIONS IInvestigation revealed that the limit switch was out of adjustment.

The L

ilimit was adjusted and the valve was proven operable per T.S.4.6.3.1.1, ii i Table 3.6-1.

The valve was returned to service in less than two hours, I meeting the requirement of Action Statement T.S.3.6.la.

1 I

i 1

e s ec sTa EPOWEF OTwE N s1 ATUC DsG Y

iCo.EH4 DE hH * '.ON LBJ@ 1015 10 l@ Pwr Escal. Testi LAj@l NA l

i t

A C T i v.1 v CONTENT Avou;TcrACTmTvh a.tooNorHr;Eath ati s An a or ut tE Ast LZ_J @ LZ_J8l NA l

NA i

c E asoN E1 E.,cs " Es ass...m~@

ev.E.

T.,E liI l l 010l Ol@[Z_J@l NA l

.E,scNN A',NJ E s

'2 cEsC-,r.cN@

s u.m n il-101010 l@l NA c,: w y a l

i.,

o avuuuv Lcs. or ce DAvAGE To s ACmTv.

,n 1 vet C E sC FI'* T ION 1

M 9

10 p,

is%gC DE sCR PTION

~ '

l 121 e l LEJ@l NA

! !I i l ll1II1 Iil Chris N. Shively 5d1/968-2519

  • ave cr Paf rAnto

,,,g,,

'l909170396