05000324/LER-1979-048-03, /03L-0:on 790805,while Performing Reactor Bldg Exhaust Vent Monitoring Check,Outboard Supply Damper Would Not Stay Closed.Caused by Maladjustment of Control Switch. Switch Readjusted

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/03L-0:on 790805,while Performing Reactor Bldg Exhaust Vent Monitoring Check,Outboard Supply Damper Would Not Stay Closed.Caused by Maladjustment of Control Switch. Switch Readjusted
ML19207B954
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/30/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19207B950 List:
References
LER-79-048-03L-01, LER-79-48-3L-1, NUDOCS 7909060225
Download: ML19207B954 (1)


LER-1979-048, /03L-0:on 790805,while Performing Reactor Bldg Exhaust Vent Monitoring Check,Outboard Supply Damper Would Not Stay Closed.Caused by Maladjustment of Control Switch. Switch Readjusted
Event date:
Report date:
3241979048R03 - NRC Website

text

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