ML19095A346

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Submit Operating Report for the Month of June 1975
ML19095A346
Person / Time
Site: Surry  Dominion icon.png
Issue date: 07/09/1975
From: Stallings C
Virginia Electric & Power Co (VEPCO)
To:
Office of Nuclear Reactor Regulation
References
Download: ML19095A346 (8)


Text

'.

RICHMOND.VIRGINIA 23261 . ' /

/

July 9, *.1975* /.~~i

' *~  !

Office of Plans and Schedules *.:~*/rTJ>.er.;i;~l ijo. 565/021974 Division of Reactor Licensing ~PO&M/JTB: clw U.S. Nuclear Regulatory Commission Washington, D. C. 20555 Docket Nos *<ibi?

License Nos. DPR-32 DPR-37

Dear Sir:

Operating information for Surry Unit Nos. 1 and 2 for the month of June 1975 is attached.

Very truly yours,

~-m#~

C. M. Stallings Vice President~Power Supply and Production Operations Attachment cc: Mr. Norman C. Moseley

DOCKET NO. 50-280 UNIT Surry Unit No. 1 DATE July 2, 1975 COMPLETED BY W. C. Earl AVERAGE DAILY UNIT POWER LEVEL MONTH JUNE

~~~~~~~~~~-

AVER AGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net) DAY (MWe-net) 1 746.6 17 737.1 2 746.4 18 734.5 3 750.4 19 737.0 4 748.4 20 737.6 5 764.4 21 726. 7 6 748.6 22 743.6 7 748.6 23 744.2 8 711. 5 24 367.5 9 748.8 25 0 10 748.8 26 0 11 682.7 27 377~1 12 750.4 28 651.8 13 746.9 29 '748. 3 14 734.6 30 746.2 15 740.4 31 16 739.1 DAILY UNIT POWER LEVEL FORM INSTRUCTIONS On this form, list the average daily unit power level in MWe-net for each day in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the* net electrical rating of the unit, there may be occasions when the daily average power level exceeds the 100% line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.

UNIT Surry Unit No. 1 DATE July 2, 1975 COMP1~ETED BY w. c. Earl DOCKET NO. 50-280 OPERA TING ST ATUS

l. REPORTING PERIOD: _ _o_o_o_1_ _7_5_0_6_0_1_______ THROUGH _ _2_4_0_0___7_5_0_6_3_0_ _ __

HOURS IN REPORTING PERIOD: _ _ 7_2_0___- - : : - . - " : - - = - - - - - - - - - - - - - - - - - - - - -

2. CURRENTLY AUTHORIZED POWER LEVEL (M\Vth) 2441 MAX. DEPENDABLE CAPACITY (MWe-NET) 788
3. LOWEST POWER LEVEL TO WHICH SPECIFICALLY RESTRICTED (IF ANY) (MWe-NET):
4. REASONS FOR RESTRICTION (IF ANY):

THIS CUMULATIVE REPORTING PERIOD YR TO DATE TO DATE

5. .HOURS REACTOR WAS CRITICAL. . . . . . . . . . . . . 662.3 3428.6 14,153
6. REACTOR RESER VE SHUTDOWN HOURS ...... . 0 0 0
7. HOURS GENERA TOR ON LINE . . . . . . . . . . . . . . . 660.8 3157.8 132575.3
8. UNIT RESERVE SHUTDOWN HOURS . . . . . . . . . . . 0 0 0
9. GROSS THERMAL ENERGY GENERATED(MWH) . . . . . . . . . . . . . . . . . . . . . 1,566,410 7,448,665 29,504,075*

JO. GROSS ELECTRICAL ENERGY

-GENERATED (MWH) . . . . . . . . . . . . . . . . . . . . . 502,800 2,435, 770 __2_._163,533 l J. NET ELECTRICAL ENERGY GENERATED (MWH) ............................ . 477,277 1._,_3152124 922452477

12. REACTOR AVAILABILITY FACTOR (1) . . . . * . . . . 92 78.9 64.0
13. UNIT AVAILABILITY FACTOR (2) . . . . . . . . . . . . 91.8 _.1..2....J_ 61. (!
14. UNIT CAPACITY FACTOR (3) .... - ......... .

84.1 67.6 53.1

15. UNIT FORCED OUTAGE RATE (4) . . . . . . . . . . . . 8.2 5.7 25.8
16. SHUTDOWNS SCHEDULED TO BEGIN IN NEXT 6 MONTHS (STATE TYPE, DATE, AND DURATION Of EACH):

Scheduled refueling October 15 1975.

17. IF SHUT DOWN AT END Of REPORT PERIOD, ESTIMATED DATE Of S T A R T U P : - - - - - - - - - - - - -
18. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION) REPORT THE FOLLOWING:

DATE LAST DATE FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICAL POWER GENERATION COMMERCIAL OPERATION HOURS REACTOR WAS CRITICAL

(!) REACTOR AVAILABILITY FACTOR X)OO HOURS IN REPORTING PERIOD HOURS GENERA TOR ON LINE (2) UNIT AV AILABI L!TY FACTOR -------------XIOO HOURS IN REPORTING PERIOD NET ELECTRICAL.POWER GENERATED (3) UNIT CAPACITY FACTOR MAX. DEPENDABLE CAPACITY (MWe-NET) X HOURS IN REPORTING PERIOD FORCED OUTAGE HOURS (4) UNIT FORCED OUTAGE RATE  :....::.:.:..:.==---=.....:~:..::..:::....:c.:..=..-=-=-------~-~----~x100 HOURS GENERA TOR ON LINE+ FORCED OUTAGE HOURS

  • Corrected figure-Corrected error carried forwarded since February 1975

DOCKET NO. - 50-280 UNIT SHUTDOWNS UNIT NAME Surry Unit No. 1 DATE July 2, 1975 COMPLETED BY W* c* Earl REPORT MONTH

- -JUNE TYPE METHOD OF F-FORCED DURATION ~HUTTING DOWN NO. DATE S-SCHEDULED (HOURS) REASON (1) THE REACTOR (2) CORRECTIVE ACTIONS/COMMENTS 75-17 062475 F 59.2 A 1 Equipment failure was a packing failure of MOV-RH-1700 resulting in excessive primary coolant leakage.

(1) REASON (2) METHOD A -EQUIPMENT FAILURE (EXPLAIN) I-MANUAL

.... ~ " B MAINT. OR TEST 2-MANUAL C

  • REFUELING SCRAM D-REGllLATORY RESTRICTION 3--A UTOMATIC E--Ol'ERATOR TRAINING AND SCRAM LICENSE EXAMINATION F-ADMINISTRATJVE

,, G-*Ol'ERATIONAL ERROR ,.

(EXPLAIN)

H-OTHER (EXPLAIN)

SUMMARY

I I

  • i DOCKET NO. 5 0-281 UNIT Surry Unit No. 2 DATE July 2, 1975 COMPLETED BY W* C. Earl AVERAGE DAILY UNIT POWER LEVEL MONTH JUNE AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net) DAY (MWe-net) 1 0 17 23.2 2 0 18 288.4 3 0 19 544.3 4 0 2.0 701.3 5 0 21 725.5 6 0 22 729.6 7 0 23 751.2 8 0 24 751. 5 9 0 25 744.7 10 0 26 746.1 11 0 27 749.5 12 0 28 752.5 13 0 29 ' 754.1 14 0 30 747.7 15 0 31 16 0 DAILY UNIT POWER LEVEL FORM INSTRUCTIONS On this form, list the average daily unit power level in MWe-net for each day in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the* net electrical rating of the unit, there may be occasions when the daily average power level exceeds the 100% line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.

Q

  • UNIT Surry Unit No. 2 DATE July 2, 1975 COMPLETED BY W. c. Earl DOCKET NO.

50-281 OPERATING STATUS

l. REPORTING PERIOD: _ _ o_oo_1_ _,7,,...50-0_6_0_1_ _ _ _ _ _ THROUGH _2_4_0_0_ _7_5_0_6_3_0_ _ _ _ __

HOURS IN REPORTING PERIOD: _ _ 7_2_0_____. , - , - - - - - - - - - - - - - - - - - - - - -

2. CURRENTLY AUTHORIZED POWER LEVEL (MWth) 2441 MAX. DEPENDABLE CAPACITY (MWe-NET) 788
3. LOWEST POWER LEVEL TO WHICH SPECIFICALLY RESTRICTED (IF ANY) (MWe-NET): _ _ _ _ _ _ _ _ __

. 4. REASONS FOR RESTRICTION (IF ANY):

THIS CUMULATIVE REPORTING PERIOD YR TO DATE TO DATE

5. . HOURS REACTOR WAS CRITICAL. . . . . . . . . . . . . 385.4 3007.1 11,516.1
6. REACTOR RESERVE SHUTDOWN HOURS . . . . . . . 0 0 304.3
7. HOURS GENERATOR ON LINE . . . . . . . . . . . . . . . 317.6 2881. 2 11~265.4
8. UNIT RESERVE SHUTDOWN HOURS . . . . . . . . . . . 0 0 0
9. GROSS THERMAL ENERGY GENERA TED (MWH) . . . . . . . . . . . . . . . . . . . . . 720, 968 6,621,747 24,846,536 IO. GROSS ELECTRICAL ENERGY

-GENERA TED (MWH) . . . . . . . . . . . . . . *. . * . . . . 228,827 221732462 821952929 I l. NET ELECTRICAL ENERGY GENERATED (MWH) ............................ . 216,234 2,062,954 7,762,253

12. REACTOR AVAILABILITY FACTOR (1) . . . . * . . . . 53.5 69.2 60.7
13. UNIT AVAILABILITY FACTOR (2) . . . . . . . . . . . .

44.1 66.3 59.3 I4. UNIT CAPACITY FACTOR (3) .............. .

38.1 60.3 51. 9 IS. UNIT FORCED OUTAGE RATE (4) . . . . . . . . . . . . 3.0 4.3 23.9 I6. SHUTDOWNS SCHEDULED TO BEGIN IN NEXT 6 MONTHS (STATE TYPE, DATE, A.ND DURATION OF EACH):

I 7. IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF S T A R T U P : - - - - - - - - - - - - -

18. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPERATION) REPORT THE FOLLOWING:

DA TE LAST DA TE FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICAL POWER GENERATION COMMERCIAL OPERATION HOURS REACTOR WAS CRITICAL (l) REACTOR AVAILABILITY FACTOR X.100 HOURS IN REPORTING PERIOD HOURS GENERA TOR ON LINE (2) UNIT AVAILABILITY FACTOR -------------XIOO HOURS IN REPORTING PERIOD NET ELECTRICAL POWER GENERATED (3) UNIT CAPACITY FACTOR MAX. DEPENDABLE CAPACITY (MWe-NET) X HOURS IN REPORTING PERIOD FORCED OUTAGE HOURS (4) UNIT FORCED OUTAGE RATE ---------------------XlOO HOURS GENERATOR ON LINE+ FORCED OUTAGE HOURS

Page .!. of ~

DOCKETNO. _s_o_-2_8_1~~~

UNIT SHUTDOWNS UNIT NAME Surry Unit No. i; DATE July 2, 1975 COMPLETED BY W. c. Earl REPORT MONTH _ __::_JU.:...::N~E=-----

/

TYPE METHOD OF F*FORCED DURATION $HUTTING DOWN NO .. DATE S-SCHEDULED (HOURS) REASON (1) THE REACTOR (2) CORRECTIVE ACTIONS/COMMENTS 75-7 042675 s 392.3 c 1 Refueling I

75-8 061575 F 3.8 G 3 Reactor trip caused by high steam flow with low Tavg resulting from unequal pressure between steam generator and header and rapid header isolation valve opening.

75-9 061675 F 4.0 A 3 Malfunction of EHC caused turbine to roll at a high rate as the governor valves opened spiking 1st stage pressure above 15 per cent which tripped turbine.

Turbine trip, caused reactor trip.

(1) REASON (2) METHOD A EQUIPMENT FAILURE (EXPLAIN) I-MANUAL

..... _ ... B MAINT. OR TEST 2-MANUAL C- REFUELING SCRAM D-REGULATORY RESTRICTION 3-,AUTOMATIC E-OPERATOR TRAINING AND SCRAM LICENSE EXAMINATION F-ADMINISTRATIVE G--OPERATIONAL ERROR (EXPLAIN)

H-OTHER (EXPLAIN)

SUMMARY

Pagel of l DOCKET NO. ~50~--2_8_1~~~- *-

UNIT SHUTDOWNS UNIT NAME Surry Unit No. 2 '

  • DATE July 2, 1975 COMPLETED BY W. c. Earl REPORT MONTH JUNE

~~~~~~~~-

TYPE METHOD OF F-FORCED DURATION $HUTTING DOWN NO. DATE S-SCHEDULED (HOURS) REASON (1) THE REACTOR (2) CORRECTIVE ACTIONS/COMMENTS 75-10 061775 F 2.2 A 3 Turbine control valves opened rapidly spiking first stage pressure above 15 per cent tripping turbine. Reactor trip by turbine trip. EH control system mal-function.

'[

(1) REASON (2)_ METHOD A -EQUIPMENT FAILURE (EXPLAIN) 1-MANUAL

  • fl-* ~ B- MAINT. OR TEST 2-MANUAL C- REFUELING SCRAM D-REGULATORY RESTRlCTJON 3--AUTOMATIC E-OPERA TOR TRAINING AND SCRAM LICENSE EXAMINATION F-ADMINISTRATIVE G-OPERATIONALERROR (EXPLAIN)

H-OTHER (EXPLAIN)

SUMMARY