IR 05000387/2018011
| ML18241A044 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 08/27/2018 |
| From: | Jon Greives Reactor Projects Region 1 Branch 4 |
| To: | Rausch T Susquehanna |
| Greives J | |
| References | |
| IR 2018011 | |
| Download: ML18241A044 (14) | |
Text
August 27, 2018
SUBJECT:
SUSQUEHANNA STEAM ELECTRIC STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000387/2018011 AND 05000388/2018011
Dear Mr. Rausch:
On June 29, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed on-site inspection activities at your Susquehanna Steam Electric Station (SSES) and discussed the results of this inspection with you and other members of your staff. In-office review of additional information continued by the NRC, and a telephonic exit meeting was conducted on July 30, 2018, with you and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for its corrective action program. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety. The team identified one finding in the area of corrective action program effectiveness.
The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.
Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.
Finally, the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety conscious work environment.
Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
The finding involved a violation of NRC requirements and is being treated as a non-cited violation consistent with Section 2.3.2.a of the Enforcement Policy. If you contest the violation or significance, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspectors at SSES. In addition, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspectors at SSES.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects
Docket Numbers: 50-387 and 50-388 License Numbers: NPF-14 and NPF-22
Enclosure:
Inspection Report 05000387/2018011 and 05000388/2018011
Inspection Report
Docket Numbers:
50-387 and 50-388
License Numbers:
Report Numbers:
05000387/2018011 and 05000388/2018011
Enterprise Identifier: I-2018-011-0029
Licensee:
Susquehanna Nuclear, LLC (Susquehanna)
Facility:
Susquehanna Steam Electric Station, Units 1 and 2
Location:
Berwick, PA
Dates:
June 11 - July 30, 2018
Inspectors:
R. Barkley, PE, Senior Project Engineer, Team Leader
T. Daun, Resident Inspector
M. Patel, Operator Licensing Examiner
P. Boguszewski, Reactor Engineer
Approved By:
Jonathan E. Greives, Chief
Reactor Projects Branch 4
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Susquehannas performance by conducting the biennial problem identification and resolution inspection in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
Based on the samples selected for review, the inspection team concluded that Susquehanna was effective in identifying, evaluating, and resolving problems and that Susquehanna effectively used operating experience and self-assessments. The inspectors found no evidence of significant challenges to Susquehannas safety conscious work environment and concluded that the staff are willing to raise nuclear safety concerns through at least one of the several means available.
NRC-identified and self-revealing findings and violations are summarized in the table below.
List of Findings and Violations
Failure to conduct proper testing of 125 VDC molded case circuit breakers to confirm their design adequacy long-term Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000387;05000388/2018011-01 Closed P.5 - Operating Experience 71152B The inspectors identified a Green non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XI, Test Control. Specifically,
Susquehanna has not established a program to adequately exercise and test safety-related 125VDC molded case circuit breakers (MCCBs) since initial plant operation.
INSPECTION SCOPES
This inspection was conducted using the appropriate portions of the inspection procedures (IPs)in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Susquehannas performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
OTHER ACTIVITIES - BASELINE
71152 - Problem Identification and Resolution
Biennial Team Inspection (1 Sample)
The inspectors performed a biennial assessment of Susquehannas corrective action program, use of operating experience, self-assessments and audits, and safety conscious work environment. The assessment is documented below.
- (1) Corrective Action Program Effectiveness - The inspection team evaluated Susquehannas effectiveness in identification, prioritization and evaluation, and correcting problems; and verified the station complied with NRC regulations and Susquehannas standards for corrective action programs.
- (2) Operating Experience - The team evaluated Susquehannas effectiveness in its use of industry and NRC operating experience information and verified the station complied with Susquehannas standards for the use of operating experience.
- (3) Self-Assessments and Audits - The team evaluated the effectiveness of Susquehannas audits and self-assessments and verified the station complied with Susquehannas standards for the use of operating experience.
- (4) Safety Conscious Work Environment - The team reviewed Susquehannas programs to establish and maintain a safety conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs.
INSPECTION RESULTS
Evaluation of the Susquehanna PI&R Program 71152B The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined Susquehanna staffs performance in each of these areas adequately supported nuclear safety. The team identified one finding in the area of the Corrective Action Program Effectiveness.
The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.
Based on the samples reviewed, the team determined that Susquehannas performance in each of these areas adequately supported nuclear safety.
Finally, the team reviewed the stations programs to establish and maintain a safety conscious work environment, and interviewed station personnel in focus groups to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to Susquehannas safety conscious work environment. Site employees appeared willing to raise nuclear safety concerns through at least one of the several means available.
Failure to conduct proper testing of 125 VDC molded case circuit breakers to confirm their design adequacy long-term Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity
Green NCV 05000387;05000388/2018011-01 Closed
P.5 - Operating Experience 71152B The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control. Specifically, Susquehanna had not established a program to adequately exercise and test safety-related 125VDC MCCB since initial plant operation.
Description:
During the 2013 NRC Component Design Bases Inspection (CDBI), inspectors reviewed Susquehannas response to NRC Information Notice 93-64, Periodic Testing and Preventive Maintenance of Molded Case Circuit Breakers. The inspectors identified a violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, because Susquehanna did not provide design control measures to verify or check the adequacy of the design for 125VDC MCCBs to ensure that the safety-related function credited to provide external circuit protection of primary containment electrical penetrations under the overload or fault conditions was maintained (ADAMS Accession No. ML13275A074). Specifically, the CDBI team concluded that the time-current characteristic curves for the fuse, breaker, and penetration conductors depicted in UFSAR Figure 3.13-5 indicated that proper coordination between the breaker and power cable is required to be maintained in order to protect the containment penetration from damage during fault conditions. The CDBI team also concluded that the overcurrent and instantaneous trip functions of these breakers have a safety-related function for these MCCBs because they are credited to operate in order to maintain the mechanical integrity of primary containment penetration assemblies under overload or fault conditions.
In 2016 while preparing for the next CDBI, Susquehanna identified that they had not taken corrective actions associated with the previously identified NRC violation and a licensee-identified violation was documented in the 2016 CDBI inspection report (ADAMS Accession No. ML16328A097).
Inspectors reviewed the corrective actions taken for the 2013 NRC-identified and 2016 licensee identified violations. Inspectors questioned what action was taken to address the 2013 NCV. While the inspectors noted that Susquehanna performed breaker panel thermography dating back to 1996, they did not plan to complete the corrective actions they had identified, including internal inspection, cleaning, and manual cycling of these 125VDC MCCBs, until Unit 1 and 2 outages ending in 2021 and 2022. Their corrective actions did not include electrical testing.
The inspectors noted that even though Susquehanna had plans to conduct manual cycling of the MCCBs, this type of testing does not adequately provide test control measures during plant operation to assure that 125VDC MCCBs credited to provide external circuit protection of primary containment electrical penetrations under overload or fault conditions. Manually cycling the breakers provides lubrication through the manual tripping mechanism and a means of detecting the deterioration of the manual operating mechanism toward an unacceptable condition, but it does not provide any means of testing the automatic tripping mechanisms (i.e., thermal and electromagnetic). Additionally, manually cycling the breaker does not provide a means of detecting the deterioration of the overcurrent trip features toward an unacceptable condition, which is the safety-related function of the MCCB.
Corrective Actions: Susquehanna entered the issue into the corrective action program as CR-2018-09952 to evaluate the corrective actions taken to address the 2013 NRC-identified and 2016 licensee identified violations. The team noted that Susquehanna subsequently rescheduled the MCCB preventive maintenance (PM) schedule such that the cycling of these 125VDC MCCBs would occur one outage (approximately 2 years) earlier than previously planned. To address the lack of electrical testing of these 125VDC MCCBs, Susquehanna initiated CR-2018-11415. The MCCBs provide an independent backup fault protection for each load to preclude a single failure from impairing the integrity of a containment electrical penetration. Inspectors determined that the continued noncompliance while adequate corrective actions are developed did not represent a safety concern because the primary method of maintaining integrity of the containment penetrations are the fuses in the control panel and are independent of the MCCBs.
Corrective Action References: CR-1732454, CR-2016-04833, CR-2018-09952, DI-2018-03458
Performance Assessment:
Performance Deficiency: Susquehannas failure to establish a test program to assure that all testing required to demonstrate that safety-related 125VDC MCCBs will perform satisfactorily in service was a performance deficiency and was within Susquehannas ability to foresee and correct.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the Design Control and Configuration Control attributes of the Barrier Integrity cornerstone objective to provide reasonable assurance that physical design barriers (containment) protect the public from radionuclide release caused by accidents or events.
Significance: The inspectors assessed the significance of the finding using IMC 0609, Appendix A, Exhibit 3, Barrier Integrity Screening Questions, Section B, Reactor Containment, and determined that this performance deficiency did not represent an actual open pathway in the physical integrity of reactor containment and did not involve an actual reduction in the function of hydrogen igniters in the reactor containment. Therefore, the finding was determined to be of very low safety significance (Green).
Cross-Cutting Aspect: The finding has a cross-cutting aspect in the area of Operating Experience [P.5] since the organization did not systematically and effectively collect, evaluate, and implement relevant internal and external operating experience in a timely manner.
Specifically, while operating experience was available in the form of an information notice, industry guidance, and regulatory enforcement actions on low voltage MCCB testing, Susquehanna had not systematically evaluated this information into their corrective actions associated with the previously identified violations such that it included electrical testing as well as the inspection and cycling of the breakers.
Enforcement:
Violation: 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. The test program shall include, as appropriate, proof tests prior to installation, preoperational tests, and operational tests during nuclear power plant or fuel reprocessing plant operation, of structures, systems, and components.
Contrary to the above, prior to July 2018, Susquehanna had not established a test program to assure that all testing required to demonstrate that safety-related 125VDC MCCBs that provide the necessary external circuit protection of primary containment electrical penetration under overload or fault conditions.
Disposition: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.
Observation and Minor Performance Deficiency 71152B Corrective Action Program Effectiveness: The team concluded that Susquehannas corrective action program was effective. However, the following observation was noted during this inspection:
Problem Identification
During a walkdown of the Engineered Safeguards Service Water (ESSW) building, the inspectors questioned Susquehanna regarding the impact on the far field seismic monitor from groundwater that leaked into the basement of each division. While the monitor was found to be above the level of the water, the water level in the basements of both ESSW building divisions was greater than the actuation set point (7 inches and 13 inches versus 3.25 inches) of the flood detection instruments in each basement. Neither division flood instrument had actuated and alarmed in the control room. Upon identification on June 12, 2018, Susquehanna initiated additional compensatory measures per procedure EP-115, Equipment Important to Emergency Response (EITER), Revision 12, to detect flooding in this building while the instruments were examined and the water was pumped out. The equipment failures were entered into the corrective action program as CR 2018-09364 and 2018-09365. Susquehanna found that the one instrument had corroded sufficiently to restrict the internal float from moving upward and actuating the alarm; once the corrosion was removed, the instrument tested properly. The float in the other instrument was found to move freely, but a micro switch in the instrument was not operating. That instrument was returned to service once the micro switch was replaced.
The inspectors noted that this area had historically been inspected once per month and pumped out if measurable water was found, leaving the flood instruments in a relatively dry condition. However, the PM activity was last performed in March 2017 and was assigned a low priority. The inspectors also noted that operators check the ESSW pump rooms once per 12-hour shift, but do not examine the basement areas during routine rounds as it is unlit and 30 feet down below 2 levels of deck grating. Given the slow rate of groundwater in-leakage, inspectors determined Susquehanna had a reasonable opportunity to have identified the non-functional emergency equipment. The inspectors noted that while these instruments are used to warn of possible flooding in each ESSW division, alternative measures are available to detect flooding in these rooms above the ESSW basements in adequate time to make an accurate emergency action level declaration. As such, inspectors determined the failure to identify the degraded emergency equipment was of minor safety significance because it did not adversely affect the emergency preparedness cornerstone objective.
Corrective action for this event included reclassifying the PM activity for checking and pumping out the basements to ensure they are performed on a monthly basis (PMCR # 2018-09585) as well as performed an extent of condition review of other rooms with flood level instruments.
Observation 71152B Operating Experience: The team concluded that Susquehannas use of operating experience was effective. However, one Green NCV was identified during this inspection and was attributed to ineffective use of relevant internal and external operating experience.
Observation 71152B Self-Assessments and Audits: The team concluded that Susquehannas self-assessments were effective. However, the following observation was noted during this inspection:
The NRC inspectors noted numerous condition reports starting in February 2018 related to malfunctions of a specific security feature requiring compensatory actions. Though appropriate corrective actions were taken for individual alarms, inspectors identified that Susquehanna was not effective in identifying this potential adverse trend. Susquehanna subsequently initiated a trend condition report (CR-2018-09335) and identified all malfunction alarms received between January and mid-June of 2018.
Observation 71152B Safety Conscious Work Environment: The team found no evidence of challenges to the Susquehanna organizations safety conscious work environment. Site employees appeared willing to raise nuclear safety concerns through at least one of the several means available.
The comments made by the Susquehanna staff were consistent with Susquehanna internal employee survey results, particularly with regard to the use of the corrective action system and concerns with knowledge management. Several senior staff noted improvements in the corrective action process in recent years; the only concerns expressed regarding the corrective action system were with the resolution of long-term, lower level equipment issues.
EXIT MEETINGS AND DEBRIEFS
Inspectors verified no proprietary information was retained or documented in this report.
On June 29, 2018, the inspectors presented the biennial problem identification and resolution initial inspection results to Mr. Timothy Rausch and other members of the Susquehanna staff. Following additional in-office review, the final results were presented in a telephonic exit meeting on July 30, 2018, with Mr. Timothy Rausch and other members of the Susquehanna staff.
DOCUMENTS REVIEWED
Action Requests
1738163
2014-29799
2015-06525
2015-10389
2016-02190
2017-05278
2017-05294
2017-12969
Condition Reports (*initiated in response to inspection
296516
1712812
1732454
2014-05827
2014-28018
2014-36140
2015-00612
2015-19111
2015-19390
2015-27535
2015-33668
2016-02369
2016-04833
2016-06960
2016-08377
2016-09940
2016-12047
2016-12619
2016-13058
2016-13220
2016-14128
2016-14789
2016-15603
2016-15710
2016-16692
2016-16794
2016-18466
2016-19187
2016-19445
2016-20307
2016-20156
2016-20472
2016-20859
2016-20623
2016-20859
2016-21028
2016-22634
2016-22888
2016-23373
2016-23477
2016-23627
2016-23631
2016-23874
2016-23934
2016-24458
2016-24888
2016-25099
2016-25162
2016-25622
2016-26213
2016-27867
2017-00476
2017-03943
2017-04957
2017-05265
2017-05330
2017-05775
2017-06068
2017-06476
2017-06836
2017-09515
2017-11504
2017-11559
2017-11583
2017-11645
2017-11912
2017-11996
2017-12182
2017-12685
2017-13746
2017-13956
2017-15420
2017-16089
2017-16380
2017-16577
2017-16676
2017-19491
2017-19713
2017-20923
2017-21300
2018-01219
2018-01261
2018-02040
2018-02090
2018-03194
2018-04388
2018-04535
2018-05044
2018-06662
2018-08976
2018-09294
2018-09290*
2018-09291*
2018-09292*
2018-09335*
2018-09364*
2018-09365*
2018-09598
2018-09673*
2018-09808*
2018-09952*
2018-09953*
2018-10596*
2018-10597*
Self-Assessment and Audits
DI-2016-16175
DI-2016-19792
DI-2016-22542
DI-2016-22543
DI-2017-00312
DI-2017-00313
DI-2017-12776
DI-2017-12777
DI-2017-12776
DI-2017-18729
DI-2017-18730
DI-2018-09542
NCV 2016002-01 - Failure to Promptly Identify a Condition Adverse to Quality Associated with
Primary Containment Isolation Valves
NCV 2016002-02 - Failure to Promptly Correct a CAQ with the A EDG MOC Switch
NCV 2016002-04 - Failure to Critique an Incorrect PAR Notification
NCV 2016004-03 - Refuel Floor Rad Monitor Inoperable due to Improper Calibration
NCV 2016004-04 - Auxiliary Bus Load Shed When a Daisy Chained Neutral was Interrupted
During Maintenance
NCV 2016008-01 - Failure to Write a Condition Report for Degraded Conditions Which
Challenged the Operability of Safety-Related Equipment
NCV 2016008-02 - Failure to Implement and Maintain Quality Procedure Results in MCR
Chiller being Inoperable
NCV 2017003-01 - RBCCW PCIV Design Control Issue
NOS Audit Report AR-2016-22717, Emergency Preparedness Audit Report
Nuclear Safety Culture Assessment - 2017
Nuclear Safety Culture Monitoring Reports for the 2nd, 3rd and 4th quarters of 2017 and the 1st
quarter of 2018
FASA Report - Readiness for the 2016 NRC/FEMA Evaluated Exercise
Team Susquehanna Plan for Excellence, Revision 8
Maintenance Orders/Work Orders
1900523
1900539
1903970
1914356
1914357
2001009
2007122
2019613
28884
28885
28886
2031798
2037890
2070562
2070563
2112937
2114386
2114560
2114562
2114670
2114675
2114724
2165429
2165490
2166230
2184374
Procedures
EP-115, Revision 12 - Equipment Important to Emergency Response (EITER)
LS-125-1001, Revision 4, Root Cause Analysis Manual
LS-125-1009, Revision 2, Station Trending Manual
NDAP-00-0109, Revision 19, Employee Concerns Program
NDAP-00-0784, Revision 6, SSES Safety Culture Monitoring
NDAP-00-0909, Revision 15, Overview of Security Requirements
NDAP-QA-0703, Revision 31, Operability Determinations and Functionality Assessments
SI-099-210 - Semi-Annual Functional Test - Strong Motion Seismic Monitor
Engineering Changes / Evaluations
ERPM 1880933, AOV Diagnostic Test / Repack XV147F010
EPRM 1880952, AOV Diagnostic Test / Repack XV147F180
GDG-09, Valve Design Considerations for Design Changes Which Affect Components or
System Parameters, Revision 10
NDAP-QA-1170, Air Operated Valve Program, Revision 4
NDAP-QA-1220, Engineering Change Process, Revision 12
NSE-DTG-008, Station Engineering Desktop Guide #8, Valve Packing, Revision 0
SO-155-002, Quarterly SDV Vent and Drain Valve Operability Check, Revision 26
Calculations
EC-002-0518, Main Steam Isolation Valve Solenoid Fuse to Breaker Coordination 125 VDC,
Revision 0
EC-002-0533, 125 VDC Class 1E Distribution Panel 1D624 2D624, Revision 0
EC-002-0657, Coordination of 125 VDC Class 1E Distribution Panel, Revision 0
Drawings
E-26, Sheet 1, Unit 1 Schematic Meter and Relay Diagram 125 VDC System
E-26, Sheet 2, Unit 1 Schematic Meter & Relay Diagram 125 VDC Distribution Panels - ESS
1D614, 1D624, 1D634 & 1D644
M-147, P&ID for the Scram Discharge Volume, Revision 38
Operating Experience
CR-2017-06541, Security OE Review Performed under AR-2016-00376 was Inadequate
CR-2017-11645, Part 21 on Cutler Hammer/Eaton A200 Series Starters, 06/09/2017
CR-2017-11912, Reactor Recirculation Pump Trip at FitzPatrick Could Apply to SSES,
06/16/2017
CR-2017-11951, 2-inch abandoned conduit was drilled on hardened vent at Hope Creek
DI-2018-03696
ICES Report 438577
Miscellaneous
DBD001, Design Basis Document for Class 1E DC Electrical, Revision 6
DBD003, Design Basis Document for Containment Isolation, Revision 4
DBD012, Design Basis Document for Primary Containment, Revision 4
IOM117, ET EH-Frame Circuit Breakers 2 Pole,15-100 Amperes, Revision 43
MRC and Screening Reports for day the team was onsite
PM Change Request Form 2018-09585, dated June 21, 2018
PM Change Request Form ACT-03-CR-2016-04833