ML18153C743

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Insp Repts 50-280/91-24 & 50-281/91-24 on 910802-26.No Violations Noted.Major Areas Inspected:Failure of Emergency Diesel Generator 3 to Reach Required Speed to Automatically Load on Emergency Bus During 910802 Safety Injection
ML18153C743
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/30/1991
From: Branch M, Fredrickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153C742 List:
References
50-280-91-24, 50-281-91-24, NUDOCS 9109240214
Download: ML18153C743 (8)


See also: IR 05000280/1991024

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/91-24 and 50-281/91-24

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

. Facility Name:

Surry 1 and 2 *

License Nos.:

DPR-32 and DPR-37

Inspection Conducted: August 2 through 26, 1991

Inspectors:

Approved by:

Scope:

/J1 I{) &_~*6'( Mt/f;dk~k~

M. W. Branch, Senlior Resident Irfspector

-},( aJ !fl~ 1; !itt/~/n~

J. W. York, Residfnt Inspector'

.

P. E; Fredrickson, Secfl-On Chief

Division of Reactor Projects

SUMMARY

olr'-l.

~

This specfal inspection was conducted on site to evaluate the failure

of the No. 3 emergency diesel generator to * reach required speed to

automatically load (if needed) on its emergency bus during an August 2, 1991,

Unit 2 safety injection with a reactor trip.

The inspection was also conducted to evaluate the inoperability of the A

charging/high head safety injection pump under certain pump configurations.

Results:

One apparent violation was identified for failure to comply with Technical

Specification 3.16.B.1 while the No. 3 emergency diesel generator was

inoperable from May 9, 1991 to August 2, 1991 (paragraph 2) .

. A second apparent violation was identified for failure to comply with Technical

Specification 3.3.B.2, while the A charging/high head safety injection pump was

inoperable for numerous durations between 1979 and the present (paragraph 3).

9109240214 910830

PDR

ADOCK 05000280

G

PDR

1.

Persons Contacteq

Licensee Employees

REPORT DETAILS

    • R. Allen, Acting Superintendent of Opetations
    • W. Benthall, Supetvisor, Licensing
  • R. *Bilyeu, Licensing Engineer
    • R. Blount, Supervisor, Procedures

D. Christian, Assistant Station Manager

J. Downs, Superintenderit of Outage and Planning

D. Erickson, Superintendent of Health Physics

  • R. Gwaltney, Superintendent of Maintenance
    • M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

    • A. Price, Assistant Station Manager
  • R. Saunders, Assistant Vice President, Nuclear Operations
  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering

NRC Personnel

  1. M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector*
  • J. York, Resident Inspector *
  • Attended exit interview on August 19, 1991
  1. Attended exit interview on August 26, 1991

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

-

2.

Review of EOG Operallil ity

During a Unit 2 safety injection with a reactor trip on August 2, 1991,

both the No. 2 and the No. 3 EDGs received a start signal and started as

required. However, the No. 3 EDG failed to increase to the required speed*

(i.e. the EDG's output breaker would not have closed if the EDG was needed

to 1 oad on to the bus). . The EOG was running at 835 rpm.

A speed of 870

rpm is required to satisfy the output breaker closure permissive

interlock.

The detai 1 s of the August 2, 1991, event are discussed in

Inspection Report 50-280,281/91-21.

The inspector identified to the licensee that the No. 3 EOG was not

running at the required speed.

The licensee subsequently declared it

inoperable and entered the TS 3.16.B.1 action statement.

This TS is

2

applicable to both Unit 1 and Unit 2 because the No. 3 EDG is corranon to

both units, and is the standby power supply for each unit's J emergency

bus.

The licensee investigated why the EDG fai"led to reach its required

speed .. The initial detennination indicated that the govern.or's speed

adjustment was not at the required setting.

This was determined by an

inspection that showed the gear match marks inside the governor were not

correctly aligned.

The licensee readjusted the governor speed setting and

perfonned two consecutive fast starts of the No. 3 EDG to verify that the

engine would reach the required speed. After testing proved that the No.

3 EDG was operable, the licensee exited the TS action sta~ement.

After

the No. 3 EDG test, the licensee satisfactorily verified the fast start

capability of the other two EDGs.

Fast start testing during refueling outages is required by TS 4.6.A.l.b,

However, monthly surveillance requirements for the EDGs as specified in

TS 4.6.A.1.a only requires start of the EDGs and to manually increase the

speed to 900 rpm.

This mqnthly test_ does not verify all of the governor

automatic functions as does the refueling surveillance test.

On August 7, 1991, the inspector witnessed the fast start of the.No. 1

EOG.

Procedure 1-0P-EG-6.1, Number 1 EDG, dated May 29, 1991, was used to

accomplish this testing.

Procedure Change (PAR 91-912) was issued to

modify the procedure to allow this special test. The procedure included a

fast start of the EOG and a speed verific~tion. During EDG operation for

this fast start, the speed was adjusted to 900 rpm and the governor speed

gear and control knob were marked for future reference.

The EDG was

stopped and two additional fast starts were accomplished to verify

repeatability.

On the first fast start after reference marks for speed

control were made, the engine automatically increased speed to 900 rpm as

verified by local rpm indicators and test equipment monitoring output

frequency~

After the mechanical speed adjustment was reset to the match

mark the second fast start was initiated.

The No. 1 EDG again automati-

cally increased lo the required 900 rpm speed.

Fast start testing of the No. 2 EDG was conducted after completion of

tfle No. 1 EDG test.

During the first fast start the speed increased

to approximately 928 rpm.

This as-found condition, was outside the

upper speed limit of 918 rpm and corresponded to a generator frequency

of 61.89 HZ.

The governor speed was adjusted to 900 rpm and the EDG was

~ubsequently fast started two additional times.

Each time the speed was

within the a 11 owab le 1 imi.ts.

The as-found speed of 928 rpm was eva 1 uated

by engineering and determined to be acceptable.

After each of the above tests, the licensee had to manually adjust th~

. governor upper speed setpoint.

The governor is equipped with two mkro

switches that control power to the governor servo motor.

T_he servo motor

is designed to automatically drive the upper speed adjustment to the

required setting that corresponds to 900 rpm.

It is considered that the

out-of-band speed for the No. 2 EOG indicates that speed is not repeatable

without the manual adjustment between EDG operation.

This type of *

governor (Woodward UG-8) is* generically used to control speed in many

nuclear applications.

3

The licensee initiated a CNS review of the No. 3 EDG failure.

The

inspectors met with the group and were provided with an initial root

cause for the EOG failure to reach the required speed.

The CNS group

determined that the governor had been_ replaced in the* May 1991 timeframe *

and that adjustments had been made without a subsequent fast start test.

The inspectors questioned the licensee as to the reportability of the EOG

failure.

The licensee indicated that reportability would be evaluated

after completion of review of the above issues.

The inspectors performed an independent review of the past maintenance of

the No *. 3 EDG. governor and examined the maintenance history of the EDG

to determine if recent maintenance contributed to the failure.

On May 7

through 9, 1991, the governor was installed in accordance with

WO 3800111115.

The inspectors reviewed the work package associated with

this maintenance.

The licensee did not utilize a formal procedure to

accomplish this maintenance.

The maintenance was accomplished utilizing

job steps outlined on the WO and SNSOC approved instructions for adjust-

ment of the governor.

The governor vendor was a 1 so at the job site

to assist in the* adjustment of the new governor *. Review of the work

package indicated that the new governor was installed and that the speed

control was adjusted.

The EOG was started and governor adjustments were

made; however, the EDG would not properly 1 oad.

It was secured and

additional adjustments were made to the fuel racks. It was restarted and

loaded properly.

Another problem was encountered during installation of

the new governor when, during steady state operation of the EOG, engine

speed slowly increased.

With the EOG running, the vendor representative

for the .Woodward governor made adjustment to stabilize the speed.

The EOG*

was operated for approximately 40 more minutes with ~ngine speed remaining

stable. It was then secured and declared operable.

The licensee concluded.and the inspectors agreed that No. 3 EOG failed to

achieve the correct speed on August 2, because the vendor ma~e adjustments

on May 9, 1991, which affected the speed of the EOG during an automatic

start.

When the vendor made the adjustment, the licensee failed to

realize that engine speed would be affected during an automatic EDG*start.

The inspectors identified several other deficiencies during review of the

work package for replacement of the governor.

These deficiencies were not

directly responsible for the August 2, 1991~ failure of No. 3 EOG, but

they may have contributed to the failure.

The first deficiency was that

  • the PMT follower sheet for this maintenance did not specify all the

required post-maintenance testing.

The SNSoc*approved instructions for

governor adjustment required that the EDG be fast started to verify

correct speed following governor replacement; however, the PMT follower

only required that the EOG be slow started. This issue was discussed with

the PMT coordinator who stated that this weakness had previously been

identified in the PMT program.

This weakness was the failure to specify

all applicable testing on the PMT follower when other instructions

associated with the maintenance required additional tests.

The licensee

was in the process of cor~ecting this weakness.

The s~cond deficiency was

that the EOG was not tested in accordance with the SNSOC approved

instructions.

4

The SNSOC approved instructions required that the EDG be fast started

following governor adjustment.

These instructions were signed off as

performing a. fast sp~ed start.

The inspectors* reviewed the operator

logs and PTs utilized to accomplish the EDG testing and concluded that

No. 3 EDG was *not fast speed started as required by the SNSOC approved

instructions.

The failure to fast start the EDG was attributed to poor

corrmunications between maintenance and operations. The third deficiency

was that a formal procedure was not utilized to accomplish this

maintenance.

The WO co.ntained 16 one line steps to accomplish this

maintenance and included a two page SNSOC approved document providing

instructions for governor adjustment and testing.

A lack of a formal

procedure contributed to poor communications* between operations, ma

intenance, engineering, and the vendor.

Confusion as to the requirement

for fast starting the EDG after the vendor made the governor adjustments

also resulted from the lack of a procedure.

TSs state that an EOG is required to start within 10 secon*ds and assume

load in less than 30 seconds after receiving a start signal.

The

inspectors concluded that since May 9, 1991, the No. 3 EDG was unable to

automatically operate in accordance with. TS time constraints and was

therefore inoperable.

It should be noted, however,* that operators could

have taken manual c~ntrol of the EOG, increased its speed, and aligned the

EDG to the emergency bus.

Because No. 3 EOG is a swing EOG, inoperability

of the EOG affects both Units 1 and 2 abi 1 ity to respond to an event

requiring the EOGs to operate and load automatically onto the emergency

bus.

The inspectors reviewed the work histories of the Nos. l.and 2 EOGs

from M~y 9, i991 through August 2, 1991.

The results of this review

indicated that on July 15, 1991, No. 2 EOG was inoperable from 9:28 a.m.

to 11:06 p.m. for installation of a balance weight on the drive shaft.

Unit 2 was at power on July 15, 1991, and if an event would have occurred

that required Nos. 2 and 3 EOGs to automatically start and load, both of

the EDGs would not have been available.

However, operators could have

operated both EDGs manually.

The -i nabi 1 i ty of Nos. 2 and 3 EDGs to

automatically start for 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> and 38 minutes on July 15, 1991, was

beyond the scope of TSs.

TS 3.16.A requires that two EDGs, the dedicated EOG for each unit, and the

shared backup No. 3 EOG, be operable prior to exceeding 450 psig and.350

degrees F respectively.

TS 3.16.B.1 allows either the dedicated or shared

backup EOG to be inoperable provided the operability of the other EOG is

demonstrated daily and the inoperable EOG returned to an operable status

within seven days.

If this is not met, the unit is to be brought to a

cold shutdown condition.

The inspectors reviewed the operating history

for Units 1 and 2 over the period that the No. 3 EOG was inoperable (May

9, 1991,

to August 2, 1991).

The results of this review were that Unit 1

operated the entire period without complying with TS 3.16.B.1 action

statement.

Unit 2 operated June 1 and 2, June 5 through 11, and July 2

through August 2, 1991, without complying with TS 3.16.B.1 action

statement.

The failure to comply with this TS requirement was identified

as Apparent Violation 50-280, 281/91-24-01, Failure to Comply with TS 3.16.B.1 Requirements *With No! 3 EOG Inoperable.

5

Within the areas inspected, one apparent violation was identified.

3.

Rev*;ew Of Charging P.ump Operability

On August 19, 1991, the inspectors discussed the charging/HHS! pumps

interlocks with several system engineers.

During this discussion, the

inspectors questioned how the pumps sequenced on and off their respective

emergency bus during an undervoltage condition.

As a result of this

discussion, an engineering review of these interlocks was performed.

On

August 21, 1991, the inspectors were informed by system engineering that.

under certain charging/HHS! pump configurations, the A pump would lockout

on an undervoltage condition on its emergency bus.

Based on this

discussion, the inspectors concluded-that if an undervoltage occurred on

the H bus coincident with an ECCS actuation signal, the A pump would not

have started automatically.

There are three charging/HHS! pumps in each unit.

The A pump is powered

from the H emergency bus, the B pump is powered from the J emergency bus,

and the C pump is a swing pump that can be powered from the Hor J bus *. *

  • TSs require that two charging/HHS! pumps be available in a unit when

critical, one pump powered from the H bus and the other pump powered from

the J bus.

When the A and B pumps' control switches are in the run or

automatic start positions, the C pump control switch is in the

pull-to-lock position, and the C pump J bus supply breaker is racked-out,

the configuration exists where the A pump would lockout on an H bus *

undervoltage condition.

This charging/HHS! pump configuration was

frequently*utilized in both of the units.

On initiation of an ECCS signal

in this configuration, coincident with a H bus undervoltage condition, the*

A pump would have locked out and not started automatically.

Operator

action would have been required to manually start the A pump.

The above charging/HHS! pump configuration was frequently utilized since

the implementation of Design Change No. 78~5378, dated September 19, 1979.

Prior to the implementation of this design change, all three charging/HHS!

pumps were normally aligned to automatically start upon receipt of an ECCS

initiation signal.

Upon receipt of an ECCS signal without an undervoltage -

on the H bus, all three charging/HHS! pumps would automatically start. If

an undervoltage condition developed on the H bus, the A pump would lockout

and the Band C pumps would continue to operate.

One of the results of

Design Change No. 78-5378, was to change pump configuration such that only

two charging/HHS! pumps, one off each emergency bus, were aligned to

automatically started upon receipt of an ECCS initiation signal. The pump-

. configuration change was required to ensure that the LHSI pumps could

maintain adequate NPSH to the HHSI pumps during the recirculation transfer

mode of operation and to conserve RWST inventory.

Upon discovery of the inadequate charging/HHS! pump configuration on

August 21; 1991, engineering initiated a deviation report. At the time of

the discovery, Unit 1 charging/HHS! pumps were aligned such that the A and

B pump control switches were in the automatic start and run positions and

..

.

6

the C pump control swi~ch was in pull-to-lock.

The A pump was decla~ed

inoperable and a six hour requirement to be in hot shutdown was enteredin

accordance with TS 3.0.1..

The pumps were rea1igned such that the A,

control switch was in the pull-to-lock position, B pump control switch in

run, and~ pump control switch in the automatic start position and the six

hour. clock was exited.

The Unit 2 charging/HHS! pumps control switches

were positioned such that the A pump was in pull-to-lock, B pump in

automatic start, and C pump in run and therefore did not require

realignment.* In addition, on August 22, 1991, at approximately 4:18 p.m.

the licensee made a one-hour non-emergency report in accordance with 10

CFR 50.72. Since automatic HHSI initiation is assumed in the design basis

accident in coincidence with a single active failure, the units would be

outside the design bases in certain pu~p configurations if credit for

manual operator could not be taken.

The deviation report stated that during a design basis accident which

includes an undervoltage on the H bus, the inadequate charging/HH~I pump

configuration concurrent with a single failure of the B pump would result

in the unit not having a HHSl pump available for automatic start.

As

previu~sly discussed in paragraph 2 of this report~ the No. 3 EOG was

inoperable from May 7, 1991 to August 2, 1991.

Review of operator logs

. indic*ated that the Unit 1 charging/HHS! pumps were in an inadequate

configuration from April 26, through May 26, and June 20 through August 2,

1991.

With the No. 3 EOG inoperable and the charging/HHS! pumps

inadequately configured, none of the Unit 1 HHSI pumps were available for

automatic start if a design basis accident would have occurred.

TS 3.3.B.2 states that two of the three charging pumps in a unit may be

out of service, provided inrnediate attention is directed to making repairs

and one of the inoperable pumps be restored to an operable status within

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. If one of the inoperable pumps is not restored within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,

then the reactor shall be placed in the shutdown condition. If one of the

inoperable pumps is not restored within an additional 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, the

reactor shall be placed in a cold shutdown condition.

The failure to

configure Units 1 and 2 charging/HHS! pumps since approximately 1979 such

that ~he A pump would automatically operate during a design basis accident

was identified as Apparent Violation 50-280,281/91-24-02, Failure to

Comply With TS 3.3~8.2 Due To Inadequate Charging/HHS! Pump Configuration.

The inspectors were informed by the licensee that operators were t_rained

on the A charging/HHS! pump lockout and were aware that the pump would

have to be manually started if a lockout did occur.

Also, a similar

finding was identified *at the North Anna Power Station in 1983.

LER

83-058/03L-O, dated October 5, 1983, reported a condition where the A

charging/HHS! pump would have locked out and failed to start automaticilly

in response to an ECCS initiation signal during an ~ndervoltage on:the H

bus.

The corrective actions implemented at the North Anna Power Station

in response to this LER were not implemented at Surry.

Within the areas in~pected, one apparent violation was Jdentified.

7

4.

Exit Interview

The inspection scope and results were summarize-d on August 19, -1991 and

August 26, 1991

with those individuals identified in paragraph 1.

The

following summary of inspection activity was discussed by the inspectors

during this exit.

Item Number

Apparent VIO 50-280,281/91-24-0l

Apparent VIO 50-280,281/91-24-02

Description and Reference

Failure to comply with the

requirements of TS 3.16.B.1

with the No. 3 EOG inoperable.

Failure to comply with the

requirements of TS 3.3;8.2 _

with the A chargin~/HHSI pum~

inoperable

  • *

The licensee acknowledged the inspection conclusions with no dissenting

  • comments.

The licensee did not identify as proprietary any of the*

materials provided to *or reviewed by the inspectors during this

inspection.

5.

Index of Acronyms and Initialisms

CNS

ECCS

EOG

F

GPM

HHSI

LER

-NPSH

NRC

PMT

PT

RWST

SNSOC

TS

WO

CORPORATE NUCLEAR SAFETY

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

FAHRENHEIT

GALLONS PER MINUTE.

HIGH HEAT SAFETY INJECTION

LICENSEE EVENT REPORT

NET POSITIVE SUCTION HEAD

NUCLEAR REGULATORY COMMISSION

POST MAINTENANCE TESTING

PERIODIC TESTS

-REFUELING WATER STORAGE TANK

STATION NUCLEAR AND SAFETY OPERATING COMMITTEE

TECHNICAL SPECIFICATIONS

WORK ORDER