ML18153A485

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/96-12 & 50-281/96-12 on 961110-1214. Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support
ML18153A485
Person / Time
Site: Surry  
Issue date: 01/13/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153A483 List:
References
50-280-96-12, 50-281-96-12, NUDOCS 9702100455
Download: ML18153A485 (15)


See also: IR 05000280/1996012

Text

Docket Nos:

License Nos:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9702100455 970113

PDR

ADOCK 05000280

G

PDR

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

50-280, 50-281

DPR-32, DPR-37

50-280/96-12, 50-281/96-12

Virginia Electric and Power Company (VEPCO)

Surry Power Station, Units 1 & 2

5850 Hog Island Road

Surry, VA 23883

November 10 - December 14, 1996

R. Musser, Senior Resident Inspector

P. Byron, Resident Inspector

K. Poertner, Resident Inspector

G. Belisle, Chief, Reactor Projects Branch 5

Division of Reactor Projects

ENCLOSURE 2

EXECUTIVE SUMMARY

Surry Power Station. Units 1 & 2

NRC Inspection Report 50-280/96-12, 50-281/96-12

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 5-week

period of resident inspection.

Operations

One violation was identified involving an inadequate procedure that

resulted in the Alternate Alternating Current (AAC) Diesel Generator not

being available for operation from the control room assuming a station

blackout event.

The inspectors also determined that operations

exhibited a lack of questioning attitude during return to service of the

AAC diesel generator (Section 01.2).

Unit 2 tripped from approximately 11 percent on December 13 during a

unit shutdown.

Primary plant response was normal and plant safety

systems functioned as designed.

However. four Individual Rod Position

Indicators (IRPis) failed to properly display rod position following the

trip. Control room personnel performed well during the trip recovery.

As demonstrated in previous transients, the steam generator water level

control system does not lend itself to stable operations at low power

levels (Section 01.3).

The Unit 1 Auxiliary Feedwater System was properly aligned. Equipment

operability, component labeling, material condition, and housekeeping

were acceptable (Section 02.1).

The Unit 2 Containment Spray System alignment and material condition

were found to be satisfactory. Two Updated Final Safety Analysis Report

(UFSAR) discrepancies were identified and are being resolved by the

licensee's corrective action process (Section 02.2).

Maintenance

Maintenance activities involving feedwater flow control valve positioner

adjustment and service water pump rotating assembly replacement and

surveillance activities involving control rod drop and turbine driven

auxiliary feedwater pump tests were performed in accordance with work

package requirements. The feedwater valve positioner repair evolution

was well staffed and executed, and had excellent management support

(Sections Ml.l, Ml.2, Ml.3, and Ml.4).

Engineering

Temporary modification S2-96-28 was acceptable and the associated safety

evaluation adequately justified _implementation (Section El.1).

Plant Support

Health physics practices were observed to be proper (Section Rl) .

i_ --. ----

-- ----- ----

2

The performance of the emergency response organization during the annual

Emergency Preparedness (EP) exercise conducted November 13 was

considered fully satisfactory (Section Pl.l).

A previously identified exercise weakness was sucessfully resolved

(Section PB . 1).

Security and material condition of the protected area perimeter barrier

were acceptable (Section Sl) .




---- ---------


--

Report Details

Summary of Plant Status

Unit 1 operated at or near 100 percent power the entire reporting period.

Unit 2 began the reporting period at approximately 100 percent power.

On

November 19, with the unit at reduced power for the quarterly turbine inlet

valve freedom test, the D reheat stop valve would not open after being

exercised to the closed position. As required by the valve freedom test

procedure, Unit 2 power was reduced to less than 50 percent (approximately 49

percent). The valve was repaired, reopened, and the unit returned to 100

percent power on November 20.

On November 25, power was again reduced to 49

percent due to the B reheat intercept valve failing to reopen during a

performance of the turbine valve freedom test procedure. The valve did not

reopen due to a failure of the electrohydraulic control dump valve. The valve

was repaired and the unit was returned to 100 percent power on November 26.

The unit operated at approximately 100 percent power until December 12 when a

unit shutdown commenced for a scheduled maintenance outage to modify the

letdown piping configuration. During the shutdown activities, a reactor trip

occurred on December 13 at 2:33 a.m. (Section 01.3). The unit remained

shutdown the remainder of the reporting period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707. 40500)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness, and adherence to approved *procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved. The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Inoperable AAC Diesel Generator

a. Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding the mispositioning

of the AAC Diesel Generator output breaker control switch.

b. Observations and Findings

On November 13 at 10:30 p.m. operations was tagging out the AAC Diesel

Generator for battery maintenance per procedure O-MOP-AAC-001, Removal

- -.-----

  • -*

2

from Service of the AAC Diesel Generator, Revision 1, when the operator

determined that the AAC Diesel Generator output breaker control switch

was already in the pull-to-lock position. The operators initiated a DR

on the as found condition of the control switch and completed the

procedure to remove the AAC Diesel Generator from service.

Review of procedure O-MOP-AAC-002, Return to Service of the AAC Diesel

Generator, Revision 1, determined that the procedure placed the control

switch in the pull-to-lock position prior to racking in the output

breaker but did not return the switch to the auto position after the

breaker was racked in. The AAC Diesel Generator automatically starts

during a station blackout scenario and the output breaker closes to

power AAC busses. The operators in the control room then manually align

the AAC busses to the emergency busses from the control room.

With the

control switch in the pull-to-lock position the generator output breaker

would not automatically close following a station blackout event.

Failure of the breaker to close would result in an alarm in the control

room and the annunciator response procedure and abnormal procedure would

direct the operator to align the AAC Diesel Generator manually. This

would require that an operator be dispatched to the AAC Diesel Generator

Building.

The licensee determined that procedure O-MOP-AAC-002 had last been

performed on September 24.

The AAC Diesel Generator had been removed

from service to allow scaffolding removal from the exhaust stack. The

procedure had also been performed on September 20 following application

of a coating to the exhaust stack. The AAC Diesel Generator had not

been run in either case because the maintenance performed did not effect

the operation of the AAC Diesel Generator. The procedure had not been

performed prior to September 20.

The licensee initiated a Category 2 root cause evaluation to determine

why the problem had occurred and to provide corrective actions to

prevent recurrence. The licensee had not completed the root cause

evaluation as of the end of the inspection period.

However, several

corrective actions had been implemented. These included revising the

deficient procedure, revising operator logs to require that the control

switch position be verified, and additional training of operations

personnel on AAC Diesel Generator operation.

The AAC Diesel Generator is not addressed in the TS's. The licensee

committed to install the AAC Diesel Generator to meet the requirements

of 10 CFR 50.63.

AAC Diesel Generator installation and testing was

completed for both units in May 1996. Station Administrative Procedure,

VPAP 2802, Notifications and Reports, Revision 6, Section 6.28,

Discretionary Reports, requires that a special report be submitted to

the NRC if the AAC system is out of service for 14 consecutive days.

The licensee submitted a special report as required by VPAP 2802.

The inspectors determined that procedure O-MOP-AAC-002 was inadequate to

return the AAC Diesel Generator to service. This item is identified as

Violation 50-280, 281/96012-01. The licensee had an opportunity to


. ---

3

identify that the AAC Diesel Generator control switch was mispositioned

on September 24 during the second performance of procedure O-MOP-AAC-

001.

The failure to question the as-found switch position resulted in

the system not being available for operation from the control room as

designed for an extended period of time.

c. Conclusions

One violation was identified involving an inadequate procedure that

resulted in the AAC Diesel Generator not being available for operation

from the control room assuming a station blackout event. The inspectors

also determined that operations exhibited a lack of questioning attitude

during return to service of the AAC Diesel Generator.

01.3 Unit 2 Reactor Trip During Shutdown

a.

Inspection Scope (71707)

The inspectors reviewed the circumstances related to the December 13

Unit 2 reactor trip.

b. Observations and Findings

On December 13, 1996, at 2:33 a.m., Unit 2 tripped from approximately 11

percent reactor power (80 MWe).

The unit was being shutdown for a

planned maintenance outage to replace a portion of the letdown line.

Steam generator (S/G) water level was being manually controlled with the

feedwater regulation bypass valves at the time of the trip. During

previous operations at low power levels, the inspectors had observed

that the S/G water level control system does not lend itself to stable

operations. The reactor trip signal resulted from a steam flow/feed

flow mismatch coincident with a low level in the A S/G.

One of the two

channels of the A S/G water level was less than 20 percent narrow range

with one of the two channels of A S/G steam flow greater than feedwater

flow by .709E06 pounds mass per hour.

The motor driven auxiliary

feedwater pumps automatically initiated as designed. Reactor Coolant

System (RCS) temperature decreased to a minimum of approximately 539

degrees F.following the trip.

No primary or secondary power operated*

relief valves or safety valves actuated during the transient.

Four control rod Individual Rod Position Indicators CIRPis) displayed

between 10 and 32 steps (P6-17 steps, D4-34 steps, M4-11 steps, and F6-

17 steps) following the trip and the associated rod bottom light for

control rod P6 did not illuminate. Emergency boration was initiated in

accordance with the Emergency Operating Procedures (EOPs) to compensate

for the indicated rod positions. The unit was stabilized in hot

shutdown with a RCS temperature of approximately .546 degrees F.

The inspectors were in the control room at the time of the trip and

observed the immediate and recovery actions performed by the operators.

The appropriate EOPs were entered and executed. Following the trip,

command and control within the control room was good.

The unit

~-* ----


4

supervisor ensured his orders were carried out before proceeding to the

next action in the EOPs.

The actions specified in the EOPs were

completed at approximately 3:10 a.m. Accordingly, the shift entered the

. general operating procedure for plant cooldown.

The event was reported

to the NRC operations center at 4:25 a.m. in accordance with 10 CFR

50.72.

A post trip debrief was conducted with the operations shift following

their relief. Other than the problems with the four IRPis and one rod

bottom light discussed above, there were no other significant additional

plant equipment problems.

Hot rod drop testing was conducted following

the trip to confirm the capability of. the four rods discussed above to

fully insert (see Section Ml.3). Plant personnel were planning to

repair the four IRPis and one rod bottom light prior to restart of the

unit.

c. Conclusions

The inspectors concluded that response of the primary plant following

the reactor trip on December 13 was normal.

Plant safety systems

functioned as designed.

However, four IRPis failed to properly display

rod position following the trip. Control room personnel performed well

during the trip recovery.

As demonstrated in previous transients, the

S/G water level control system does not lend itself to stable operations

at low power levels.

02

Operational Status of Facilities and Equipment

02.1 Auxiliary Feedwater (AFW) System Walkdown

a.

Inspection Scope (71707)

During the inspection period the inspectors walked down portions of the

Unit 1 AFW System.

b. Observations and Findings

The inspectors reviewed the AFW system alignment using procedure 1-0P-

FW-OOlA, Auxiliary Feedwater System Alignment, Revision land system

drawing 11448-FM-068A, Feedwater System.

The inspectors also reviewed

equipment operability, component labeling, general material condition,

and housekeeping.

The specific system portions inspected included the

AFW pumps, and the accessible pump suction.and discharge piping.

c. Conclusions

Equipment operability, component labeling, material condition; and

housekeeping were acceptable. The inspectors did not identify any

discrepancies between the required system alignment and the actual

system configuration.


5

02.2 Unit 2 Containment Spray (CS) System Walkdown

a.

Inspection Scope (71707)

A walkdown of the Unit 2 CS System was performed to check the major flow

paths. system material condition, and the system parameters and

  • conditions specified in the TS and the Updated Final Safety Analysis

Report (UFSAR).

b. Observations and Findings

The inspectors performed a hand over hand walkdown of a majority of the

accessible portions of the Unit 2 containment spray system. This

included piping, control switches, breakers. and associated

instrumentation for proper alignment and material condition. All system

components were found in their designated position for system standby

readiness. Overall material condition of the equipment was good.

However, during the walkdown, a pressure gauge, 2-CS-PI-203 (Refueling

Water Storage Tank (RWST) Test Recirc Inlet Header Pressure), was found

pegged upscale. This was brought to the attention of the shift

supervisor who initiated action to repair the gauge.

The guage provides

local indication only. A followup walkdown revealed that the condition

had been repaired.

The inspectors reviewed the UFSAR to ensure specified system parameters

demonstrated actual plant conditions. During the review of UFSAR

Paragraph 6.3.l.3, the inspectors noted a statement concerning RWST

level being in conflict with TSs. Specifically TS 3.4.A.3, requires a

minimum RWST level of 387,100 gallons of borated water, while the UFSAR

specified 387,000 gallons. The licensee attributed this matter to a

typographical error during a previous UFSAR revision. The licensee

stated that this minor discrepancy would be resolved during an upcoming

UFSAR revision.

During the review of UFSAR Paragraph 6.3.1.2.1, the inspectors noted a

statement which described conditions within the containment spray piping

following a system actuation. The statement reads as follows; "This

system contains the sodium hydroxide solution only while operating

during an incident, which is a period of approximately 30.min." The

inspectors explored this matter further because the licensee is

currently experiencing leakage of sodium hydroxide solution from the

chemical addition tank into the system through the normally closed tank

outlet valves 2-CS-MOV-202A and 2028. This matter was brought to the

attention of the licensee. A DR (S-96~2739) was initiated. The

licensee currently monitors chemistry in the CS piping downstream of the

chemical addition tank valves. Flushing of the lines occurs if sodium

levels exceed 500 ppm.

6

c. Conclusions

The Unit 2 CS System alignment and material condition were found to be

satisfactory. Two UFSAR discrepancies were identified and are being

resolved by the licensee's corrective action process.

II. Maintenance

Ml

Conduct of Maintenance

Ml.1 Feedwater Flow Control Valve Positioner Adjustment (62707)

On December 3, the inspectors observed activities associated with Work

Order (WO) 00354668, Repair Valve Positioner, which replaced positioner

components for Feedwater (FW) Flow Control Valve (FCV) 1-FW-FCV-1478.

The maintenance was performed to prevent failure of the positioner due*

to increased valve oscillations. The work was accomplished in

accordance with the work package requirements. The operators reduced

reactor power, throttled the A FW isolation valve (1-FW-MOV-154A), and

opened the corresponding bypass valve (1-FW-MOV-155A).

FCV-1478 was

placed on the jack, repaired, stroke tested, and returned to service in

24 minutes. The evolution was well staffed and executed, and had

excellent management support. The inspectors observed that the valve

had a packing leak and steam was visible. The repair did not appear to

reduce valve oscillation .

Ml.2 Service Water Pump Maintenance (62707)

The inspectors observed portions of the work activities associated with

WO 354376, Replace rotating assembly for pump 2-SW-P-lOB.

The

maintenance activity was accomplished in accordance with procedure. O-

MCM-0130-05, Goulds 3996ST Pump Overhaul, Revision 1. The inspectors

verified that the system isolation boundary was adequate to perform the

maintenance activity and that maintenance personnel were implementing

the maintenance procedure.

Ml.3 Unit 2 Control Rod Drop Testing (61726)

The inspectors observed Unit 2 control rod drop testing conducted

December 13. The testing was performed following a Unit 2 reactor trip

discussed in Section 01.3. During the reactor trip four control rods

did not indicate less than 10 steps as required by the emergency

procedures.

The rod testing was performed using procedure 2-NPT-RX-014, Hot Rod

Drops by Bank, Revision 2. The inspectors observed the testing of all

control rod banks and reviewed the control rod drop time data obtained.

All control rod drop times were acceptable and the control rods

exhibited full insertion.

7

Ml.4 Turbine Driven Auxiliary Feedwater (TDAFW) Pump Testing (61726)

On December 11. the inspectors observed the performance of procedure

1-0PT-FW-003, Turbine Driven Auxiliary Feedwater Pump 2-FW-P-2,

Revision 7.

The procedure demonstrates the operability of the TDAFW

pump and associated valves. The inspectors monitored activities in

progress and verified that procedure acceptance criteria were met.

Ml.5 Conclusions on Conduct of Maintenance

Maintenance and surveillance activities observed were performed in

accordance with work package requirements. The feedwater valve

positioner repair evolution was well staffed and executed and had

excellent management support.

III. Engineering

El

Conduct of Engineering

El.1 Temporary Modification Review

a.

Inspection Scope (37551)

The inspectors reviewed temporary modification package S2-96-28,

Thermowell for RTD 2-FW-RTD-2118 Failed.

b. Observations and Findings

The inspectors reviewed the temporary modification package and safety

evaluation associated with temporary modification S2-96-28. * The

temporary modification was implemented to relocate the 8 feedwater line

Resistance Temperature Detector (RTD) to a spare thermowell.

The

temporary modification was required due to the failure of the RTD as the

result of thermowell leakage. The feedwater RTD supplies input to the

plant computer and the calorimetric program.

With the B feedwater RTD

failed the plant computer calorimetric program was inaccurate and

operations was required to perform manual calorimetric calculations.

c. Conclusions

The inspectors determined that temporary modification S2-96-28 was

acceptable and that the associated safety evaluation adequately

justified implementation.

E7

Quality Assurance in Engineering Activities

E7.1 Review of UFSAR Commitments (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compared plant practices, procedures and/or

parameters to the UFSAR description. While performing the inspections

8

discussed in this report, the. inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected.

Two UFSAR

discrepancies associated with the CS System were identified and are

discussed in Section 02.2.

IV. Plant Support

Rl

Radiological Protection and Chemistry Controls (71750)

On numerous occasions during the inspection period, the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit, survey results, and radiological area material

conditions.

No discrepancies were noted, and the inspectors determined

that RP practices were proper.

Pl

Conduct of EP Activities

Pl.1 Annual EP Drill

a.

Inspection Scope (82301)

On November 13, the inspectors observed the performance of the

licensee's annual EP drill.

b. Observations and Findings

The purpose of the exercise conducted November 13 was to activate and

evaluate major portions of the Surry emergency response plan. The

inspectors reviewed the drill scenario and observed activities conducted

at the simulator, Technical Support Center and Operations Support

Center. Activities observed were consistent with the drill scenario and

demonstrated proper accident mitigation and damage control

considerations.

c. Conclusions

The performance of the emergency response organization was considered

fully satisfactory.

PB

Miscellaneous EP Issues (92904)

P8.l(Closed) Exercise Weakness CEW) 50-280, 281/95010-01:

damage control

teams were not timely managed. The inspectors observed an emergency

drill conducted November 13. The inspectors observed activities

conducted at the Operations Support Center throughout the drill

scenario. The drill demonstrated the ability to prioritize tasks and

identify accident mitigation activities. Damage control teams were

dispatched in a *timely manner t~ accomplish designated tasks .

9

Sl

Conduct of Security and Safequards Activities (71750)

On numerous occasions during the inspection period, the inspectors

performed walkdowns of the protected area perimeter to assess security

and general barrier conditions.

No deficiencies were noted, and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained .

10

V. Management Meetings

Xl

Exit Meeting SuDIDary

The inspectors presented the inspection results to members of licensee *

management at the conclusion of the inspection on December 20, 1996.

The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified.

X2

SALP Presentation Meeting

On November 18, the Regional Administrator presented the results of the latest

SALP assessment.

The Regional Administrator also met with local officials and

conducted a press conference .

11

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Blount, Superintendent, Maintenance

D. Christian, Station Manager

M. Crist, Superintendent, Operations

J. McCarthy, Assistant Station Manager, Operations & Maintenance

B. Shriver, Assistant Station Manager, Nuclear Safety & Licensing

T. Sowers, Superintendent, Engineering

B. Stanley, Director, Nuclear Oversight

J. Swientoniewski, Supervisor Station Nuclear Safety

W. Thorton, Superintendent, Radiological Protection

G. Belisle, Chief, Branch 5, Division of Reactor Projects, Region II

S. Ebneter, Regional Administrator, Region II

G. Edison, Surry Project Manager, Office of Nuclear Reactor Regulation

J. Johnson. Deputy Director, Division of Reactor Projects, Region II

M. Reinhart, Acting Director, Project Directorate II-1, Office of Nuclear

Reactor Regulation

.,.. ,J.,

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 82301:

IP 92904:

Opened

12

INSPECTION PROCEDURES USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Surveillance Observation

Maintenance Observation

Plant Operations

Plant Support Activities

Evaluation of Emergency Exercises for Power Reactors

Followup - Plant Support

ITEMS OPENED AND CLOSED

50-280, 281/96012-01

VIO

inadequate AAC Diesel Generator return to

service procedure (Section 01.2).

Closed

50-280, 281/95010-01

EW

damage control teams were not timely managed

(Section P8.1) .