ML18153A083

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Insp Repts 50-280/96-09 & 50-281/96-09 on 960728-0907. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maintenance & Plant Support
ML18153A083
Person / Time
Site: Surry  Dominion icon.png
Issue date: 10/07/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153A080 List:
References
50-280-96-09, 50-280-96-9, 50-281-96-09, 50-281-96-9, NUDOCS 9610220117
Download: ML18153A083 (30)


See also: IR 05000280/1996009

Text

, *

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

License Nos:

Report Nos:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9610220117 961007

PDR

ADOCK 05000280

G

PDR

50-280, 50-281

DPR-32, DPR-37

50-280/96-09, 50-281/96-09

Virginia Electric and Power Company (VEPCO)

Surry Power Station, Units 1 & 2

5850 Hog Island Road

Surry, VA 23883

July 28 - September 7, 1996

R. Musser, Senior Resident Inspector

M. Branch, Senior Resident Inspector

D. Kern, Resident Inspector

W. Poertner, Resident Inspector

P. Fillion, Reactor Inspector (Section El.1)

J. York, Reactor Inspector (Sections E2.l, E3.2,

E4.l, E5.2, and E7.1)

R. Moore. Reactor Inspector (Sections E2.l,

E3.2, E4.l, E5.2, and E7.1)

G. Edison, Project Manager, NRR (Sections El.3,

E3.l, and E5.l)

R. Gibbs, Reactor Inspector (Sections M8.6,

M8.7, M8.8, and El.2)

D. Taylor, Resident Inspector, North Anna

(Section Ml.2)

G. Belisle, Chief, Reactor Projects Branch 5

Division of Reactor Projects

ENCLOSURE 2

EXECUTIVE SUMMARY

Surry Power Station, Units 1 & 2

NRC Inspection Report 50-280/96-09, 50-281/96-09

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support.

The report covers a six-week

period of resident inspection; in addition, it includes the results of

announced inspections by four regional inspectors, the North Anna Resident

Inspector, and the Office of Nuclear Reactor Regulation Surry Project Manager.

Operations

Primary plant response following the Unit 2 reactor trip on August 3 was

normal and the unit was promptly placed in a stable hot shutdown condition by

the operating crew. Safety systems functioned as designed and equipment

problems were evaluated and resolved prior to returning the unit to power.

Operator action to trip the unit following the closure of the turbine governor

valves was appropriate and demonstrated excellent awareness of ongoing

activities that could potentially challenge plant operation (Section 01.2).

The licensee's actions in repairing the failed Consequence Limiting Safeguards

(CLS) relay were appropriate. The initiation of a controlled plant shutdown

approximately six hours prior to expiration of the Limiting Condition of

Operation (LCO) demonstrated a sound and safe operating judgement (Section

01.3).

Preparations for Hurricane Fran were conservative. Operators communicated

closely during the storm while responding to heavy storm debris fouling at the

low level intake structure (Section 01.4).

A Non-Cited Violaton (NCV) was identified for not maintaining Unit 2 control

room logs in the form required by procedures (Section 01.5).

Maintenance

The inspectors concluded that the licensee's repair of the letdown line was

acceptable. However, this leak is the third such occurrence in the last nine

months and no root cause had been identified (Section Ml.1).

Appropriate corrective action was taken to restore 1-SW-P-lA to service prior

to Hurricane Fran arriving on-site. Operators performed the operability

surveillance procedure in a professional manner (Section Ml.2).

One NCV was identified for operating with a non-isolable leak (Section M8.8).

Engineering

The inspectors performed a review of 348 Deviation Reports (DRs) covering

various systems, significance levels and time periods. Observations and

findings from this review indicated that the conduct of engineering was good.

A violation was identified for failing to specify breaker set points in a

design change package which resulted in incorrect set points and breakers

spuriously tripping during operation of the plant (Section El.l).

2

The inspectors concluded that through careful management attention, the number

of Temporary Modifications CTMs) for both units has been maintained at a low

level (fewer than ten) for several years (Section El.3).

The engineering process for material upgrade and item equivalency evaluation

adequately provided for installation of appropriate quality level material in

safety related applications (Section E2.1).

The inspectors concluded that the licensee's 10 CFR 50.59 procedures were

comprehensive, thorough, and well written (Section E3.1).

Manager training on a wide variety of subjects was being used to enhance the

engineering supervision in making more informed decisions (Section E5.2).

The Design Control and Engineering Program audit was thorough, detailed and

resulted in meaningful findings (Section E7.1).

Plant Support

Radiological protection personnel took prompt and appropriate action when

notified that contaminated steel plating may have been inadvertently shipped

to the site (Section R8.1) .

Report Details

Summary of Plant Status

Unit 1 operated at approximately 100 percent power the entire reporting

period.

Unit 2 operated at approximately 100 percent power until August 3, when the

reactor was manually tripped due to a loss of Electro Hydraulic Control (EHC)

pressure during a maintenance evolution. Following repairs. the unit was

taken critical at 12:57 a.m. on August 5, and reached 100 percent power at

8:51 p.m. the same day.

Unit 2 remained at approximately 100 percent power

until August 27, at 3:19 a.m., when the licensee initiated a shutdown in

accordance with Technical Specification (TS) 3.7-2 due to a failed relay in

the Hi Hi Consequence Limiting Safeguards (CLS) logic system.

At 7:27 a.m.,

with power at approximately 30 percent, repairs were completed and the

Limiting Condition of Operation (LCO) was exited. Unit 2 was returned to 100

percent power at 8:14 p.m.

Unit 2 remained at approximately 100 percent power

until September 6, when at 5:01 a.m., the operations shift began reducing

power due to debris in the river causing fouling problems at the low level

intake structure. At 9:39 a.m., the unit had been reduced to 49 percent

power.

At 12:49 p.m., a power increase commenced until a maximum attainable

power level of approximately 94 percent was achieved.

Power was limited due

to reduced flow through the main condenser.

Unit 2 remained at this power

level for the remainder of the inspection period while repairs were being

completed at the intake.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707, 40500)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness. and adherence to approved procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with TSs.

Instrumentation and

safety system lineups were periodically reviewed from control room

indications to assess operability. Frequent plant tours were conducted

to observe equipment status and housekeeping. Deviation Reports (DRs)

were reviewed to assure that potential safety concerns were properly

reported and resolved. The inspectors found that daily operations were

generally conducted in accordance with regulatory requirements and plant

procedures.

01.2 Unit 2 Reactor Trip

a.

Inspection Scope (71707)

At 3:05 p.m. on August 3, the Unit 2 reactor operator manually tripped

Unit 2 from 88 percent power due to closure of the turbine governor

2

valves and intercept valves. The inspectors reviewed the circumstances

surrounding the Unit 2 trip and independently reviewed the plant

response following the reactor trip.

b.

Observations and Findings

On August 3, a leak was identified on a one-inch EHC compression fitting

located on the emergency trip header for the turbine governor and

intercept valves. The licensee attempted to stop the leak by tightening

the compression fitting. While tightening the leaking fitting, tubing

separated from another union that was not being tightened. The loss of

EHC oil pressure resulted in the closure of the turbine governor and

intercept valves. The control room operator was monitoring turbine

governor valve position and manually tripped the reactor prior to an

automatic trip signal being generated. The potential for a reactor trip

during the maintenance activity had been briefed by the operating crew

prior to allowing the work to commence. After the reactor trip, four

Individual Rod Position Indicators (IRPis) indicated between 10 and 12

steps withdrawn and then drifted to zero within two minutes.

Licensee

procedures require that all IRPis indicate less than 10 steps following

a reactor trip. The reactor coolant system was borated in accordance

with procedures and the shutdown margin was verified. The Auxiliary

Feedwater System (AFW) automatically initiated as designed and no

primary or secondary power operated or safety relief valves actuated

during the trip.

The licensee determined that the leaking compression fitting and the

compression fitting that separated had not been properly installed,

i.e., the ferrule was not properly set on the tubing due to inadequate

crimping torque. The two compression fitting unions that initiated the

reactor trip were repaired and four additional fittings adjacent to the

failed fittings were inspected using GO/NO GO gauges. These fittings

were loose and were repaired. The licensee was unable to determine when

the compression fittings were installed (most likely during original

construction) but did determine that no work had been performed on the

fittings during the last Unit 2 refueling outage.

The cause of why four IRPis did not initially indicate less than 10

steps was investigated. Minor adjustments were required on the signal

conditioning card for one IRPI.

No other problems were identified. Hot

rod drop testing was performed on the four rods (G3, F6, Fl2, and Jl3)

and the inspectors verified that rod drop times were acceptable.

The inspectors independently reviewed the post trip review and attended

the restart meetings conducted by the licensee. The unit was taken

critical at 12:57 a.m. on August 5, and was returned to 100 percent

power at 8:51 p.m. later that same day.

c. Conclusions

Primary plant response following the reactor trip on August 3 was normal

and the unit was promptly placed in a stable hot shutdown condition by

3

the operating crew. Safety systems functioned as designed and equipment

problems were evaluated and resolved prior to returning the unit to

power. Operator action to trip the unit following the closure of the

turbine governor valves was appropriate and demonstrated excellent

awareness of ongoing activities that could potentially challenge plant

operation.

01.3 Unit 2 Power Reduction

a.

Inspection Scope (71707. 92901)

On August 27, at 3:19 a.m., the licensee initiated a shutdown of Unit 2

in accordance with TS 3.7-2 due to a failed relay in the Hi-Hi CLS logic

system.

The inspectors were notified of the condition and responded to

the site to follow the licensee's actions.

b. Observations and Findings

On August 26, during the performance of monthly Hi-Hi CLS logic testing,

train A would not reset rendering the A train inoperable. A 12-hour

to hot shutdown LCO was initiated at 9:10 p.m., in accordance with

TS 3.7-2. Investigation revealed that a relay (3-CLS-2AMX) failed

resulting in the train being inoperable. Replacement of the relay

required the development and installation of a Temporary Modification

(TM).

Appropriate personnel were called into the station to support the

repair effort.

The inspectors were informed of the problem at approximately 2:20 a.m.

on August 27, and responded to the site to review the licensee's

actions. At 3:19 a.m., the licensee began a controlled reactor shutdown

by reducing power at approximately 150 megawatts electric per hour.

This problem was appropriately reported to the NRC Operations Center in

accordance with 10 CFR 50.72 at 3:27 a.m.

The inspectors arrived on

site and attended the Station Nuclear Safety and Operating Committee

(SNSOC) review of the TM and plant status. The TM was appropriately

reviewed and approved.

At 6:50 a.m., with Unit 2 at 30 percent power,

the power reduction was stopped while the repair effort was underway.

The operations shift and maintenance personnel were appropriately

briefed by the cognizant engineer.

An extra reactor operator was placed

in the control room to monitor plant parameters while the repair was in

progress. The relay was replaced, successfully tested and the system

returned to service. The LCO was exited at 7:27 a.m.

Unit 2 was

returned to 100 percent power at 8:14 p.m.

c. Conclusions

The licensee's actions in repairing the failed CLS relay were

appropriate. The initiation of a controlled plant shutdown

approximately six hours prior to expiration of the LCO demonstrated

sound and safe operating judgement.

4

01.4 Preparations for Hurricane Fran

a.

Inspection Scope (71707)

The inspectors reviewed the Updated Final Safety Analysis Report

(UFSAR), the Virginia Power Hurricane Response Plan, revision 2, and

monitored the licensee's hurricane preparations. Additionally, on

September 5 and 6, the inspectors toured outside areas looking for loose

or unsecured items and monitored the low level intake structure to

evaluate the storm's effect on the water supply for the ultimate heat

sink.

b. Observations and Findings

Hurricane Fran approached the North Carolina coast on September 5.

The

licensee monitored the storm track and implemented severe weather

preparations in accordance with Operations Checklist (OC)-21, Severe

Weather, and O-AP-37.01, Abnormal Environmental Condition, revision 6.

The Virginia Electric Power Company (VEPCO) Hurricane Response Plan is

triggered by the prediction of hurricane force winds on-site by the

Vi rgi ni a Power Weather Center. Hurricane force wi nd_s were not predicted

during the approach of Hurricane Fran; however, the licensee did

implement the plan on September 5 as a precautionary measure when the

storm was predicted to pass through the area. The inspectors reviewed

the licensee's preparations, reviewed the status of important systems,

and monitored the storm's progress. The outside areas inspected were

clean. Siding at the high level intake structure which became loose

during the high winds was promptly secured.

Maintenance and

surveillance activities performed by the licensee were minimized during

the approach of the storm. Repairs to Emergency Service Water (ESW)

pump 1-SW-P-lA (see Section Ml.2) continued through all three shifts and

the pump was declared operable at 10:15 p.m. on September 5 prior to the

storm's arrival.

Heavy debris from the river began fouling the low level intake structure

screens early on September 6 as the storm reached the site. Two

Circulating Water (CW) pumps became unavailable due to heavy screen

fouling and screen damage.

The inspectors observed operator activities

in the control room and at the low level intake structure. Operators

reduced reactor power sufficiently to maintain normal intake canal level

while the water supply from the river was degraded. Operators worked

diligently to maximize the number of available CW pumps.

Power to both onsite meteorological towers was lost when the storm

reached the site. The licensee maintained contact with local weather

services to ensure they maintained accurate tracking of area wind speed.

The maximum sustained onsite wind speed was 40 mph with gusts to 54 mph.

Following the storm, Unit 2 reactor power was increased from 49 percent

to 94 percent. Hurricane force winds were not observed onsite and the

VEPCO Hurricane Response Plan was terminated at 1:55 p.m. on September

6.

5

At 12:40 p.m. on September 6, the licensee determined that 26 of 61

emergency warning sirens for the surrounding Emergency Planning Zone

(EPZ) were inoperable. Storm damage caused power to be lost to 23 of

the 26 sirens. The licensee made a I-hour non-emergency notification to

the NRC and a 4-hour notification to state officials to report the

partial loss of off-site emergency notification capability. The

inspectors discussed alternate notification methods with emergency

preparedness personnel. Alternate notification methods to the effected

areas by local officials are established by letters of agreement.

Repairs were promptly initiated. Fifty-six sirens were operable by noon

on September 7 and all 61 sirens were operable by 7:30 a.m. on

September 9.

c. Conclusions

The licensee's actions in preparation for Hurricane Fran were

conservative. Operators communicated closely during the storm while

responding to heavy debris fouling at the low level intake structure.

01.5 Operations Logs

a.

Inspection Scope (71707)

On September 6, the inspectors performed a control room tour to review

current plant conditions.

As a part of this activity, control room logs

were reviewed.

b. Observations and Findings

During the review of plant conditions, the inspectors determined that at

approximately 2:00 p.m. on September 6, no official Unit 2 control room

log had been initiated for the day shift (8:00 a.m. - 4:00 p.m.)

operating crew.

At the Surry Power Station, control room logs are

normally maintained on the plant computer system. The inspectors

observed that only an informal log was being maintained by the Unit 2

reactor operator.

When the inspectors questioned the operating shift

about this matter, the inspectors were informed that because the site

computer was out of service, an informal log was being maintained until

the plant computer was returned to service.

The inspectors had recently reviewed procedure OPAP-0004, Logs and

Operating Records, revision 5, which stated that handwritten narrative

logs should be written on pre-formatted loose-leaf pages approved by the

Superintendent, Operations. The inspectors questioned the shift

supervisor about this matter and he was unaware of this requirement.

The plant computer was returned to service shortly after this

observation and the informal log was transcribed into the computer.

The inspectors brought this matter to the attention of the

Superintendent. Operations. who stated he would ensure the operations

staff was informed of this requirement. The inspector's concern in this

matter was the lack of formality for the official record of the plant

6

six hours into the operating shift. The Superintendent, Operations,

stated that this matter did not meet his expectations and would be

corrected. This was an isolated observation. This failure to maintain

the handwritten narrative logs in a form as required by procedures is a

violation. This failure constitues a violation of minor significance

and is being treated as an NCV, consistent with Section IV of the NRC

Enforcement Policy (50-281/96-09-01).

c. Conclusions

A. NCV was identified for not maintaining Unit 2 control room logs in the

form required by procedures. This was an isolated observation.

II. Maintenance

Ml

Conduct of Maintenance

Ml.1 Unit 2 Letdown Line Repair

a.

Inspection Scope (62703)

On August 13, plant operators determined that Unit 2 total Reactor

Coolant system (RCS) unidentified leakage had increased from previous

values.

A containment entry revealed a leak on the normal letdown line

(2-inch line) downstream of valve 2-CH-HCV-2200C.

The inspectors

monitored the licensee's repair of the normal letdown line.

b. Observations and Findings

On August 13, following the identification of a leak on the normal

letdown line, normal letdown was isolated and excess letdown was placed

into service.

RCS unidentified leakage never exceeded TS allowed

values.

Inspection of the leak revealed a 1-inch crack on the vertical

weld on the tee downstream of letdown orifice isolation valve 2-CH-HCV-

2200C. This weld had previously failed in 1987.

The horizontal weld on

the same tee experienced two previous failures in December 1995 and

March 1996 (See NRC Inspection Report Nos. 50-280, 281/95-23 and 50-280,

281/96-02).

Station management conducted numerous meetings on this matter to

determine a course of action to repair the leak. A number of repair

options were proposed, one of which included shutting down and repairing

the leak with the unit offline. A unit shutdown was decided against due

to the challenges the operating shift would face in shutting down the

unit without normal letdown in service.

On August 14, the licensee

determined that the repair_ would take place with the unit online.

The repair was conducted by machining and grinding the defective weld

and rewelding the joint with the unit at power.

The joint was

successfully tested following its repair. This repair method eliminated

the affected area, preventing any meaningful failure analysis. Repairs

7

were completed and normal letdown was returned to service on August 16.

The licensee's engineering staff concluded that the most probable cause

of the failure was adverse flow induced vibration due to two phase flow.

To alleviate this, an interim support was proposed for installation

upstream of the 2-CH-HCV-2200C valve. A support is installed in Unit 1

at the same location. Additionally, the licensee plans to evaluate the

need to redesign the Unit 2 letdown piping configuration.

c. Conclusions

The inspectors concluded that the licensee's repair of the letdown line

was acceptable.

However. this leak is the third such occurrence in the

last nine months and no root cause had been identified.

Ml.2

ESW Pump Surveillance Observation

a. Inspection Scope (61726)

On September 4, the inspectors observed personnel performing O-OPT-SW-

001, Emergency Service Water Pump (ESWP) 1-SW-P-lA, revision 6.

The

diesel driven pump had tripped on overspeed on September 3, and the test

was being performed to prove operability after corrective maintenance to

the overspeed trip device. Approximately 11 minutes after pump start,

the pump tripped again on an apparent overspeed condition. The pre-test

brief. procedure preparation and pump start were observed.

b. Observations and Findings

The pre-test brief was thorough.

Procedure preparation steps were

observed to be properly performed. During the performance of procedure

step 6.1.7, which required pump house ventilation air dampers to be

opened, the operator noted that water tight hurricane covers had been

placed over the four wall damper openings.

The ceiling damper was not

obstructed. The covers were recently placed over the dampers due to

potential adverse weather conditions. The covers appeared to defeat the

intent of the step. After consultation with engineering and the unit

Senior Reactor Operators (SROs), the operator signed the step as

complete but made a reference to the covers in the procedure (the

dampers were open). A procedure change request was initiated to

recognize this condition for future procedure performance.

The

inspectors verified by an UFSAR review that operation of the diesel-

driven ESW pumps would not be affected with the damper covers installed.

The pump was started, and pump speed was increased to approximately 900

Revolutions Per Minute (rpm). After 11 minutes of operation, the pump

tripped on an apparent overspeed condition.

Pump rpm was not being

monitored at the time of the trip; however, there was no evidence that

pump speed had actually increased. Maintenance personnel consulted with

the vendor and system engineers and ran the pump several times to

evaluate the overspeed trip setpoint. Engineers found the trip setpoint

to be inconsistent and replaced the overspeed trip device.

Mechanics

8

readjusted the trip setpoint and ran the pump to demonstrate trip

setpoint repeatability and pump reliability. Procedure 1-0PT-SW-001 was

successfully performed as a post maintenance test and 1-SW-P-lA was

declared operable at 10:15 p.m. on September 5, in advance of Hurricane

Fran's arrival. The inspectors verified that the procedure was revised

to permit the test to be run with the hurricane covers installed over

the four wall dampers.

c. Conclusions

The inspectors concluded that test performance was good. Appropriate

corrective action was taken to restore 1-SW-P-lA to service prior to

Hurricane Fran arriving onsite.

Ml.3 Work Order 00343977 (62703)

The inspectors observed maintenance activities associated with Work

Order (WO) 00343977, Investigate Possible Grounds on 480 Volt Load

Center 2H.

The work activity involved obtaining ground detection system

voltage readings to allow comparison between the 3 phases and determine

if grounds were present. The inspectors observed activities in progress

and discussed the data obtained with engineering personnel. The work

activity was accomplished in accordance with the WO's instructions and

proper electrical safety precautions were implemented.

The voltage

readings obtained did not indicate that grounds were present.

Ml.4 Emergency Diesel Generator Testing (61726)

On August 31, the inspectors observed portions of the testing conducted

on the number 2 Emergency Diesel Generator (EOG).

The testing was

accomplished in accordance with procedure 2-0PT-EG-009, Number 2

Emergency Diesel Generator Major Maintenance Operability Test,

revision 0. Testing observed was accomplished in accordance with the

procedure and no discrepancies were noted.

The inspectors also reviewed

the completed procedure and verified that the acceptance criteria was

met prior to the licensee declaring the EDG operable.

MB

Miscellaneous Maintenance Issues (92700, 92902)

M8.l (Closed) Violation 50-280. 281/94-173 01014:

failure to identify and

promptly correct conditions adverse to quality.

On June 16, 1994, a

chemical release occurred which degraded both Auxiliary Ventilation

Exhaust Filter (AVEF) trains beyond TS requirements. The licensee

failed to recognize the potential for AVEF filter degradation and failed

to perform TS required filter efficiency testing in a timely manner.

The event and corrective actions were previously documented in NRC

Inspection Report Nos. 50-280, 281/94-21, 94-24, and 94-33 and Licensee

Event Reports (LERs) 50-280/94008-00, -01, and -02.

The licensee had

not anticipated filter damage from limited exposure to chemicals used

for Steam Generator Chemical Cleaning (SGCC).

Follow-up evaluation

failed to identify the specific chemical which caused the damage, but

did conclude that chemicals used for SGCC did damage the AVEF charcoal

9

filters. The inspectors reviewed corrective actions for this event to

determine whether they were adequately implemented to preclude

recurrence.

A broad TS review for event driven surveillances was completed.

Procedure revisions were implemented as appropriate to highlight the

need to perform specific event driven surveillances. Subsequent filter

testing confirmed that the replacement filters did not degrade following

SGCC completion. A mechanical jumper was installed to permit the non-

safety-related charcoal filters to be used for containment purge

operation during outages. including SGCC operations. This modification

in addition to procedure revisions were effective in minimizing the time

during which the category I safety-related AVEF filters are used for

routine operations. The inspectors observed that lessons learned from

this event were clearly communicated and implemented for the Unit 2 SGCC

outage. Operations personnel continued to properly implement these

lessons learned including greater sensitivity to event driven

surveillance requirements through the end of this report period. The

inspectors concluded that corrective actions for this event were

properly implemented.

M8.2

(Closed) LER 50-280/94008-01 and -02: entry into TS 4.0.3 for failure

to test new charcoal in accordance with TS 4.12.B.7(b) and a missed TS

surveillance. These LERs documented the dual train AVEF filter

degradation described in Section M8.1.

The two LER updates were

submitted to document subsequent charcoal filter efficiency test results

and clarify that the current test standards for new charcoal satisfied

TS requirements.

The LERs accurately documented the event and met

10 CFR 50.72 reporting criteria. The inspectors independently reviewed

charcoal filter test results and confirmed that the test results met the

TS acceptance criteria. The NRC is presently reviewing testing

requirements used by the industry and specified in TS to determine if

changes in requirements are warranted.

Any further review in this area,

if any, will be conducted as followup on that effort.

Corrective actions to review event driven TS surveillance requirements,

identified that a visual inspection following sensitized stainless steel

piping flushes was not performed as required by TS 4.2 during certain

occasions in the past. However, the piping has been successfully

visually inspected in accordance with the American Society of Mechanical

Engineers (ASME)Section XI program on a periodic basis. The missed

visual inspections following pipe flushes did not adversely affect

public health and safety. Procedures were revised to clearly identify

the visual inspection requirement. The inspectors determined that

corrective actions described in the LERs were complete.

M8.3

(Closed) LER 50-281/94001: both AVEF trains inoperable.

On January 24,

1994, the Unit 1 A train AVEF fan 1-VS-F-58A tripped repeatedly due to

excessive air flow and was declared inoperable. The normal power supply

to the redundant train fan, 1-VS-F-588, was unavailable due to a

surveillance test configuration. Operators declared both AVEF trains

inoperable and entered a six-hour LCO as required by TS 3.0.2. Both

10

AVEF trains were returned to service later that day, within the time

interval permitted by TS.

An alternate power supply remained available

to the 1-VS-F-58B fan throughout this event. The inspectors therefore

concluded that this event did not adversely effect public health and

safety.

Engineering determined that when the AVEF system was aligned other than

in its accident configuration, small flow anomalies can cause the

running fan to trip. Corrective actions included tighter controls for

making ventilation system adjustments and more frequent filter cleaning

to provide more margin between normal operations and the fan trip

setpoints. The inspectors reviewed procedure revisions, posted operator

aids, and log revisions. These actions have improved AVEF system

operation since the event. Engineering additionally proposed a design

change which would greatly reduce ventilation duct alignment

sensitivity. Engineering plans to have the design change fully

developed for management approval and implementation by October 1996.

The inspectors concluded that corrective actions were appropriate.

M8.4

(Closed) LER 50-281/94004: station battery 2A inoperable longer than

allowed due to personnel error.

On four separate occasions in October

1994, documented station battery 2A voltage readings indicated that cell

52 was inoperable. Licensee personnel failed to recognize the

inoperable condition and therefore failed to implement TS required

actions. Violation 50-281/94032-01 was issued for failure to promptly

identify and correct conditions adverse to quality.

NRC Inspection

Report Nos. 50-280, 281/94-24, 94-32, 95-07, 95-17, and 96-03 previously

documented the event and corrective actions. The LER documented the

event and causal factors in adequate detail and satisfied reporting

criteria specified in 10 CFR 50.72. The inspectors verified that

corrective actions for this event were appropriate and had been

completed.

The inspectors identified one minor error in the LER.

The

LER stated that the licensee verbally requested a Notice of Enforcement

Discretion for the inoperable station battery on October 27, 1994.

The

actual request date was October 28, 1994. The inspectors determined

that this error was administrative in nature and did not alter the

event's significance.

No LER update is necessary.

M8.5

(Closed) LER 50-280/96001-01: station and EDG battery connections not

coated with anti-corrosion material due to procedural error. The

original LER stated that a 24-hour LCD was entered for not completing TS

surveillance requirements for Station Battery 18 and EDG Batteries 1, 2,

and 3. This LER update was submitted to clarify that the LCD also

applied to Station Battery 28. This LER update corrected the original

omission. This event was documented in NRC Inspection Report 50-280,

281/96-07 and resulted in NCV 50-280, 281/96007-01.

M8.6 (Closed) Deviation 50-280. 281/96002-03: deviation from commitment to

reduce probability of core damage from flooding. This item reported two

deviations from commitments concerning inspections of CW rubber

expansion joints, i.e., internal inspections of the joints were not

being conducted in accordance with the vendor's recommendations, and

M8.7

11

changes to the inspection and service life replacement of these joints

were not receiving SNSOC review.

The first deviation was subsequently

withdrawn by the NRC, due to a change in the vendor's recommended

inspection of the joints. The deviation concerning SNSOC review was

acknowledged by the licensee and the following corrective actions were

specified in the licensee's response: 1) Revise model WOs for joint

inspections to require an 18 month inspection frequency (matching the

original commitment) and require SNSOC review of any changes to

inspection frequency; 2) Revise mechanical maintenance procedure

O-MCM-1003-01 to require SNSOC review of inspection frequency changes;

3) Revise VPAP-0803 to require SNSOC review of PM task evaluations and

deferrals for expansion joints; and, 4) Replace 16 expansion joints and

inspect four joints during the 1996 Unit 2 refueling outage.

The inspectors verified that procedures O-MCM-1003-01, Expansion Joint

  • Removal, Inspection and Installation, revision 2 Change P2, and VPAP-

0803, Preventive Maintenance Program, revision 6, had been revised to

include the SNSOC review requirements.

The inspectors reviewed a sample

of the model WOs and verified that proper inspection frequency and SNSOC

review requirements were included (Reference WOs 297013-01, 334126-01,

252622-01, 297009-01, 341927-01, and 341973-01).

In addition, the

inspectors reviewed a scheduling matrix which showed each CW joint along

with the last inspection and replacement date, and the next inspection

and replacement date, and verified that the dates had been adjusted to

match the licensee's original inspection and replacement commitments

(i.e., inspection every 18 months and replacement every eight years).

Additionally, the inspectors verified that the dates on the matrix

reflected that 16 joints had been replaced and four joints had been

inspected during the Unit 2 outage. The inspectors also reviewed a

sample of the completed WOs which accomplished the inspection and

replacement work (Reference 336640-01, 336641-01, 355179-01, 338875-01,

and 335180-01).

Based on this review the inspectors concluded that adequate corrective

actions had been completed to close this deviation.

(Closed) Unresolved Item (URI) 50-280. 281/96002-04:

review preventive

maintenance program deferral process. This unresolved item was issued

due to concerns related to the Preventive Maintenance (PM) deferral

process discovered during the investigation that led to Deviation 50-

280, 281/96-02-03. The concern was that PM deferrals were being

approved without an adequate technical basis, and rescheduling dates

were not being accurately established based on these deferrals.

As stated in the closure of Deviation 50-280, 281/96002-03 (Section

M8.6), the inspectors verified the accuracy of the scheduling dates for

the CW system joint inspections and replacements.

Inspection of the

licensee's PM program for the Low Head Safety Injection system,

documented in NRC Inspection Report Nos. 50-280, 281/96-07, included a

detailed review of inspection frequencies, scheduling dates, and the

technical adequacy of PM deferrals. That inspection concluded that

these areas were satisfactory. In addition, scheduling personnel

12

conducted a 100 percent review of all PM deferrals issued in the past

two and a half years to verify scheduled date accuracy.

The inspectors

reviewed the results with the scheduling supervisor and determined that

over 99 percent of the PM deferrals reviewed had correctly scheduled due

dates. The errors identified were promptly corrected and the PM

performed as necessary to bring them within the required periodicity.

Based on the review of Deviation 50-280, 281/96002-03, additional

inspections documented in NRC Inspection Report Nos. 50-280, 281/96-07,

and the 100 percent deferral review, the concerns which were the subject

of this URI were resolved.

M8.8 (Closed) LER 280/95007-00. (Open) LER 280/95007-01 (90712): operation

with non-isolable leak in pressurizer instrumentation nozzles. This LER

reported a leak in two of the upper pressurizer instrument line nozzles

on Unit 1. This condition was discovered by the licensee while other

work was being performed on the pressurizer during an outage.

The

licensee's immediate corrective actions included boroscopic and liquid

penetrant inspection of the two defective nozzles, and additional

inspection of the other instrument line penetrations into the

pressurizer. Cracks were found in the two leaking nozzles.

No evidence

of leakage on the other pressurizer penetrations was found.

The leaking

nozzles were removed and new nozzles were subsequently installed.

One

of the removed nozzles was retained for a detailed metallurgical

examination.

An evaluation for the continued operation of Unit 2

determined that the unit could be safely operated until an inspection of

the Unit 2 pressurizer could be conducted at the next forced or

scheduled outage.

Corrective actions to prevent recurrence of this deficiency included:

1) Perform a visual inspection of the Unit 2 pressurizer nozzles; 2)

Conduct a metallurgical examination of the nozzle removed from Unit 1:

and, 3) Report the results of the metallurgical examination and any

additional corrective actions in a supplement to this LER.

The

inspectors reviewed evidence of the completion of these corrective

actions. Inspection of the Unit 2 pressurizer nozzles determined that

there was no leakage. The results of the metallurgical examination were

issued and the supplement to this LER (i.e., LER 95007-01) was issued.

The LER supplement indicated that an additional inspection of the Unit 1

pressurizer nozzles would be necessary prior to the specification of any

further long term actions concerning this problem.

As a result of the

completion of corrective actions specified in LER 95007-00 the LER will

be closed, additional followup of the completion of corrective actions

for this issue will be accomplished by review of LER 95007-01.

The inspectors determined that the pressurizer nozzle leakage was in

violation of TS section 3.1.C.4, which prohibits continued operation

with a non-isolable RCS leak. This licensee identified violation is

being treated as a NCV, consistent with Section VII.~.l of the NRC

Enforcement Policy (NCV 50-280/96009-02) .

13

III. Engineering

El

Conduct of Engineering

El.1 Review of Deviation Reports

a.

Inspection Scope (37550)

The inspectors performed a review of DRs.

The purpose of the review was

to discern whether any adverse trends existed, whether the resolution of

problems was thorough and whether any violations of NRC requirements had

occurred with regard to the conduct of engineering. A secondary purpose

of the review was to form a basis for making a conclusion regarding the

effectiveness of the engineering organization. At the inspectors'

request. the licensee generated various summaries of DRs, which*gave a

succinct statement of the problem and corrective action. The summary

reports reviewed by the inspectors were sorted as follows:

All the DRs classified as "significant" by the licensee and

initiated since August 1994. There were eight in this sort. The

problems described in these DRs were operational or maintenance

type problems that did not have a direct bearing on the

performance of the engineering organization, therefore, none were

selected for further review.

All the DRs classified as "potentially significant" by the

licensee and assigned to engineering and initiated since October

1995.

In this sort, 29 were associated with Unit 1, 23 were

associated with Unit 2 and 7 applied to both units. After review

of the summary, seven were selected by the inspectors for further

review. These were DRs S-95-2442 and 2919; S-96-0064, 0798, 0850,

0851 and 1136.

All the DRs written against the top three systems from the risk

perspective since August 1995. These systems were Emergency

Electrical Power (including the EDGs). AFW, and Safety Injection.

There were 109 DRs written against Emergency Electrical Power, but

this did not represent all the DRs associated with electrical or

instrumentation and control equipment because DRs could also be

written against a mechanical system for that type problem.

Nine

DRs from the Emergency Electrical Power sort were chosen for

further review. These were: S-95-2705, S-96-0243, 0284, 0360,

0422, 0445, 0489, 1081 and 1445.

Review of these DRs led to

review of DR S-93-1383 having to do with a fault on a 34.5 kV

cable in the switchyard.

In addition, an ongoing investigation

concerning recent unusual indications of the DC ground detection

lamps in the main control room was evaluated by the inspectors .

The DRs for the Feedwater and AFW Systems could not be sorted separately

since both these systems were coded FW.

There were 89 DRs in this sort.

14

The sort for the Safety Injection System contained 83 DRs.

None of the

AFW or Safety Injection DRs received further review.

The inspectors

did, however, conclude that no adverse trends in these systems were

indicated by the DRs written against them.

Reviewing of a DR included review of relevant documents, questioning of

the cognizant engineer, and inspection of installed equipment to verify

corrective actions as deemed appropriate.

b. Observations and Findings

Through review of the selected DRs, the inspectors made the following

observations and findings:

Batteries The inspectors identified that there was a small amount of

corrosion on several terminals of the 125 VDC and 48 VDC batteries in

the 230 kV switchyard relay house. These batteries were non-safety-

related, however, they were important to safety, in that, they were

important to the reliability and functionality of the offsite power

system.

The licensee determined, after consultation with the

manufacturer, that the corrosion was nickel cobalt due to corrosion of

the stainless steel hardware; and white lead due to moisture and oil.

The inspectors met with the Superintendent of Substation Maintenance,

who stated that the corrosion would be cleaned off and lubricant as

recommended by the manufacturer would be applied to the terminals. This

work would take place no later than October 1996. This corrective

action was acceptable to the inspectors. The inspectors noted that

these batteries had recently passed the capacity tests which

demonstrated that the observed corrosion was not creating any high

resistance connections.

The inspectors did not observe any indicators of battery degradation

such as sedimentation, deformation, cracking, etc. The inspectors

inquired as to the age of the batteries. The licensee responded that

the date codes stamped on the posts indicated that the batteries had

been shipped in August 1969. This meant that the batteries were 27

years old. The licensee stated that the batteries were being subjected

to annual capacity tests as recommended in IEEE Standard 450,

Recommended Practice for Maintenance, Testing and Replacement of Large

Lead Storage Batteries for Generating Stations and Substations. The

licensee stated that the batteries were testing above 100 percent

capacity.

Circuit Breakers On February 4, 1996, there was a fault on the

transmission system near the plant. Immediately following the fault,

breakers for the service water pump (1-VS-P-1D) and the chilled water

pump (1-VS-P-2D) associated with chiller Din the mechanical equipment

room tripped. This resulted in shutdown of safety-related chiller D

(1-VS-E-4D).

On March 8, 1996, there was a fault on the 34.5 kV system

in the switchyard. The same breakers tripped and the chiller shutdown

as before. These two events were the subjects of DRs S-96-0243 and

0489. After the second occurrence, the licensee's investigation

e

15

determined the cause of the chiller shutdown to be wrong set points of

the molded-case magnetic-only circuit breakers protecting the circuits

for the pumps.

The breakers in question were in a motor control center which was

installed in 1993 as part of Design Change Package (DCP)90-008. This

plant modification installed several new safety-related chillers. The

new breakers were magnetic-only type in contrast to the thermal magnetic

type which were utilized in the rest of the motor control centers in the

plant. The magnetic-only type breakers have a fairly wide range of

adjustments from which the user can select to protect a given motor.

The DCP did not specify a set point for the breakers nor did it provide

specific guidelines for that purpose.

The set points were determined by

the test group as they performed the start-up tests on the breakers.

The test group did not contact the engineers responsible for the DCP to

obtain a set point, but rather used guidelines provided by the breaker

manufacturer.

The set points, as confirmed by the test data sheets, were approximately

ten times the motor full load amperes. These set points were too low in

that, they did not.take into account all the relevant design

considerations, and in effect were too sensitive. The short-circuits

described above were followed by voltage transients which caused the

motors in question to slow down to stall speed.

When the voltage

recovered, the motors drew full starting current which was above the set

point of the circuit breaker, and the breakers tripped.

With loss of

the auxiliary equipment, the chiller shutdown as designed.

The two breakers in question were reset according to the licensee's

design guides, STD-EEN-0011, Standard for Protective Device Settings.

The inspectors noted that the new set points were acceptable. The

licensee also initiated Engineering Commitment (EC) 96-44 to review the

set points of all the new magnetic-only circuit breakers (approximately

six additional breakers). This EC had a due date of October 15, 1996,

and the work had not been completed at the time of this inspection.

10 CFR 50, Appendix B, Criterion V. Instructions, Procedures and

Drawings, requires that activities affecting quality shall be prescribed

by documented instructions appropriate to the circumstances. The fact

that DCP 90-008 did not specify any set points for the breakers being

installed by the modification was in conflict with that requirement.

This deficiency resulted in the breakers being set at a too sensitive a

setting as evidenced by the fact that two breakers tripped during an

anticipated transient that should not have caused tripping of the

breakers. The safety significance of the wrong breaker set points was

that safety-related equipment could have spuriously de-energized due to

normal starting current during an accident or reactor event.

Additionally, this chiller provided cooling to the Emergency Switchgear

Room and Control Room.

These systems are identified in the top 10 list

of risk-significant systems for the plant. The licensee identified the

set point problem; however, the underlying problem that the set point

was not specified in the design package was not identified. The

16

corrective action of reviewing other similar applications was proceeding

slower than appropriate for the significance of the problem and work

involved (i.e., problem was identified in March 1996 and reviewing and

resetting of six breakers was scheduled to be completed in October

1996). The circumstances of the breaker set point problem constitute a

violation of 10 CFR 50, Appendix B, Criterion V, and will be identified

as Violation 50-280/96009-03, Design Change Package Failed to Specify

Breaker Set Point.

c. Conclusion

The inspectors did not identify any adverse trends during the review of

the licensee's DRs.

With one exception, corrective action associated

with the problems described in the DRs were thorough.

The corrosion on

the non-safety-related switchyard batteries identified by the inspectors

represented a maintenance item. and did not indicate any deficiency in

the conduct of engineering. A violation of NRC requirements was

identified for failure to provide adequate instructions for setting

safety-related molded case circuit breakers.

The inspectors concluded

that the engineering organization was effective in supporting plant

operations. This statement was based on the fact that 348 DRs were

reviewed and only one problem was identified. The violation involving

breaker set points did not change the overall positive conclusion.

El.2 High Head Safety Injection Electrical Logic

a.

Inspection Scope (37551)

A problem occurred recently at another utility which raised a concern

requiring investigation at Surry.

The problem at the other utility

involved the design of the electrical logic for the High Head Safety

Injection (HHSI) pumps, which allowed two of the three pumps to start

and run on the same degraded electrical bus.

Due to similarities

between the plant at the other utility and Surry, the Surry design was

reviewed.

b. Observations and Findings

Investigation of this issue determined that a similar problem (but not

the same problem) had been identified in NRC Violation 50-280, 281/

91024-02. This issue was closed in NRC Inspection Report NOs. 50-280,

281/93-13 based on additional administrative controls that corrected the

identified problem. Subsequently, the licensee installed a design

change (DCN 92-064-3) to permanently correct the HHSI pump electrical

logic. The inspectors reviewed the electrical logic in this design

change and the test procedure (2-FDTP-92-64-3-1, Charging Pump Logic

Modifications/Surry Units 1 and 2, revision 0) which verified the

operability of the new logic, and concluded that Surry's HHSI pump logic

would not allow two HHSI pumps to start and run on the same degraded

electrical bus.

17

c. Conclusions

Surry's HHSI pump electrical design will not permit two HHSI pumps to

start and run on the same degraded electrical bus.

El.3 Review of 10 CFR 50.59 Process

a.

Inspection Scope

The inspectors reviewed 12 change packages including DCPs, UFSAR change

packages (FSs), and Temporary Modification (TM) packages.

Most of the

documents were issued during the previous 12 months.

Five of the

documents (all DCPs) had been determined, through activity screening,

not to require a 10 CFR 50.59 evaluation.

The other seven included five

FSs, one DCP, and a TM.

The inspectors also reviewed the status of TMs.

b.

Observation and Findings

The inspectors confirmed that the five DCPs, which had not been

evaluated pursuant to 10 CFR 50.59, did not require a safety evaluation

according to 50.59. The activity screening criteria had been properly

evaluated .

The inspectors confirmed that adequate safety evaluations had been

performed for five FSs, a DCP, and a TM in accordance with 10 CFR 50.59.

The inspectors determined that several administrative errors had been

made in preparing the documents; however, these were of a minor nature.

Signoff/concurrence procedures were followed for all change packages.

The inspectors visited the control room and determined that procedures

for TMs were being followed.

Logs of TMs were present for both units as

required and appropriate signatures existed for current active TMs.

Only seven TMs were active, four on Unit 1 and three on Unit 2.

Records

indicated that the number of TMs for two units has been maintained at a

low level, fewer than ten, for several years through careful management

attention.

c. Conclusions:

The inspectors concluded that the five DCPs not evaluated pursuant to

10 CFR 50.59 did not require 10 CFR 50.59 safety evaluations and that

the activity screening criteria had been properly evaluated. It was

further concluded that through careful management attention, the number

of TMs for both units has been maintained at a low level (fewer than

ten) for several years.

" *

I I

18

E2

Engineering Support of Facilities and Equipment

E2.1 Engineering Support- Procurement Engineering

a.

Scope

The inspectors reviewed engineering activities related to procurement of

replacement equipment, materials, and parts. This included item

equivalency evaluations and dedication of commercial grade items for use

in safety related applications. A sample review consisted of 15

material upgrades and 15 item equivalency evaluations. The following

provided regulatory guidance for this inspection area:

Regulatory Guide 1.123, Quality Assurance (QA) Requirements for Control

of Items and Services for Nuclear Power Plants

ANSI N45.2.13-1976, QA Requirements for Control of Items and Services

for Nuclear Power Plants

NRC Generic Letter 91-05, Licensee Commercial Grade Procurement and

Dedication Programs.

b. Observations and Findings

Procurement Technical Evaluations (PTEs) demonstrated that critical

characteristics for material upgrades and item substitutions were

adequately identified and appropriate tests or inspections were

specified for quality verification.

PTEs included documentation of

appropriate 50.59 safety evaluation screening. Receipt inspection

reports documented the verification of the specified critical

characteristics. Vendor exceptions to purchase order requirements and

receipt inspection deficiencies were adequately resolved.

Equipment

requiring post installation testing for critical characteristics was

appropriately tagged.

The inspectors identified no occurrences in which

unqualified equipment or materials were installed in safety related

applications.

The inspectors noted that the licensee's self-assessment in the

engineering material upgrade process was limited to a minimal review in

a 1994 procurement audit. The licensee indicated that the scheduled

1996 procurement audit could include this activity.

c. Conclusions

The engineering process for material upgrade and item equivalency

evaluation adequately provided for installation of appropriate quality

level material in safety related applications .

. *

19

E3

Engineering Procedures and Documentation

E3.l Review of 10 CFR 50.59 Process

a.

Inspection Scope

The inspectors reviewed procedures governing the 50.59 process,

including those controlling DCPs, procedure changes, TMs, FSs, and

safety evaluations.

In addition the inspectors reviewed policy

documents (Nuclear Standards) on which the procedures were based.

b. Observation and Findings

The inspectors found the procedures governing the 50.59 process to be

comprehensive, thorough, and well written.

One procedure, VPAP-3001

(safety evaluations), had two features of particular interest.

VPAP-

3001 appeared to adopt the approach of NSAC-125 including one area where

the NRC staff has not yet accepted the approach.

Where a change in

probability is so small or the uncertainties in determining whether a

change in probability has occurred are such that it cannot be reasonably

concluded that the probability has actually changed, VPAP-3001 follows

NSAC-125 in stating that the change need not be considered an increase

in probability. The NRC staff is still considering the merits of that

approach and has not yet accepted it. In reviewing change packages

during the audit, the inspectors found no instance where this was an

issue. A second feature of interest is that "Safety Analysis Report" is

defined in VPAP-3001 as a broad spectrum of documents which includes

much more than the UFSAR.

It also includes the operating license, TS

and bases, technical requirements manual, emergency plan, quality

assurance program, offsite dose calculation manual, all correspondence

supporting submittals approved by NRC, NRC safety evaluations and

referenced correspondence, final environmental statement, and Appendix R

fire protection report. Thus, when the licensee applies 10 CFR 50.59 to

changes in the "Safety Analysis Report," it is a very conservative

application compared to that required by a literal reading of the

regulation.

c. Conclusions:

The inspectors concluded that the licensee 10 CFR 50.59 procedures were

comprehensive, thorough, and well written.

E3.2

UFSAR Update Process

a.

Scope

The inspectors discussed the approach to be taken by the licensee for

evaluating and updating the UFSAR at Surry.

,* *

20

b. Observations and Findings

In May 1996, the licensee formed a UFSAR project team for both Surry and

North Anna to examine the state of the UFSARs at both sites. The team

identified problems in the current UFSAR processes, content and usage.

The project team collected relevant data, identified problem areas. and

proposed corrective actions. The licensee developed long term

corrective actions to resolve many of the content and usage problems.

Included in the strategy of the plan.were several near-term actions to

assess current UFSAR quality and develop recommendations based on

assessment findings.

Recommendations in the process and user

improvement areas involved developing a UFSAR writers guide, simplify

administrative controls, electronic versions of the document, and

conduct awareness training.

The licensee stated that the Nuclear Energy Institute (NEI) approach

would be used to review the UFSAR.

An evaluation of four systems would

be performed, two safety related systems, and two non-safety related

systems.

At Surry these systems are safety injection, auxiliary

feedwater. component cooling water, and circulating water.

The

assessment at Surry will be completed by October 11, 1996, with the NEI

initiative due by June 1, 1997.

Conclusions

The licensee formed a UFSAR project team to examine the state of the

UFSAR.

The NEI approach would be used to review the UFSAR.

E4

Engineering Staff Knowledge and Performance

E4.1 Engineering Self Assessment Program

a.

Scope

A review of the licensee's engineering self assessment program was

conducted by the inspectors to see if strengths and weaknesses were

identified and if corrective actions were initiated for the weaknesses.

b. Observations and Findings

The inspectors reviewed procedure SSES-1.3, Controlling Procedure for

Engineering Self Assessment, revision 0, dated May 1, 1996.

The

licensee had completed one self assessment project and has five more in

progress. The inspectors reviewed parts of the following self

assessments.

ENG-SA-96-001, Plan of the Day Effectiveness (Involves engineering

support to other site organizations)

ENG-SA-96-002, Procedural Compliance

J

21

ENG-SA-96-003, UFSAR Update Process.

The first self assessment resulted in improvement in the engineering

internal and external communications process. Part of this assessment

was a survey of engineering's customers (planning, maintenance,

electrical. scheduling, and Nuclear Site Services) in order to evaluate

the customers perception of the engineering group's response to requests

for support emanating from the Plan of the Day meetings.

Eighteen

people representing a cross section of personnel requesting engineering

support in their daily tasks rated the engineering support as very good.

c. Conclusions

The new self assessment process was still in its early stages of

development and it was too early to form an analysis of the licensee's

efforts.

E5

Engineering Staff Training and Qualification

E5.1 Review of 10 CFR 50.59 Process

a.

Inspection Scope

The inspectors reviewed training records for staff who had

completed training in the requirements and procedures for

10 CFR 50.59 evaluations.

b. Observation and Findings

The inspectors determined that 10 CFR 50.59 training is required

by the licensee to be current for all staff who perform or review

safety evaluations. About 200 staff have received the training.

Annual requalification is required with a 3-month grace period.

Although SNSOC members/alternates and offsite Management Safety

Review Committee (MSRC) members are not required to take the

training, most of the SNSOC members/alternates had taken the

training and maintained it current. Only one MSRC member had

current training.

c. Conclusions:

The inspectors concluded that 10 CFR 50.59 training was maintained

current for all personnel who performed and provided 10 CFR 50.59

safety evaluations.

E5.2 Engineering Manager Training

a.

Scope

A review was made of some of the training being conducted for the

engineering managers at the Surry site.

22

b. Observations and Findings

The inspectors discussed the leadership development/awareness training

for the engineering supervisors.

In particular. the review of issues,

processes, and process revisions conducted during the supervision staff

meetings was examined.

Some of the topics discussed during these

meetings were:

plant safety analysis, the maintenance rule, 10 CFR

50.59 safety analysis standard, outage safety assessment, discrepancy

trend report, UFSAR update of self assessment, operator workarounds,

hurricane response plan, NRC Bulletin 96-01 summary results, vibration

monitoring, and other. These topics have been covered over a seven

month period at Surry. The awareness training conducted for the

engineering supervision staff was considered a positive finding.

c. Conclusions

Manager training on a wide variety of subjects was being used to enhance

the engineering supervision in making more informed decisions and was

identified as a positive finding.

E7

Quality Assurance in Engineering Activities

E7.1 Design Control Program Audit

a.

Scope

The inspectors reviewed part of an audit (part identified for Surry and

corporate engineering) covering the design control program.

b. Observations and Findings

The inspectors reviewed the results of Audit Number 96-04, Design

Control and Engineering Programs, conducted during March and April 1996,

at Surry, North Anna, and at corporate Engineering. The audit reviewed

controls for plant design and modifications, engineering programs for

scaling, set points, seismic qualifications, design basis documents,

software control, and potential problem plant controls.

Findings were identified with multiple examples. Several of the

findings identified a number of procedural compliance, quality, and

human performance deficiencies within the Engineering organization.

Some corrective actions such as reinstruction of individuals, procedure

improvements, calculation revisions, design change package revisions,

lessons learned memorandums, etc., have been taken or were in progress.

Longer term corrective actions were being undertaken by the Engineering

Redesign Project Team.

One of the goals of this team was to improve

design quality and conform_ance.

23

c. Conclusions

The Design Control and Engineering Program audit was thorough, detailed

and resulted in meaningful findings. The high quality of this audit was

identified as a positive finding.

IV. Plant Support

Sl

Conduct of Security and Safeguards Activities (71750)

On several occasions during the inspection period. the inspectors

performed walkdowns of the protected area perimeter to assess security

and general barrier conditions.

No deficiencies were noted, and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained.

Rl

Radiological Protection and Chemistry (RP&C) Controls (71750)

On several occasions during the inspection period, the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit, survey results, and radiological area material

conditions.

No discrepancies were noted, and the inspectors concluded

that RP practices were proper.

RS

Miscellaneous Radiation Protection and Chemistry Issues

R8.l Potentially Contaminated Construction Materials (71750)

On July 26, another nuclear power facility found that a shipment of 1/4

inch steel plate construction material was contaminated. The source and

batch number of the contaminated steel was identified.

VEPCO was one of

several utilities who received material from this same batch. The

inspectors discussed the issue with the Superintendent RP to determine

whether Surry Station had received contaminated steel from the suspect

batch. Fifteen steel plate sheets from the suspect batch were received

at North Anna Power Station. Licensee personnel initiated action to

account for the steel plating usage and final location. Material

records indicated that Surry Station did not receive material from the

suspect batch. The inspectors determined that licensee response to the

potentially contaminated steel issue was appropriate.

V. Management Meetings

Xl

Exit Meeting SUD1Dary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on September 12 and 23 and

October 7.

The licensee acknowledged the findings presented.

24

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified .

,. *

25

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Blount, Maintenance Superintendent

D. Christian, Station Manager

M. Crist, Operations Superintendent

J. McCarthy, Assistant Station Manager, Operations & Maintenance

R. Saunders, Vice President, Nuclear Operations

8. Shriver, Assistant Station Manager, Nuclear Safety and Licensing

T. Sowers, Engineering Superintendent

8. Stanley, Director Nuclear Oversight

J. Swientoniewski, Supervisor, Station Nuclear Safety

W. Thorton, Superintendent, Radiological Protection

IP 37550:

IP 37551:

IP 37700:

IP 40500:

IP 61726:

IP 62703:

IP 71707:

IP 71750:

IP 90712:

IP 92700:

IP 92902:

IP 92901:

26

INSPECTION PROCEDURES USED

Engineering

Onsite Engineering

Design Changes, and Modifications

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

Surveillance Observation

Maintenance Observation

Plant Operations

Plant Support Activities

Inoffice Review of Written Reports of Nonroutine Events at Power

Reactor Facilities

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

Followup - Engineering

Followup - Plant Operations

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-281/96009-01

NCV

failure to maintain Unit 2 control room

logs in the form required by procedures

(Section 01.5)

50-280/96009-02

50-280/96009-03

Closed

50-280, 281/94-173 01014

50-280/94008-01

50-280/94008-02

NCV

operation with non-isolable leak in

pressurizer instrumentation nozzles

(Section M8.8)

VIO

design change package failed to specify

breaker set point (Section E.1.b)

VIO

failure to identify and promptly correct

conditions adverse to quality (Section

M8.l)

LER

entry into TS 4.0.3 for failure to test

new charcoal in accordance with TS 4.12.B.7(b) and a missed TS surveillance

(Section M8.2)

LER

entry into TS 4.0.3 for failure to test

new charcoal in accordance with TS 4.12.B.7(b) and a missed TS surveillance

(Section M8.2)

r-----------------------------------------* -

27

50-281/94001

LER

both AVEF trains inoperable (Section M8.3)

50-281/94004

LER

station battery 2A inoperable longer than

allowed due to personnel error (Section

M8.4)

50-280/96001-01

LER

station and EOG battery connections not

coated with anti-corrosion material due to

procedural error (Section M8.5)

50-280, 281/96002-03

DEV

deviation from commitment to reduce

probability of core damage from flooding

(Section M8.6)

50-280, 281/96002-04

URI

review preventive maintenance program

deferral pProcess (Section M8.7)

50-280/95007-00

LER

operation with non-isolable leak in

pressurizer instrumentation nozzles

(Section M8.8)

50-281/96009-01

NCV

failure to maintain Unit 2 control room

logs in the form required by procedures

(Section 01.5)

50-280/96009-02

NCV

operation with non-isolable leak in

pressurizer instrumentation nozzles

(Section M8.8)

Discussed

50-280/95007-01

LER

operation with non-isolable leak in

pressurizer instrumentation nozzles

(Section M8.8)