ML18152B324

From kanterella
Jump to navigation Jump to search
Forwards Insp Repts 50-280/88-32 & 50-281/88-32 on 880912-16,26-30 & 1114-18.Violations Noted:Svc Water Sys Would Not Have Met Safety Design Objectives W/O Relying on nonsafety-grade Equipment.Executive Summary Encl
ML18152B324
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/15/1988
From: Ernst M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
Shared Package
ML18151A513 List:
References
GL-83-28, NUDOCS 8812220021
Download: ML18152B324 (4)


See also: IR 05000280/1988032

Text

<.

  • e

Docket Nos. 50-280, 50-281

License Nos. DPR-32, DPR-37

/Virginia Electric and Power Company

~ ATTN:

Mr. W. R. Cartwright

Vice President

Nuclear Operations

5000 Dominion Boulevard

Glen Allen, VA

23060

Gent1emen:

e

December 1,5, 1.988

SUBJECT:

NRC INSPECTION REPORT NOS. 50-280/88-32 AND 50-281/88-32

()-ff: c iq_ I

This refers to the Nuclear Regulatory Commission (NRC) inspection conducted by

G. A. Belisle on September 12 - 16, September 26 - 30, and November 14 -18,

1988.

The inspection included a review of activities authorized at your Surry

facility.

At the conclusion of the inspection, the findings were discussed

with those members of your staff identified in the enclosed inspection report.

A Confirmation of Action Letter was also sent to you on November 2, 1988.

Areas examined during the inspection are identified in the report.

Within

these areas, the inspection consisted of selecti~e examination of procedures

and representative records, interviews with personnel, and observation of

activities in progress.

The inspection findings indicate that certain activities appeared to violate

NRC requirement? .in that the service water systems would not have met their

safety design objectives without relying on nonsafety-grade equipment.

The

apparent violations described in the enclosed inspection report are under

consideration for escalated enforcement action.

Accordingly, no Notice of

Violation is being issued at this time, and no response to this letter is

required for these apparent violations.

However, please be advised that the

number and characterization of apparent violations described in the enclosed

Inspection Report may change as a result of further NRC review.

An Enforcement

Conference to discuss these apparent. violations will be scheduled in the near

future.

You will be advised by separate correspondence of the results of our

deliberations on this matter.

However, you have agreed to resolve these issues

prior to restart of either unit.

The inspection findings also indicate that certain activities appear to deviate

from your commitments to NRC Generic Letter 83-28, Required Actions Based on

Generic Implications of Salem ATWS Events, issued on July 8, 1983, and your

Updated Final Safety Analysis Report commitment to IEEE-279, Standard Nuclear

Power Plant Protection Systems, dated August 1968.

No Notice of Deviation is

being issued at this time, and no response to this letter is required for these

apparent deviations.

You will be advised by separate correspondence of the

results of our deliberation on this matter.

8812220021 881215

PDR

ADOCK 05000280

G

PNV

'

(I

e

Virginia Electric and Power Company

2

December 15, 1988

Your attention is

inspection report.

invited to the unresolved items identified in this

These matters will be pursued during future inspections.

In accordance with Section 2.790 of the NRC's "Rules of Practice," Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its

enclosures will be placed in the NRC Public Document Room.

The responses directed by this 1 etter and its enclosures are not subject to

the clearance procedures of the Office of Management and Budget as pequirea by

the Paperwork Reduction Act of 1980, Pub. L. No.96-511.

Should you have any questions concerning this letter, please contact us.

Enclosures:

1.

Executive Summary

2.

NRC Inspection Report

cc w/encls:

M. Kansler, Station Manager

,1L E. Hardwick, Manager:... Nuclear

Programs and Licensing

Commonwealth of Virginia

bee w/encls:

vNRC Resident Inspector

DRS Technical Assistant

Document Control Desk

1/f ! '

RI I

, .

)

£\\ieL

Mell en: btm

L)_t!)

ABe }i .sl e

111 l'-f /88

RI!

BWifs:ft-

ll// j/88

11/ :t./88

! '

RI~~

LReyes

111,s 88

R~

CJ~ , an

11/ /88

/1- IS

Sincerely,

(Original si.gned by M. L.. Ernst)

Malcolm L. Ernst

Acting Regional Administrator

RI~A

RII ?,., 4

.

~L-

AG~so~

FCantrell

1~ /88

I 1s

U.l/)/88

r pi,.1/1

RI!

1 ~r

RII

0 ti

,....-------)

PStohr

~*

11/ /88

...----41/ /88

\\ 1., I I ,.__

\\_

e

ENCLOSURE 1

Executive Summary

An announced Safety System Functional Inspection on the Service Water (SW),

Recirculation Spray (RS), and associated electrical systems was conducted on

September 12-16, 26-30, and November 14-18, 1988.

The inspected activities

included design control, operations, maintenance, surveillance, and qua1ity

assurance/quality control. The inspection objective was to assure that these

systems would perform their safety function as required by the design basis of

the plant.

The SW systems for Surry Units 1 and 2 were designed to remove sufficient decay

heat from these plants to prevent fuel damage following coincident Loss of

Coolant and .Loss of Offsite Power accidents.

This design objective could not

have

been

met

during

previous Surry operations without relying

on

nonsafety-grade equipment.

The Surry upper intake canal provides the only source of service water for the

station. This upper intake canal (reservoir) is separated from the James River

by an earth dam.

The canal is filled by circulating water pumps during normal

operation and by emergency service water pumps when offsite power is lost. The

upper intake canal water level is higher than the river level. The inspection

revealed that the upper intake canal could be siphoned back to the river

through idle circulating water pumps following loss of offsite power if

non safety-grade siphon breakers on the pump discharge piping failed.

Water

would also drain from the upper intake canal by gravity flow if nonsafety-grade

canal level instrumentation failed to close main condenser isolation valves.

The rate of loss of water from the upper intake canal under either circumstance

could far exceed the makeup capacity of the emergency service water pumps

resulting in l-0sing the service water supply to both units.

Service water is

essential for decay heat removal following a design basis accident.*

Other significant findings concerning service water operability included the

questionable reliability and capacity for the emergency service water pumps.

The inspection identified that the emergency service water pumps could not

meet the design basis flow requirements.

There was extensive fouling of the

service water heat exchangers and upstream piping.

Therefore plant operation

was conducted since plant startup with canal level too low to provide suffi-

cient service water inventory to support the design basis.

Some of the factors contributing to these deficiencies included the following:

Inappropriate assumptions in the original plant design were not questioned

by the licensee.

Failure to properly maintain the plant .

Inadequate surveillance testing to ensure continued operability.

e

Executive Summary

2

Failure to maintain appropriate design basis documentation.

Failure to take adequate corrective action on upper intake canal l~vel

issue (i.e., errors in the justification for continued operation when

first identified by the licensee).

Inaccurate plant drawings.

Inadequate quality assurance (i.e., the licensee did not identify tf\\ese

problems sooner).

Both units were shut down (Unit 2 was in an outage and Unit 1 was

resolve diesel load sequencing problems) during the inspection.

agreed to resolve all issues regarding operability of the service

prior to restarting either unit .

shut down to

The licensee

water system