Similar Documents at Surry |
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NflC Form 366 (9-83)
FACILITY l'IAME (1)
Surry Power Station, Unit 2 POW 28~06-01-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3160-0104 El<PIRES: 0/31/llS DOCKET NUMBER (2)
PAGE (3) o I s I o I o I o I 21 a I 1 1 I oi=
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- TITLE (1)
Lifting of Power Operated Relief Valve Due To Procedural Inadequacy
!:Vi:i'IT,>A Tf. (6)
LER NUr,113ER (6)
Rtl:PORT DATE (7)
OTHER FACILITl!:S INVOLVED (8)
YEAR FACILITY NAMES DOCKET NUMBER(S) q,*E:l/'ITiNG THIS Rf:PORT IS 1.!U!IMITTED PURSUANT TO THE R!:QUIREMENTS OF 10 Cf'R §: (Ch<ck on* or moro of th* follo>ying) (11)
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N 20.402(b) 20.tl05(c) tii0.38(e)(1)
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S0.73(o)(2)(M 00.73(al<2)M 73.71(b) 73.71 (c)
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OTHER (Spsclfy in Abstr*ct bolow ond in T*xt. NRC Form 366A) 60.73(0)(2)(11) 00.73(a)(2)(vlli)(B) 11Special Report" 60.73(o)(2)(11i)
S0.73(o)(2)(x)
LICENSEE CONTACT FOR THIS LEA (12)
NAME TELEPHONE NUMBER AREA COOE D. L Benson, Station Manager 8 I O I 4 31 5 I 71 -I ~ I 1 IR I U CAUSE SYSTEM COMPONENT I
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COMPLETE ONE LINE FOR EACH COMPONENT C'AILURE DESCRIBED IN THIS REl'ORT (13)
MANUFAC*
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I SUPPLEMENTAL REPORT EXPECTED (14)
MONTH DAY YEAR EXPECTED SUBMISSION n YES /If v*s. complot* EXPECTED SUBMISSION DATE) ha NO OATE (15)
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.MlSTRACT./Limit to 1400 spscas, i.e.* opproximot*ly fiftsen singl*-spsce typewritten lin*sl (16)
On May 28, 1988 at 0228 hours0.00264 days <br />0.0633 hours <br />3.769841e-4 weeks <br />8.6754e-5 months <br />, with Unit 2 in cold shutdown, a Reactor Coolant System (RCS) {EIIS-AB} Power Operated Relief Valve (PORV), PCV-2455C {EIIS-PCV} cycled open and then closed.
At the time of the event, RCS venting and filling was in progress and a Reactor Coolant Pump (RCP) {EIIS-P} had just been started" The pressure transient, caused by the start of the RCP with a solid water plant condition, created a pressure rise and lifted the PORV which was set to open at 375 psig.
The PORV immediately closed and the RCS pressure stabilized at approximately 340 psig.
This event is reportable pursuant to Technical Specification (T.S.) 3.1.G.3 and 6.6.C.
The cause of the event was failure to revise the RCS venting procedure when the PORV lift setpoints were reduced.
The administrative procedure which provides the instructions for processing setpoint change requests requires that documents affected by the setpoint change be reviewed.
However, there was no mechanism to ensure that these documents were revised.
The operating procedures for both units are being revised to reduce the required RCS pressure band for operating a RCP when venting the RCSo The administrative procedure will be revised to provide a mechanism to ensure that documents affected by the setpoint change will be revised in a timely manner.
8807010450 880627 PDR ADOC~ 05000281 S
DCD NRC Form 366 (9-83)
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NRC fol'/ll 3SIIA (IJ.83) l't\\C.ll17Y NAME (1) i DOCKET NUMIJER (2)
POW 28~06=01-01 U.S. lllUC!.EAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31/68 LER NUMBER (6)
PAC,E (3)
- SEQUENTIAL
- ::::::::: REVISION Y~AR NUMBER
- '.:::::::: NUMBER Surry Power Station, Unit 2 o I 5 Io Io I O I 21 a I 1 s I $t -
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'NRC FORM 366A CS-831 1.0 Descri_Etion of the Event On May 28v 1988 at 0228 hour0.00264 days <br />0.0633 hours <br />3.769841e-4 weeks <br />8.6754e-5 months <br />su with Unit 2 in cold shutdown, a Reactor Coolant System (RCS) {EIIS=AB}
Power Operated Relief Valve (PORV), PCV-2455C
{EIIS-PCV} cycled open and then closedo At the time of the eventu RCS venting and filling was in progress and a Reactor Coolant Pump (RCP) {EIIS=P} had just been started.
The pressure transient, caused by the start of the RCP with a solid water plant conditionr created a pressure rise and lifted the PORV which was set to open at 375 psigo The PORV irrunediately closed and the RCS pressure stabilized at approximately 340 psigo This event is reportable pursuant to Technical Specification (T.S.) 3.1.G.3 and 6.6oC.
2.0 Safety Conseguences and Implications The operability of two PORVs or the RCS vented through an opened PORV ensures that the reactor vessel will be protected from pressure transients which could exceed the limits of Appendix G of 10CFR Part 50, when the RCS temperature is less than or equal to 350 degrees Fahrenheit and the reactor vessel head is bolted.
During the event, PCV-2455C performed as required to maintain RCS pressure within T.S. limits.
Therefore 1 the health and safety of the public were not affected.
3.0
Cause
The cause of the event was failure to revise the RCS venting procedure when the PORV lift setpoints were reduced.
The setpoints were changed in April, 1988 following an analysis from the reactor vessel material surveillance program, which revised the heatup and cooldown curves currently in Technical Specifications.
The administrative procedure which provides the instructions for processing setpoint change requests requires that documents affected by the setpoint change be reviewed.
However, there was no mechanism to ensure that these documents were revised.
- U.S.GP0.19B6-0-624-538/455
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.i::'UW NRC Fol'l'I> 366A (9-831 LICENSEE EV-W!EPORT (LER) TEXT CONTiNUATle U.S. NUCLEAR REGULATORY COMMISSION APPROV!:D 0MB NO. 3150....0104 EXPIRES: 0/31 /88 DOCKET NUMBER (2)
LER NUMBER (6)
- -:*:*:*:*: SEQUENTIAL *:*:*:*:*:* REVISION NUMBER
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Immediate Corrective Action(s)
The PORV was verified shut and RCS pressure was verified below the PORV setpointo 5.0 Additional Corrective Action(s) 6.0 7.0 8.0 The PORV setpoint was verified to be 375 psig.
The PORV was cycled open and closed to verify operabilit*y.
Action(s) Taken to Prevent Recurrence The operating procedures for both units are being revised to reduce the required RCS pressure band for operating a RCP when venting the RCS.
This will increase the available pressure operating band prior to reaching the PORV setpointso The administrative procedure will be revised to provide a mechanism to ensure that documents affected by the setpoint change will be revised in a timely manner.
Similar Events
None.
Manufacturer/Model Number N/A
- U.S.GP0.1966*0*624 538/455
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June 27s, 1988 U.S. N~clear Regulatory Commission Documa~t Control Desk 016 Phillips Building Washington, D.C.
20555 Gentlemen:
Vl~Gll\\llA ~l.!fC'filllC ANO POWER COMPANY
$yrrv i'@'Mlr auitlon
,. o. 13<>!! :mi l;hm1f, '\\.?lr@JRIO ~ml
Docket No.:
Licensee No.:
88-030 50-281 DPR-37 Pursuant to Surry Power Station Technical Specifications 9 Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 2.
REPORT NUMBER 88-014-00 This report bas been reviewed by the Station Nuclear Safety and Operating Cotmnittee and will be reviewed by Safety Evaluation and Control.
Very truly yours, David L. Benson Station Manager Enclosure cc: Dr. J. Nelson Grace Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta 9 Georgia 30323
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| 05000281/LER-1988-001, :on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys |
- on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys
| | | 05000281/LER-1988-001-02, :on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted |
- on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted
| | | 05000280/LER-1988-001-01, :on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position |
- on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position
| | | 05000281/LER-1988-002, :on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced |
- on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced
| | | 05000281/LER-1988-002-02, :on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results |
- on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results
| | | 05000280/LER-1988-002-01, :on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr |
- on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr
| 10 CFR 50.73(a)(2)(iii) | | 05000281/LER-1988-003-01, :on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings |
- on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings
| | | 05000280/LER-1988-003-02, :on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions |
- on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions
| | | 05000281/LER-1988-004, :on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced |
- on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced
| | | 05000280/LER-1988-004, :on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci |
- on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci
| | | 05000280/LER-1988-005-01, :on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated |
- on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated
| | | 05000281/LER-1988-005-02, :on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction |
- on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction
| | | 05000280/LER-1988-006-01, :on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc |
- on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc
| | | 05000281/LER-1988-006-02, :on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced |
- on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced
| | | 05000281/LER-1988-007-02, :on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached |
- on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached
| | | 05000280/LER-1988-007-01, :on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow |
- on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow
| | | 05000280/LER-1988-008-01, :on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily |
- on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily
| | | 05000281/LER-1988-008-02, :on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised |
- on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised
| 10 CFR 50.73(o)(2)(ii) | | 05000280/LER-1988-009-01, :on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core |
- on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core
| | | 05000281/LER-1988-009-02, :on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made |
- on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000281/LER-1988-010-02, :on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup |
- on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup
| | | 05000280/LER-1988-010-01, :on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted |
- on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted
| 10 CFR 50.73(a)(2) | | 05000281/LER-1988-010-03, :on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup |
- on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup
| | | 05000280/LER-1988-011, :on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued |
- on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000280/LER-1988-011-01, :on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions |
- on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(v) 10 CFR 50.73(o)(2)(i) | | 05000281/LER-1988-011-02, :on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced |
- on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced
| | | 05000280/LER-1988-012-01, :on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled |
- on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled
| | | 05000281/LER-1988-012-02, :on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes |
- on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes
| 10 CFR 50.73(o)(2)(iv) | | 05000281/LER-1988-013-01, :on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures |
- on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures
| | | 05000280/LER-1988-013-02, :on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown |
- on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000280/LER-1988-014-01, :on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break |
- on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break
| | | 05000281/LER-1988-014-02, :on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised |
- on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised
| 10 CFR 50.73(o)(2)(vii) | | 05000281/LER-1988-015-02, :on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily |
- on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily
| 10 CFR 50.73(a)(2)(i) | | 05000280/LER-1988-015-01, :on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies |
- on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies
| | | 05000281/LER-1988-016-02, :on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted |
- on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted
| | | 05000280/LER-1988-016-01, :on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted |
- on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted
| 10 CFR 50.73(a)(2)(i) | | 05000281/LER-1988-017-02, :on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable |
- on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable
| | | 05000280/LER-1988-017-01, :on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented |
- on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000280/LER-1988-017, :on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed |
- on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed
| | | 05000281/LER-1988-018-02, :on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode |
- on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode
| | | 05000280/LER-1988-019-01, :on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers |
- on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers
| | | 05000281/LER-1988-019-03, :on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified |
- on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified
| | | 05000280/LER-1988-020, :on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented |
- on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented
| | | 05000281/LER-1988-020-01, :on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted |
- on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted
| | | 05000281/LER-1988-021-01, :on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered |
- on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered
| | | 05000280/LER-1988-021, :on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed |
- on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed
| | | 05000280/LER-1988-022, :on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced |
- on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced
| | | 05000281/LER-1988-022-01, :on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed |
- on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed
| | | 05000280/LER-1988-023, :on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode |
- on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode
| | | 05000281/LER-1988-023-02, :on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened |
- on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened
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