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~. NRC Form 366 19-83)
FACILITY NAME 11)
LICENSEE EVENT REPORT (LERI POW 28-06-01-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB. NO. 3150-0104 EXPIRES: 8/31/88 I
PAGE 131 SURRY*POWER STATION, UNIT 2 I
DOCKET NUMBER 12) o I 5 I o I o I o I 2 18 11 1!0F 013 TITLE 141 Inoperable Individual Rod Position Indicators Due to Instrument Drift EVENT DATE 15)
LEA NUMBER 16)
REPORT DATE 17)
OTHER FACILITIES INVOLVED 18)
MONTH DAY YEAR YEAR 1:::::::,:: SEQUENTIAL :/::::: REVISION MONTH DAY i:::::::::;:
NUMBER
- NUMBER YEAR FACILITY NAMES DOCKET NUMBERISI o Is 11 7 s s s ls -
o 11 I 2 -
o Io o I 6 1 16 s Is OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more of the folloY(ing) (11)
MODE (9) 20.402(b)*
20,4051c)
r---....... -+---1 50.36lcll11 LEVEL 73.711b) 73.71(c)
POWER I 20.406lall1Jlil (10) -
0 IO p 20.40s1a11111;;1 Iii llllllll111lillllll =
- ~::: ::::
X 50,36(c)(21 50,73loll2lli) 50.73(o)(2)(iv) 60.73loll2!M 60.731a112llvii) 50,73(o)l2llvlii)(Al 60.731all2)(viii)(BI 60.731oll2Hxl OTHER (Spocify in Abstroct bslow snd in Text, NRC Form 366A}
50.73loll2llii) 50.73lall2)(iiil LICENSEE CONTACT FOR THIS LEA (12)
NAME TELEPHONE NUMBER AREA CODE I
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COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113)
CAUSE
SYSTEM COMPONENT MANUFAC*
TURER MANUFAC-TURER I*:*::.:.. :.*
X AIA Z II I I
MI 01315 1*.*:.:.* *.-:
I N
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I I I I I I I
I I I I I I I SUPPLEMENT~L REPORT EXPECTED 1141 EXPECTED MONTH DAY YEAR SUBMISSION bl NO n YES (If yes, complete EXPECTED SUBMISSION DATE/
DATE 115)
I I
I ABSTRACT (Umit to 1400 spaces, i.e., spproximstsly t;freen single-sf)Bce typewritten lines} 116)
NRC Form 366 On May 17,
- 1988, Unit 2
was at intermediate shutdown and proceeding to cold shutdown as required by Technical Specifications (T.S.)
due to reduced auxiliary feedwater flow following a reactor trip on May 16, 1988.
At 0557 hours0.00645 days <br />0.155 hours <br />9.209656e-4 weeks <br />2.119385e-4 months <br /> on May 17,
- 1988, the Individual Rod Position Indicators (IRPis)
[EIIS-ZI] for four rods in shutdown bank "B" differed from the rod group demand counter by greater than 12 steps.
This is contrary to T.S. 3.12.
The IRPis were adjusted at
- 0631, but during the continued cooldown, six IRPis for shutdown bank "A" drifted out of the 12 step band at 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />.
The IRPis were not able to_ be calibrated, and the unit was placed in cold shutdown at 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on May 18, 1988.
Incorrect rod position indication due to Reactor Coolant System (RCS)
[EIIS-AB]
temperature changes is known to be a
generic Westinghouse PWR concern.
A T.S. change is being prepared which will ~ccommodate the effects of RCS temperature on the rod position.indicators.
A setpoint change was made which lowered the P-250 process computer rod deviation alarm to alert the operator when the rods are 10 steps out of alignment to preclude exceeding the *T.S. limit of 12 steps.
The IRPis will be calibrated prior to unit criticality.
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19*831
-- ---(9-831 FACILITY NAME (1)
LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER (21 POW 28-06-01-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: B/31 /88 LEA NUMBER (6)
PAGE (3)
SURRY POWER STATION, UNIT 2 0 15 1°1°1°121811 818 -ol1 l2 -
ol c 012 °Fo 13 TEXT /ff more space is rr,quired, us,, addition*! NRC Form 3S6A's/ 1171 19-831 1.0 Description of the Event On May 17,
- 1988, Unit 2 was at intermediate shutdown and proceeding to cold shutdown as required by Technical Specifications (T.S.)
due to reduced auxiliary feedwater flow following a reactor trip on May 16, 1988.
At 0557 hours0.00645 days <br />0.155 hours <br />9.209656e-4 weeks <br />2.119385e-4 months <br /> on May 17,
- 1988, the Individual Rod Position Indicators (IRPis) [EIIS-ZI] for four rods in shutdown bank 11B 11 differed from the rod group demand counter by greater than 12 steps.
This is contrary to T.S. 3.12.
The IRPis were adjusted at 0631, but during the continued cooldown, six IRPis for shutdown bank 11A 11 drifted out of the 12 step band at 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />.
The IRPis were not able to be calibrated, and the unit was placed in cold shutdown at 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on May 18, 1988.
2.0
Safety Consequences and Implications
The IRPis provide control rod position indication in the main control room.
The control rod demand counters, which indicate control rod position as demanded by the Rod Control System [EIIS-AA],
remained operable during the time the IRPis were not operable.
Only the shutdown banks were withdravm during this event.
Inoperable IRPis will not affect the operation of the control rod assemblies, and all rods were capable of being inserted into the core if required.
Therefore, the h~altp and safety of the public were not affected.
3.0
Cause
Incorrect rod position indication due to Reactor Coolant System (RCS) [EIIS-AB] temperature changes is known to be a
generic Westinghouse PWR concern.
The decision was made to continue the plant cooldown to place the unit in the T.S.
required condition.
4.0 Immediate Corrective Action(s)
At 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on May 18, 1988, cold shutdown was achieved.
A work request was submitted to calibrate the IRPis. (9-83)
FACILITY NAME (11 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER (2)
POW 28-06-01-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: B/31 /88 LER NUMBER (6)
PAGE (JI SURRY POWER STATION, UNIT 2 01s10101012l8ll 818 -01112 -010 Ol3 OF Ol3 TEXT /If moro space is mquil'9d, USIJ odditionol NRC Form 366A's/ (171 5.0 Additional Corrective Action{s)
A Technical Specification change is being prepared which will accommodate the effects of RCS temperature on the rod position indicators.
A setpoint change was made which lowered the P-250 process computer rod deviation alarm to alert the operator when the rods are 10 steps out of alignment to preclude exceeding the Technical Specification limit of 12 steps.
The IRPis will be calibrated prior to unit criticality.
6.0 Action(s) Taken to Prevent Recurrence is approved, the the step demand changes below Until the Technical Specification change IRPis will be adjusted to agree with counters as required during RCS temperature hot shutdown.
7.0
Similar Events
Ul LERs:
88-010,88-006, 88-002,86-021, 85-019.
U2 LERs:
88-007,88-003, 86-019,85-009.
8.0 Manufacturer/Model Number Magnetics Inc./Project #K9391, K9392.
e June 16, 1988 U.S. Nuclear Regulatory Commission Document Control Desk 016 Phillips Building Washington, D.C.
20555 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY Surry POW9r Station P.O. lox 315 Surry, Virginia 23883 Serial No.:
Docket No.:
Licensee No.:
88-027 50-281 DPR-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 2.
REPORT NUMBER 88-012-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control.
Very truly yours*,
~
l--t'7"l
..!)OJl./lQ. "'--.j E:/)"W..C?<...
David L. Benson Station Manager Enclosure cc:
Dr. J. Nelson Grace Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323
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| 05000281/LER-1988-001, :on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys |
- on 880127,discovered That Leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Greater than ASME Section XI Spec.On 880202,wrong Leads Lifted for Trip Valves.Caused by Impurities in Sys
| | | 05000281/LER-1988-001-02, :on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted |
- on 880127,leakage Through Containment Isolation Valves TV-SS-201A & TV-SS-201B Discovered Greater than ASME Section XI Spec.Valves Declared Inoperable.Caused by Misinterpretation of Sketches.Leads Lifted
| | | 05000280/LER-1988-001-01, :on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position |
- on 880131,containment Isolation Valve Not Properly Locked Under Administrative Control.Cause Undetermined.Valve Verified to Be in Closed Position
| | | 05000281/LER-1988-002, :on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced |
- on 880202,determined That Individual Valve Leakage Through Reactor Coolant Cold Leg Sample Isolation Valves Was Greater than ASME Section XI Spec.Caused by Impurities in Sys.Valves Replaced
| | | 05000281/LER-1988-002-02, :on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results |
- on 880202,containment Isolation Valves Declared Inoperable Due to Leakage in Excess of Spec Value. Cause Not Determined.Valves Will Be Replaced/Repaired Based Upon Failure Analysis Results
| | | 05000280/LER-1988-002-01, :on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr |
- on 880206,individual Rod Position Indicators Declared Inoperable Following Turbine Stop Valve/Governor Valve Freedom Test.Caused by Instrument Drift.Indicators Recalibr
| 10 CFR 50.73(a)(2)(iii) | | 05000281/LER-1988-003-01, :on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings |
- on 880220,individual Rod Position Indicators Differed from Demand Counter by Greater than 12 Steps. Caused by Generic Westinghouse PWR Concern.Indicators Calibr to Give Correct Readings
| | | 05000280/LER-1988-003-02, :on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions |
- on 880216,reactor Trip Occurred Due to Power Range Lo Setpoint Hi Flux & Intermediate Range Hi Flux Trip Signals.Caused by Personnel Error.Peer Group Reviewed Event & Switches Returned to Correct Positions
| | | 05000281/LER-1988-004, :on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced |
- on 880327,turbine Runback Automatically Initiated Due to Loss of Power to Power Range Nuclear Instrument NI-43.Caused by Internal Conductor Failure Due to Age.Vital Bus Inverters Replaced
| | | 05000280/LER-1988-004, :on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci |
- on 880216,reactor Coolant Dose Exceeded Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core. Level of dose-equivalent I-131 Monitored at Least Every 4 H Until Level Returned to Less than 1 Mci
| | | 05000280/LER-1988-005-01, :on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated |
- on 880219,heat Tracing Proper Control Setpoints Could Not Be Verified.Caused by Inadequate Surveillance & Maint Procedures.Verification of Correct Setpoints Initiated
| | | 05000281/LER-1988-005-02, :on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction |
- on 880305,control Rod Urgent Failure Alarm Received in Control Room.Caused by Failed Phase Control Card in 1BD Power Cabinet.Control Room Operator Placed Rod in Manual Per Abnormal Procedure for Malfunction
| | | 05000280/LER-1988-006-01, :on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc |
- on 880219,individual Rod Position Indicators Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Generic Westinghouse PWR Concern.Rods Calibr to Give Correct Indication & Returned to Svc
| | | 05000281/LER-1988-006-02, :on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced |
- on 880310,fire Detection Circuit for Facility Containment & Emergency Switchgear Instrument Rack Room Rendered Inoperable.Caused by Failure of Remote Control Module EIIS-IC Imod.Failed Module Replaced
| | | 05000281/LER-1988-007-02, :on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached |
- on 880405,individual Rod Position Indicators Declared Inoperable Due to Instrument Drift.Setpoint Change Evaluated to Lower Rod Deviation Alarm to Warn Operator Before Deviation Reached
| | | 05000280/LER-1988-007-01, :on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow |
- on 880224,control/relay Room Chiller Tripped. Caused by Insufficient Svc Water Flow.Throttled Svc Water Valves Fully Opened & Correct Outlet Valve Throttled to Obtain Proper Svc Water Flow
| | | 05000280/LER-1988-008-01, :on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily |
- on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested Satisfactorily
| | | 05000281/LER-1988-008-02, :on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised |
- on 880505,reactor Operator Discovered That No Boric Acid Flowpath Existed from Boric Acid Storage Tanks to Charging Pumps.Caused by Personnel Error & Procedural Inadequacy.Procedures Will Be Revised
| 10 CFR 50.73(o)(2)(ii) | | 05000280/LER-1988-009-01, :on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core |
- on 880311,specific Activity Sample of Reactor Coolant Showed dose-equivalent I-131 Level of 1.5 Uci Which Exceed Tech Spec Limit.Caused by Fuel Element Defect in Reactor Core
| | | 05000281/LER-1988-009-02, :on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made |
- on 880420,component Cooling Water HXs Declared Inoperable.Caused by Vacuum Priming Lines Up to Isolation Valves Not Being Seismically Supported.Engineering Work Request to Install Seismic Supports Made
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000281/LER-1988-010-02, :on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup |
- on 880516,reactor Trip Occurred as Result of Steam Generator lo-lo Level.Caused by Rapid Closure of Turbine Governor Valves.Recorder Will Be Used to Monitor Electrohydraulic Control Sys During Startup
| | | 05000280/LER-1988-010-01, :on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted |
- on 880409,individual Rod Position Indicators (Irpis) Inoperable.Caused by Incorrect Rod Position Indication Due to Primary Coolant Temp Changes.Work Request to Calibr Irpis Submitted
| 10 CFR 50.73(a)(2) | | 05000281/LER-1988-010-03, :on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup |
- on 880516,reactor Trip Occurred Due to lo-lo Steam Generator Level.Caused by Rapid Closure of Turbine Governor Valves.Turbine Impulse Pressure Transmitter Calibr. Further Monitoring Performed During Startup
| | | 05000280/LER-1988-011, :on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued |
- on 880415,PORVs PCV-1455C & PCV-1456 Failed to Manually Open When Selector Switches Placed in Open Position from Auto Position.Caused by Procedural Inadequacy. Valve Actuator Bolts & Screws Torqued
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000280/LER-1988-011-01, :on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions |
- on 880415,power-operated Relief Valves Failed to Manually Open When Selector Switches Placed in Open Position.Cause Under Investigation.Selector Switches,Air Supply & Valves Examined for Malfunctions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(o)(2) 10 CFR 50.73(o)(2)(v) 10 CFR 50.73(o)(2)(i) | | 05000281/LER-1988-011-02, :on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced |
- on 880423,control Room/Relay Room Chiller Removed from Svc After Second Chiller Removed from Svc. Caused by Fouled Chiller Refrigerant filter-dryer Elements. Filter-dryer Elements Replaced
| | | 05000280/LER-1988-012-01, :on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled |
- on 880418,Tech Spec 1.0.H.5 Violated.Caused by Discovery of Valve 1-RS-11 Held in Open Position by Counter Weight Due to Personnel Error.Valves Inspected & Verified to Be in Closed Position & 1-RS-11 Disassembled
| | | 05000281/LER-1988-012-02, :on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes |
- on 880517,individual Rod Position Indicators for Four Rods in Shutdown Bank B Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Incorrect Rod Position Indication Due to RCS Changes
| 10 CFR 50.73(o)(2)(iv) | | 05000281/LER-1988-013-01, :on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures |
- on 880523,reactor Trip Breakers Automatically Opened in Response to Reactor Trip Signal Generated on Low Steam Generator Water Level.Caused by Inadequate Procedure. Personnel Reinstructed on Deviating Procedures
| | | 05000280/LER-1988-013-02, :on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown |
- on 880523,emergency Diesel Generator 3 Automatically Started.Caused by Performing Multiple Procedures W/O Adequate Review of Individual Procedures. Testing Suspended & Diesel Shutdown
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | | 05000280/LER-1988-014-01, :on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break |
- on 870630,determined That Unique Scenario Could Exist Whereby Auxiliary Feedwater Could Be Lost to Operating Unit.Administrative Controls Established & Safety Analysis Reviewed for high-energy Line Break
| | | 05000281/LER-1988-014-02, :on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised |
- on 880528,RCS PORV PCV-2455C Cycled Open & Closed,Simultaneous W/Rcs Venting & Filling.Caused by Failure to Revise RCS Venting Procedure.Operating Procedures Revised
| 10 CFR 50.73(o)(2)(vii) | | 05000281/LER-1988-015-02, :on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily |
- on 880626,rod Urgent Failure Annunciator Activated in Control Room.Caused by Failed Circuit Card & Blown Fuse.Failed Circuit Card & Blown Fuse Replaced & Rod Control Sys Tested Satisfactorily
| 10 CFR 50.73(a)(2)(i) | | 05000280/LER-1988-015-01, :on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies |
- on 880523,emergency Bus Transformer Cooling Fans Powered from nonsafety-related Power Supply.Caused by Design Deficiency.Power Sources Relocated to Diesel Generator Backed Supplies
| | | 05000281/LER-1988-016-02, :on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted |
- on 880731,discovered That Individual Rod Position Indicators (Irpis) Differed from Group Step Demand Counter by Greater than 12 Steps.Caused by Drift in Irpi Indication.Irpis Adjusted
| | | 05000280/LER-1988-016-01, :on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted |
- on 880510,pressurizer Safety Valve Setpoints Found Outside of Allowable Limits During Refueling Surveillance Testing.Possibly Caused by Setpoint Drift. Valves Refurbished & Lift Setpoints Adjusted
| 10 CFR 50.73(a)(2)(i) | | 05000281/LER-1988-017-02, :on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable |
- on 880730,failure of Recirculation Spray Svc Water MOVs Due to Premature Actuation of Torque Switch. Both Valves Declared Inoperable & Tech Spec 3.0.1 Entered on Basis That Both Subsystems Were Inoperable
| | | 05000280/LER-1988-017-01, :on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented |
- on 880606,discovered Debris in Temporary Discharge Cone Strainer & Recirculation Spray Sump Pumps. Caused by Inadequate Insp Program.Containment Sump & Pump Screen Surveillance Will Be Implemented
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000280/LER-1988-017, :on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed |
- on 880606,foreign Matl Found in Temporary Discharge Cone Strainer & Deficiencies Found in Sump Screens.Caused by Inadequate Insp Program During Const Activities.Foreign Objects Removed
| | | 05000281/LER-1988-018-02, :on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode |
- on 880811,steam Generator B Channel III Steam Flow Failed to High Flow Indication.Failed Multiplier/ Divider Replaced.Affected Channels Placed in Trip Mode
| | | 05000280/LER-1988-019-01, :on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers |
- on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing Jumpers
| | | 05000281/LER-1988-019-03, :on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified |
- on 880901,steam Generator a Inside Containment Steam Valve Closed for No Apparent Reason Due to Actuation of High Flow Trip Solenoid.Solenoid Reset,Blowdown Flow Established & Trip Valve & Solenoid Verified
| | | 05000280/LER-1988-020, :on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented |
- on 880628,control/relay Room Chiller Condenser Svc Water (SW) Pumps & Unit 2 Charging Pump SW Pumps Lost Suction.Caused by Inadequate Procedure.Filling of SW Supply Line Secured & Supply Header Vented
| | | 05000281/LER-1988-020-01, :on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted |
- on 880909,individual Rod Position Indicators for Four Control Rods of Control Bank D Differed from Demand Counter by More than 12 Steps.Caused by Indicator Indication Drift.Indicators Adjusted
| | | 05000281/LER-1988-021-01, :on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered |
- on 880908,required Test Frequency for B Low Head Safety Injection Pump Exceeded.Caused by Inability of Operator to Obtain Required Vibration Test W/Test Equipment Used.Formal Training of Equipment Administered
| | | 05000280/LER-1988-021, :on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed |
- on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed
| | | 05000280/LER-1988-022, :on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced |
- on 880710,unit Ramped Down to Shutdown.Caused by MOV-CS-101B Leakage Due to Lost Motion in Shaft & Linkage Between Motor Operator & Shaft.Valve Disassembled & Valve Seat & O-rings Replaced
| | | 05000281/LER-1988-022-01, :on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed |
- on 880910,reactor Trip by Turbine Trip Occurred While Attempting to Maintain Turbine at Synchronous Speed.Caused by Inadequate Procedure & Faulty Valve Position Indication.Testing to Be Performed
| | | 05000280/LER-1988-023, :on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode |
- on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip Mode
| | | 05000281/LER-1988-023-02, :on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened |
- on 881006,three Containment Trip Valves Found Closed & Radiation Monitor Sample Pump & Particulate Monitor Discovered Stopped Due to Trip Valve Interlock.Caused by Personnel Error.Trip Valves Opened
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