ML18152A546

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Insp Repts 50-280/95-07 & 50-281/95-07 on 950402-29.No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Engineering Insps, Plant Support & Licensee Event Rept follow-up
ML18152A546
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/24/1995
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A547 List:
References
50-280-95-07, 50-280-95-7, 50-281-95-07, 50-281-95-7, NUDOCS 9506200154
Download: ML18152A546 (12)


See also: IR 05000280/1995007

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/95-07 and 50-281/95-07

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

April 2 through 29, 1995

Lead Inspector:

Inspectors:

Approved by:

~ft./~

W. Branch, Senior Resident Inspector

D. M. Kern, Resident Inspector

G. A. Harris, Resident Inspector

~~nChief

Reactor Projects Section 2A

Division of Reactor Projects

SUMMARY

Scope:

s;=-.2,~9:r-

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, engineering

inspections, plant support, and Licensee Event Report follow-up.

Inspections

of backshift activities were conducted on April 19, 21, and 26.

Results:

Operations

The Unit 2 Safety Injection system configuration was properly controlled and

material condition was good (paragraph 3.2).

Overtime controls, including monitoring for indicators of fatigue, were

effective during the Unit 2 refueling outage (paragraph 3.3) .

9506200154 950524

PDR

ADOCK 05000280

G

PDR

2

Conservative decision making was noted when Unit 1 was manually tripped to

ensure plant conditions were boundJwhen problems were encountered after a

control rod dropped into the core (paragraph 3.1).

Maintenance

Material condition of the Spent Fuel Pool Cooling System did not meet the

plant's normal high standards (paragraph 3.4).

Engineering

A weakness was noted in procedure 1-0PT-RX-004, Reactor Power Calorimetric

Using Feed Flow With P-250 Out of Service (Manual), (paragraph 5.1).

Plant Support

Confined space entry (CSE) training was comprehensive and appropriate to

support personnel safety at the station. Personnel demonstrated sound

knowledge of CSE requirements and atmosphere test equipment (paragraph 6.2) .

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

  • W. Benthall, Supervisor, Licensing
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

D. Erickson, Superintendent of Radiation Protection

  • B. Garber, Licensing

B. Hayes, Supervisor, Quality Assurance

D. Hayes, Supervisor of Administrative Services

  • D. Llewellyn, Superintendent, Nuclear Training

C. Luffman, Superintendent, Security

  • R. MacManus, Supervisor, System Engineering
  • J. McCarthy, Assistant Station Manager
  • A. Price, Assistant Station Manager
  • S. Sarver, Superintendent of Operations

R. Saunders, Vice President, Nuclear Operations

K. Sloane, Superintendent of Outage and Planning

  • E. Smith, Site Quality Assurance Manager

T. Sowers, Superintendent of Engineering

  • B. Stanley, Supervisor, Station Procedures

J. Swientoniewski, Supervisor, Station Nuclear Safety

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector

D. Kern, Resident Inspector

G. Harris, Resident Inspector

  • Attended Exit Interview

Acronyms used throughout this report are listed in the last paragraph.

Plant Status

Unit 1 began the inspection period at 100% power.

On April 12, control

rod J-7 dropped to the fully inserted position, causing a turbine

runback.

Operators stabilized the unit at 74% power.

A CRDM cable

failure precluded operators from recovering control rod J-7 to the

desired group position.

The fully inserted control rod resulted in a

higher axial flux difference than was permitted for power operations

above 50%.

Operators reduced reactor power to 45% and manually tripped

the reactor (paragraph 3.1).

2

Unit 1 was restarted and placed on-line on April 16 following CROM

System repairs. Operators observed an unexpected steam.flow imbalance

between SGs as the reactor approached full power.

The B SG was

producing about 200,000 pounds mass/hour less steam flow than either the

A or C SGs.

Initial licensee evaluation concluded that the reactor trip

had removed an oxide layer from the B SG U-Tube region which resulted in

a temporary reduction of heat transfer capability. Operators stabilized

reactor power at 98.5% to reduce the magnitude of the steam flow

imbalance.

Unit 1 remained at 98.5 % power through the end of the

inspection period.

Unit 2 operated at 100% power throughout the entire inspection period.

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

50.72 Report

At 5:56 pm, on April 12, Unit 1 was manually tripped from 45

percent reactor power.

All control rods inserted into the core as

designed.

Auxiliary feedwater automatically initiated as designed

on low-low steam generator level following the trip.

No primary

safety or power operated relief valves were actuated during the

event.

No secondary safety relief valves actuated; however, the A

main steam power operated relief valve was actuated briefly at the

start of the transient. It subsequently closed and reseated. All

electrical buses transferred properly following the trip and all

emergency diesel generators were operable.

The manual reactor trip was well coordinated and demonstrated

conservative decision making.

There were no Technical

Specification or procedural requirements to shutdown the unit.

Plant maintenance and engineering personnel had determined that a

high probability existed for dropping additional control rods if

an orderly shutdown was attempted.

Troubleshooting was being

performed as a result of a dropped control rod, which occurred

earlier that day at approximately 8:20 am.

At 9:20 pm the licensee informed the NRC via the Emergency

Notification System of the event.

The inspectors determined that

the event was properly reported as required.

. .

3

3.2

SI System Lineup Verification

3.3

The inspectors reviewed the material conditions and positions of

approximately 70 SI system valves within the Unit 2 Safeguards

Building to verify that the SI system was correctly configured to

perform the LHSI safety function.

The general material condition

of the system was good.

Minor discrepancies including packing

leaks, a missing label, and a degraded position indicator were

discussed with the Supervisor of Shift Operations and appropriate

corrective actions were initiated. All SI system valves inspected

were found properly positioned in accordance with procedure

2-0P-SI-OOlA, SI System Alignment, revision 2.

The current

position of SI system valves was properly documented in the system

lineup library maintained by the Operations Department.

The

inspectors concluded that the Unit 2 SI system configuration was

properly controlled and maintained.

Personnel Overtime Controls During Outage

VPAP-0103, Working Hours and Limitations, rev1s1on 2, establishes

policy to control overtime work.

The inspectors reviewed

VPAP-0103, timekeeping records, interviewed personnel, and

observed outage work activities to determine whether overtime

controls were effectively implemented .

VPAP-0103 clearly defined administrative overtime limits for

personnel who perform safety-related functions.

These limits and

approval authority were consistent with NRC GL 82-12, Nuclear

Power Plant Staff Working Hours.

The inspectors reviewed overtime

records for the February-March, 1995 period.

With limited

exceptions, workers requested and received Station Manager's

approval prior to exceeding station administrative overtime

limits.

The Administrative Services department reported

authorized and unauthorized overtime usage (above the

administrative limits) to the station manager on a weekly basis.

When appropriate, station DRs were initiated to resolve

discrepancies regarding pre-authorization to exceed administrative

overtime limits. The inspectors determined that overtime controls

were implemented consistent with VPAP-0103.

The inspectors observed that, on several occasions, a single

request to exceed overtime limits for selected activities was

written for an entire department (i.e., electrical maintenance -

60 people, mechanical maintenance - 90 people).

However, only

approximately 10 to 15% of those persons authorized under the

blanket overtime authorization actually exceeded the guidance.

The inspectors questioned whether the program continued to

preclude excessive worker fatigue when blanket overtime

authorization of this scale was granted.

The inspectors discussed

this concern with the Station Manager who noted that several

actions to prevent worker fatigue and monitor for fatigue were

effective during the outage.

These included rescheduling of work

. .

~~

-

-~---

4

to maintain crew continuity, frequent in-plant observation tours

by management, human factors assessment of DRs and job rework, and

QA oversight.

In addition, workers received behavioral

observation training annually.

The inspectors independently

interviewed workers during the outage and attended daily work

progress meetings.

Workers did not appear to be adversely

affected, physically or mentally, due to working overtime.

The

quality of work performed was not negatively impacted by use of

overtime.

The inspectors concluded that licensee overtime

controls, including continued monitoring for indicators of

fatigue, satisfied the intent of NRC GL 82-12.

3.4

Spent Fuel Pool Cooling and Purification System Walkdown

On April 11 and 12, the inspectors performed a valve alignment

verification and an evaluation of the material condition of the

spent fuel cooling pumps, skimmer, and purification system

components.

The inspectors noted that the material condition of

these components, while generally adequate, was not in keeping

with that in the rest of the station. Discrepancies noted

included the following:

Several pressure gage isolation valves were found to be out

of their specified full open position.

For example, the

spent fuel cooling pump A suction pressure gage isolation

valve, l-FC-6 was found nearly closed causing the gage to

read abnormally low.

In another example, spent fuel cooling

pump B discharge pressure gage isolation valve, l-FC-10, was

found throttled. These isolation valves we~e for gages that

provided local indication only ..

Both inboard and outboard mechanical seals for the IA and 18

spent fuel cooling pumps appeared to have been leaking as

evidenced by the accumulation of a considerable amount of

boron.

The oil bubbler for the 18 spent fuel cooling pump was

observed to be abnormally low for a period of two days while

the pump was in service. Oil was added to the pump on the

third day.

The coatings for both the IA and 18 spent fuel cooling water

pumps and their base plates were significantly degraded.

Spent fuel pool cooling heat exchanger component cooling

water pressure gage, l-CC-PI-1018, read offscale high.

The local power control hand switches for the IA spent fuel

cooling water pump was not labelled in accordance with

station standards. This was the only example of a labeling

problem identified.


-


---- ---- -- ----- ---- -

5

Both the 3A and 3B purification pumps had extensive rust on

the base plates and their coatings were degraded.

Both the 2A and 2B skimmer pumps had oil and water

accumulation on their base plates resulting in an

undesirable radioactive mixed waste.

The inspectors concluded that despite the noted discrepancies the

spent fuel cooling water pump, skimmer and purification pumps were

operable. These discrepancies were discussed with station

management for investigation and correction as necessary.

Within the areas inspected, no violations or deviations were identified.

4.

Maintenance Inspections (62703)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

4.1

Battery Status Update

In October 1994, the 2A station battery became inoperable due

to a degraded cell as documented in NRC Inspection Report Nos.

50-280/94-32 and 50-281/94-32.

NRC and licensee follow-up

identified several programmatic weaknesses which resulted in

failure to recognize battery degradation in a timely manner.

Station management subsequently issued a management expectation

policy statement which directed that *a station DR be written each

time a battery cell is found in the Alert performance range. This

action was taken to ensure that indications of battery degradation

were raised to management's attention before a battery became

inoperable.

The licensee also initiated a RCE to assess battery

performance throughout the station. The inspectors reviewed

battery maintenance activities to determine whether the policy

statement had been implemented in an effective manner.

The number of DRs pertaining to the IA and 2A station batteries

dramatically increased since October 1994. -in addition, the

number of DRs reported pertaining to the EDG, TSC, Black, and

security inverter batteries also increased as the policy statement

was implemented.

Prior to October, very few battery problems were

documented.

The inspectors observed that improved documentation

of marginal battery performance has been beneficial in

highlighting continuing problems with the station batteries for

management, driving corrective actions to be taken, and in

increased maintenance support.

In December 1994, six IA station battery cells were replaced.

The

replacement cells were spares obtained from another facility. The

replacement cells had been in service for approximately two years

at the other facility, and then stored for approximately three

6

years. Several ,of the replacement cells exhibited marginal

performance following installation, warranting increased

attention.

Two cells were replaced a second time prior to reactor

startup in December 1994.

In March 1995, eighteen 2A station

battery cells were replaced. This included replacement of the

cell which had caused the battery to be inoperable in October

1994.

The jumper which had temporarily bypassed the inoperable

cell was removed and the 2A station battery was restored to its

design condition. Several additional maintenance activities have

been completed in the past six months to improve the condition of

the EDG, TSC, Black, and security inverter batteries.

Marginal cell voltage and non-uniform specific gravities were

observed following cell replacements on IA and 2A station

batteries. These conditions persisted despite repeated battery

equalization charges.

System engineers determined that low

equalization charge voltage was a major contributor to these

problems.

It was not possible to increase the equalization charge

voltage further for these batteries due to DC bus voltage

limitations. This limited the amount of battery improvement that

can be gained from a charge.

The RCE team discussed this

situation with the vendor and continued to evaluate alternate

solutions to improve the condition of the station batteries.

The licensee RCE team determined that following the IA and 2A cell

replacements, station battery performance was acceptable.

However, there were RCE recommendations that addressed IA cell

replacement during the Fall 1995 Unit 1 RFO and possible station

battery replacement at a later date.

The RCE team also examined

the appropriateness of post maintenance test selection for cell

replacements following problems encountered on the IA replacement.

The inspectors reviewed the licensee RCE for station battery

problems and determined that it was thorough.

The increase in DRs

associated with battery problems indicated increased sensitivity

to early problem identification and resolution.

The licensee's

lower threshold for problem identification as outlined in the

October 1994 management policy statement has been effective in

early identification of equipment degradation. Additionally, as

outlined in the licensee RCE, even though the batteries remain

operable, further maintenance actions and possible battery

replacement are necessary to restore the material condition of

some of the more degraded batteries.

Within the areas inspected, no violations or deviations were identified.

5.

Engineering Inspections (37551)

During the reporting period, the inspectors reviewed engineering

activities to assure compliance with the appropriate procedure and TS

requirements.

7

5.1

Review of Reactor Power Calorimetric Manual Method

During a walkdown of the Unit 1 mechanical equipment room the

inspectors observed that one of the local feedwater temperature

indicators was missing. This instrument had been removed to allow

installation of the downstream RTD into the piping thermowell.

The thermowell for the RTD had developed a leak and had been

plugged.

The feedwater RTD provides input to the P-250 computer

for temperature information used in the computerized calorimetric

calibration of Nis.

The P-250 computer used for calorimetric calibration of the Nis

was out of service and the licensee was planning to perform a

manual calorimetric if the computer could not be returned to

service in time.

The computer was returned to service and the

computerized calorimetric was completed on time.

The inspectors reviewed procedure l-OPT-RX-004, Reactor Power

Calorimetric Using Feed Flow With P-250 Out of Service {Manual),

revision 1.

This was the procedure that the licensee would have

used to perform the calorimetric_if the computer was not

available.

The inspectors noted that the procedure required the

use of the local temperature instruments to measure feedwater

temperature.

As noted previously, one of the referenced

temperature instruments was removed and would not have been

available if needed.

The three local feedwater temperature

instruments were designated l-FW-TI-154-A, 8, and C.

These local

temperature instruments were made by Ashcroft with a span of

200 - 700 °F with 5 degree graduations on the gage face.

Given

the needed precision of the calorimetric, the inspectors reviewed

the assumed accuracy in the licensee's calculational basis for NI

setting and adjustment.

Calorimetric assumptions and calculations were contained in

"Phase 2 Results of Nuclear Unit Efficiency Study for Surry Unit 1

{VEPCO Contract No. FHN-074-0219) April 25, 1984.

11

This study

defined the assumed feedwater temperature error as the sum of

instrument specified tolerances+ instrument drift+ readout

error. The total feedwater temperature error assumed was 1.75 °F.

The inspectors reviewed licensee's vendor information on the

Ash~roft local temperature instruments to determine specified

accuracy. Additionally, I&C calibration data was reviewed to

determine calibration accuracy.

The vendor manual specifies and the licensee's lab calibrates

these type instruments to an accuracy of+/- 1% of full scale

{1% of 500 degrees or 5 °F).

The licensee's field calibration

specifies a+/- 2% full scale accuracy {2% of 500 degrees or

10 °F).

Neither of these values were within the values assumed in

the calorimetric calculation. It should be noted that, the

calorimetric formula applies instrument uncertainty in a

statistical manner.

Therefore, the increased feedwater

8

temperature error impact on the assumed calorimetric uncertainty

is unclear but believed to be slight.

The inspectors also reviewed previous calibration records for one

of the three local feedwater temperature instruments.

The

inspectors selected 1-FW-TI-154A for review.

The licensee's

records indicated that this instrument was last calibrated on

May 4, 1990, by WO 094487.

Additionally, the inspectors noted

that the local feedwater temperature instruments were not in the

periodic calibration program.

The inspectors held discussions

with reactor engineering personnel and questioned the

acceptability of using non-calibrated gages with accuracies

outside those assumed in the calculation for performing

calorimetric calibrations.

The licensee is currently performing a

review to determine the potential impact on calorimetric

uncertainties and management has placed a hold on the use of

procedures 1 & 2-0PT-RX-004.

The inspectors did not identify

cases where this procedure had been recently used to provide

values for adjustment of Nis.

The inspectors considered this

issue to be a weakness in the licensee's program and will continue

to follow the licensee's actions.

Within the areas inspected, no violations or deviations were identified.

6.

Plant Support (71707, 71750)

The inspectors conducted facility tours, work activity observations,

personnel interviews, and documentation reviews to determine whether

programs were effectively implemented to comply with regulatory

requirements in the areas of radiological protection and security.

6.1

Plant Tour Observations

The inspectors observed radiological control practices and

radiological conditions throughout the plant.

Portal and hand-

held monitors were observed to be in good condition and within

proper calibration periodicities. Radiological posting and

control of contaminated areas were good.

The licensee continued

decontamination efforts to manage the amount of contaminated floor

area to a minimum.

The inspectors observed good worker practices

regarding radwaste minimization and tool issue from the

contaminated tool locker.

Selected aspects of plant physical security were reviewed during

regular and backshift hours to verify controls were in accordance

with the security plan and implementing procedures.

This review

included security measures, vital and protected area barrier

integrity, maintenance of isolation zones, personnel access

control, searches of personnel, packages and vehicles, and

escorting of visitors.

No discrepancies were noted.

"

(I

'

..

9

6.2

Confined Space Entry Training

Certain portions of the station have been identified as confined

spaces, for which personnel require specialized training prior to

access.

The training and requirements of VPAP-1901, Industrial

Safety and Health, revision 4, were established for personnel

safety. The primary hazards of concern are flammable gas, toxic

fumes, and an oxygen deficient or enriched atmosphere.

The

inspectors attended confined space entry training prior to

inspecting LHSI components in the valve pit level of the Unit 1

and Unit 2 Safeguards Buildings.

The instructor was knowledgeable

and the training material was comprehensive.

RP personnel

demonstrated sound knowledge of confined space entry requirements

and atmosphere test equipment usage when accompanying the

inspectors to the valve pits. The inspectors concluded that the

level of training was appropriate to support personnel safety

during confined space entries.

Within the areas inspected, no violations or devi~tions were identified.

7.

Licensee Event Report Follow-up (92700)

The inspectors reviewed LERs to verify accuracy, description of cause,

previous similar occurrences, and effectiveness of corrective actions.

The inspectors considered the need for further information, possible

generic implications, and whether the events warranted further on-site

follow-up.

The LERs were also reviewed with respect to the requirements

of 10 CFR 50.73 and the guidance provided in NUREG 1022, Licensee Event

Report System, and its associated supplements.

(Closed) LER 50-281/93-03, Unit 2 Automatic Reactor Trip Due to Low

Steam Generator Water Level Coincident with Steam/Feedwater Flow

Mismatch Resulting from Spurious Closure of "A" MFRV.

The LER describes

the August 3, 1993 Unit 2 reactor trip. Safety systems responded as

designed and the event did not pose a threat to public health and

safety.

The trip resulted from a sudden and unanticipated loss of FW

flow to the A SG.

The licensee determined that a 15 vdc MFRV controller

power supply failed, causing the A MFRV to fail closed.

The event,

causal analysis, and corrective actions were previously documented in

NRC Inspection Report Nos. 50-280/93-20 and 50-281/93-20.

The

inspectors reviewed the resultant RCE and confirmed that corrective

recommendations had been implemented.

The LER was accurate and met the

requirements of 10 CFR 50.73.

Within the areas inspected, no violations or deviations were identified.

8.

Exit Interview

The inspection scope and findings were summarized on May 5, 1995, with

those persons indicated in paragraph I. The inspectors described the

. .

10

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

Item Number

LER 50-281/93-03

Status

Closed

Description/(Paraqraph No.)

Unit 2 Automatic Reactor Trip

Due to Low Steam Generator

Water Level Coincident with

Steam/Feedwater Flow Mismatch

Resulting from Spurious

Closure of "A" MFRV

(paragraph 7).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

9.

Index of Acronyms and Initialisms

CFR

CODE OF FEDERAL REGULATIONS

CROM

CONTROL ROD DRIVE MECHANISM

CSE

CONFINED SPACE ENTRY

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

EOG

EMERGENCY DIESEL GENERATOR

FW

FEEDWATER

GL

GENERIC LETTER

LER

LICENSEE EVENT REPORT

LHSI

LOW HEAD SAFETY INJECTION

MFRV

MAIN FEEDWATER REGULATING VALVE

NI

NUCLEAR INSTRUMENT

NRC

NUCLEAR REGULATORY COMMISSION

QA

QUALITY ASSURANCE

RCE

ROOT CAUSE EVALUATION

RP

RADIOLOGICAL PROTECTION

RTD

RESISTANT TEMPERATURE DETECTOR

SG

STEAM GENERATOR

SI

SAFETY INJECTION

TS

TECHNICAL SPECIFICATION

TSC

TECHNICAL SUPPORT CENTER

voe

VOLT DIRECT CURRENT

VPAP

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WO

WORK ORDER

~F

DEGREES FAHRENHEIT