ML18152A536

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Resident Insp Repts 50-280/93-07 & 50-281/93-07 on 930307- 0403.Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint Insps,Surveillance Insps & Safety Assessment & Quality Verification
ML18152A536
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/19/1993
From: Belisle G, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A537 List:
References
50-280-93-07, 50-280-93-7, 50-281-93-07, 50-281-93-7, NUDOCS 9305030376
Download: ML18152A536 (12)


See also: IR 05000280/1993007

Text

Report Nos.:

50-280/93-07 and 50-281/93-07

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

March 7 through April 3, 1993.

Inspectors:

Approved by:

Z.2§ W

J. ~~ing Senior Resident

Inspector

S. G. ~Mesidhspector

G. A. Belisle, Se<rti-On Chief

Division of Reactor Projects

SUMMARY

Scope:

~/9- Y3

Date Signed

f-19'--Y:>

Date Signed

'Wrlrs

Date Sifgned

This routine resident inspection was conducted on site in the area of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, safety assessment and quality verification, action on previous

inspection items, and licensee event review.

During the performance of this

inspection, the resident inspectors conducted review of the licensee's

backshifts, holiday or weekend operations on March 7, 13, 18, 21, 23, 26, 28,

31, and April 1, 2, and 3.

Results:

In the operations area, the following items were noted:

A strength was identified relating to the sensitivity of a reactor

operator's observation that a fire watch had certain conditions that may

have prevented the performance of the assigned functions (paragraph

3. a).

9305030376 930419

PDR

ADOC~ 05000280

G

PDR

2

The evolutions associated with defueling unit 2 were well organized and

efficiently accomplished (paragraph 3.b).

A review determined that when the containment air recirculation system

is shut down, the radiation monitors for the system are inoperable

during refueling operations. A non-cited violation was identified for

this discrepancy (paragraph 8).

In the maintenance/surveillance functional area, the following items were

noted:

During the installation of a code repair on a service water line,

quality assurance's coaching of the craft indicated that the craft was

not adequately prepared to do the job. This is considered to be a

weakness.

(paragraph 4.c).

Non-intrusive testing of accumulator discharge check valves to verify

full stroke was an improvement over the previous test method that

required the check valves to be periodically disassembled, inspected and

reassembled.

This new method of testing also resulted in a reduction in

radiation exposure (paragraph 5.a).

In the engineering/technical support area, the following item was noted:

An unresolved item was identified in the area of evaluation for open

issues identified during implementation of the design basis

documEntation program (paragraph 3.c).

In the safety assessment/quality verification area, the following items were

noted:

The corrective actions implemented to verify proper operation of steam

traps in the steam supply lines to the turbine driven auxiliary feed

pump to preclude further failures were adequate (paragraph 4.b).

The methodologies approach for assessing station performance was an

innovative method for performing audits.

The methodologies audits

performed on the Maintenance Department indicated that the performance

of the maintenance department is slowly improving (paragraph 6.b).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • R. Allen, Supervisor, Operations
  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • H. Blake, Superintendent of Site Services

M. Bowling, Manager, Corporate Nuclear Licensing

  • R. Blount, Superintendent of Engineering

D. Christian, Assistant Station Manager

  • J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

B. Foster, Supervisor, Station Engineering

  • R. Gwaltney; Superintendent of Maintenance
  • L. Hartz, Manager-Nuclear, Quality Assurance
  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

  • R. MacManus, Supervisor, System Engineering

A. Meekins, Supervisor, Administrative Services

J. McCarthy, Superintendent of Operations

J. O'Hanlon, Vice President, Nuclear Operations

  • A. Price, Assistant Station Manager
  • E. Smith, Site Quality Assurance Manager

B. Stanley, Supervisor, Station Procedures

  • J. Swientoniewski, Supervisor, Station Nuclear Safety

NRC Personnel

  • S. Tingen, Resident Inspector
  • J. York, Acting Senior Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

  • Plant Status

Unit 1 began the reporting period in power operation.

The Unit was at

power at the end of the inspection period, day 52 of continuous

operations.

Unit 2 began the reporting period in a refueling outage which is planned

to continue until May 3 .

2

3.

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operations safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility.

Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability.

Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports .w.~re reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Operator Rounds*

On March 17 during rounds in the SGR, an operator noted that four

temporary 480 volt power leads were running through the Unit 2 SGR

door.

These cables would have prevented closing this fire door.

The fire watch that was posted in the area was instructed to trip

open breaker 24Cl-7 and then cut the four 480 volt power leads in

case of a fire in the Unit 2 SGR.

The fire watch was then to move

the leads out of the path and close the door.

The operator noted

that the fire watch could not have cut the one inch diameter cable

with the tool provided.

In addition, the operator did not feel

that it safe for the fire watch to be manipulating 480 volt

breakers even though the unit was in cold shut down.

The operator

notified the shift supervisor and wrote station deviation

S-93-0339.

This action denotes a high level of sensitivity by the

operator and is identified as a strength.

b.

Unit 2 Refueling Operations

C.

On March 23 the inspectors attended the reactor vessel head lift

pre-job brief, and witnessed the lifting of the reactor vessel

head and the placement of the head in the containment basement.

This evolution was accomplished in accordance with Sections 5.8

and 5.9 of 2-0P-FH-001, Refueling Operations, dated

February 18, 1993.

The inspectors also witnessed other evolutions

associated with defueling unit 1.

These evolutions were well

organized and efficiently accomplished.

Design Basis Documentation Program

On April 2 the inspectors met with the Manager of Nuclear

Engineering to discuss the design basis documentation program.

The North Anna NRC Resident Inspectors had opened unresolved item

50-338/92-32-01, DBD Concerns, in their Inspection Report

50-338, 339/92-32. This item concerned the methodology and

resolution of open items identified during the DBD review.

The

inspectors also reviewed a QA assessment of this area that was

conducted from January 11 through February 4, 1993, (Reference-

3

Configuration Management Project, 93-01-ES-Ol-C, dated March

1993).

Among some of the items noted in this assessment were that

procedures do not have a systematic approach for resolving open

issues and that there were a large number of open issues.

Many of

the same issues identified for North Anna are also applicable to.

the Surry.

Until additional inspection can be conducted in this

area, this issue will be identified as Unresolved Item 50-280,

281/93-07-01, Evaluation of DBD Program.

Within the areas inspected, one URI item was identified.

4.

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with t~e appropriate

procedures.

a.

Replacement of a Relay in the Hi-Hi CLS System-Unit 1

While performing surveillance 1-PT-8.5, Consequence Limiting

Safeguards Logic (Hi-Hi Train), I&C technicians noted smoke coming

from the top of train B high-high CLS cabinet upon termination of

the test. Annunciator BC5 (CLS test coil failure) activated and

the technicians noted relay 3-CLS-2BM-Y was deenergized indicating

a failure of the relay.

The inspectors observed electrical craftsman replacing this relay

using WO 3800138357 and procedure No. O-ECM-1806-01, Protective

Relay and Associated Control Circuit Replacement, dated

December 3, 1992.

The system engineer was at the job site

supporting the craft for the replacement of the relay.

Visual

examination of the relay revealed a burnt condition.

The

inspectors noted that a second electrical craftsman was

independently verifying the work properly.

No problems were

identified in the maintenance activities.

b.

Unit 1 Turbine Driven AFW Pump Steam Trap Replacement.

On March 26, the Unit 1 turbine drive AFW pump, l-FW-P-2,

automatically tripped after being started for a monthly

surveillance test. The licensee concluded that the steam trap

located in the turbine steam supply piping had failed that allowed

water into the turbine causing the turbine to trip on overspeed.

The licensee replaced the steam trap in accordance with

WO 3800138831 and procedures O-MCM-1004-01, Flange, Gasket

Replacement, dated June 14, 1991 and O-MCM-1801-01,

Piping/Component/Repair/Replacement, dated December 18, 1992.

The

inspectors observed portions of the steam trap replacement and

reviewed the post maintenance test requirements .

The inspectors reviewed the post maintenance test requirements

after the maintenance was completed and the equipment returned to

4

service.

The inspectors discussed the test requirements with the

system engineer and concluded that the PMT data sheet did not

specify all the correct tests. Discussion with the system

engineer indicated that the trap should be tested by monitoring

movement of the steam trap's internals with ultrasonic test

equipment.

The PMT data sheet required that a leak test be

performed and that the trap be primed, but did not specify an

ultrasonic test.

Discussion with the PMT coordinator indicated that poor

communications between the planner who enters the test on the PMT

test data sheet and system engineer who specified the PMT was the

cause for the omitted test.

The PMT coordinator issued a PMT

Alert instructing planners when contacting a system engineer via

telecommunication, to reverify the PMT with the system engineer

prior to recording it on the PMT data sheet. Although the

ultrasonic test was not specified on the PMT data sheet, the

system engineer directed station personnel to perform an

ultrasonic test when the steam trap was returned to service. This

was performed.

Previously, on January 15, 1993, an identical event occurred when

the Unit 2 turbine driven AFW pump tripped after being started for

a monthly surveillance test. The steam trap located in the

turbine steam supply piping had failed. This resulted in water

intrusion into the turbine which caused the turbine to trip on

overspeed.

As a result of the Unit 1 and 2 turbine driven AFW

pump failures, the licensee began verifying proper operation of

the steam traps with ultrasonic test equipment on a daily basis.

The inspectors reviewed the maintenance histories for the Unit 1

and 2 turbine driven AFW pumps and concluded that these pumps did

not have a history of tripping upon starting. The inspectors

considered that the licensee was aggressively pursuing corrective

measures in order to preclude recurrence.

c.

Installation of Patch on Unit 1 SW Line

On March 26, the inspectors witnessed the installation of a code

repair (a temporary patch) on a 1/4 inch crack in bondstrand SW

piping.

The crack was located downstream of SW pump 1-SW-P-lOB,

which required the pump be isolated for maintenance.

With the

isolation of the pump, a TS twenty-four hour LCO was entered.

The

maintenance was done well within the LCO time restraints in

accordance with WO 3800138798 and vendor instructions that were

approved by SNSOC.

While observing this maintenance, the inspectors reviewed the work

package and identified several minor paperwork discrepancies that

were corrected at the job site. This maintenance was also

observed by station QA.

The inspectors noted QA's coaching the

craft on how to install the patch in accordance with the

5

requirements of the vendor's procedure.

At one point, QA stopped

the job and requested engineering assistance in determining the*

acceptability of the surface preparation for the patch and in

evaluating the proper cure time for the adhesive that secured the

patch to the pipe.

The coaching by QA, indicated to the inspector

that the craft was not properly prepared to do the job.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections (61726, 42700)

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure ~nd TS

requirements.

a.

Accumulator Discharge Check Valve Testing

b.

The inspectors reviewed the results of 2-0PT-SI-006, SI

Accumulator Discharge Check Valves Full Open Test, dated

March 9, 1993, that was performed on March 11.

The purpose of the

test is to verify that the accumulator discharge check valves

stroke fully open in accordance with the licensee's ASME Section

XI Inservice Testing Program for Pumps and Valves.

The test was accomplished with the plant depressurized.

The MOV

downstream of the accumulator was shut.

Each accumulator was

pressurized to approximately 140 psig with nitrogen.

The

accumulator level was established at 60%.

The discharge MOV was

opened and the accumulator discharged to approximately 40% level.

Temporary acoustical monitors were installed on the accumulator

discharge check valves to verify that the check valves fully

stroked.

The test was completed satisfactory.

The inspectors concluded that this new method of testing

accumulator discharge check valves was an improvement over the

previous method that required the check valves to be periodically

disassembled, inspected and reassembled.

GL 89-04, Guidance on

Developing Acceptable Inservice Testing Programs, dated April 3,

1989, states that non-intrusive testing to verify check valve full

stroke is preferred over disassembly and inspection.

In addition,

the check valves are located in the basement of the containment

which is a high radiation area.

Radiation exposure required for

non-intrusive testing was significantly less than the exposure for

disassembly and inspection.

Testing of the 2H Bus

On March 9, the inspectors observed part of the licensee's testing

on the Unit 2 2H emergency bus using procedure 2-0PT-ZZ-001, ESF

Actuation With Undervoltage and Degraded Voltage-2H Bus, Rev. 2,

dated March 1, 1993.

The test purposes were to verify the train A

SI function, to perform ERFCS verification, and to perform 3/4

6

logic verification for the CLS Hi and Hi-Hi systems.

The

inspectors observed the prejob briefing and noted various

components in operation i.e., the containment spray pump, the 3A

MDAFW pump, the LHSI pump, and EDG 2.

The inspectors noted that

operators were taking readings for the test on the instrumentation

for these pumps and recording the data in the test procedure data

sheets.

The procedure was reviewed and some of the results of the

test were discussed with the system engineer.

The requirements of

the logic test were satisfied since all of the proper signals were

received.

No discrepancies were noted.

c.

Type C Containment Testing

On March 16 the inspectors were in Unit 2 containment and

witnessed containment isolation valves 2-SS-TV-203A and B testing

in accordance with section 6.50 of 2-0PT-CT-201, Containment

Isolation Valve Local Leak Rate Testing (Type C Containment

Testing).

The inspectors attended the pre-test brief, observed

the test equipment installation, and observed the actual testing.

No discrepancies were identified.

6.

Safety Assessment and Quality Verification (40500)

a.

On March 24 the licensee presented a self-assessment to the Region

II NRC management.

This self-assessment covered a performance

review of certain business plan goals (capacity factor, forced

outages, EDG availability etc.), a self-assessment as defined by

SALP categories, and a summary of quality program evaluation of

Surry's performance.

Not only were strengths identified but also

areas of challenge for the facility.

b.

Maintenance Methodology Assessement

The inspectors reviewed the results of the Station Maintenance

Program audit conducted by QA during November 18 through December

14, 1992.

The audit utilized Performance Methodologies to assess

the maintenance department.

A Performance Methodology is a

documented systematic approach in assessing performance in a given

area to a standard or set of criteria.

Examples of performance

objectives are assignment of correct pri6rities to work orders,

verifying that all maintenance procedures are on the job site, or

verifying that the PMT instructions are adequate.

QA observes

maintenance personnel perform these objectives and rates the

performance.

The performance objectives are rated 1.0, Fully

Acceptable; 2.0, Acceptable; 3.0, Unsatisfactory; or 4.0,

Unacceptable.

The overall rating of the 1992 audit was 2.0.

Station Maintenance Program audits utilizing Performance

Methodology performance objectives were *accomplished in August

1990, and March and December 1991.

The results of the overall

ratings of these and the 1992 audits indicate that the performance

of the maintenance department is slowly improving.

The inspectors

7

concluded that the methodologies approach for assessing station

performance was an innovative method for performing audits.

Within the areas inspected, no violations were identified.

7.

Action on Previous Inspection Items (92701,92702)

a.

(Closed) Part 21 50-280, 281/P2191-09, Nuisance Tripping of

Heater Coils used in Cutler-Hammer C300 Overload Relays.

On

September 12, 1991, Eaton Corporation made a notification that

Hlll2 heater coils in C300 overload relays were defective and

should be replaced with a new design heater coil. Heater coils

Hlll3 and Hlll4 were identified as being potentially defective and

the notification recommended that they also be replaced.

The

licensee reviewed the application of Hlll2, Hlll3, and Hlll4

heater coils in safety-related systems and identified five

components that utilized these heater coils.

The heater coils

were installed in control room damper motor operators for

l-VS-MOD-103A, B, C, and D and in the Unit 1 charging pump

1-CH-P-lA auxiliary oil pump motor.

The inspectors reviewed

WOs 105516, 107042, 107041, 105058, and 104184 and verified that

the heater coils were replaced as corrective action for the

notification.

b.

(Closed) URI 50-280/93-05-03, Operability of Containment

Recirculation Spray System With Radiation Monitor Cabinet 1-2

Inoperable.

This issue involved the licensee declaring both

trains of containment recirculation spray inoperable due to the

failure of radiation monitor cabinet 1-2.

The inspectors

questioned the design of the containment recirculation spray

system in that a single failure caused both trains of a safety

system to be inoperable. Deviation Report S93-0207 documented the

failure of radiation monitor cabinet 1-2 and the inspectors

reviewed the corrective actions assigned to this DR.

The

licensee's DR analysis concluded that the operability of the

containment recirculation spray system was not dependent on the

operability of the RSHX SW radiation monitors.

The inspectors

agreed with this analysis.

It is recognized, however, that the

RSHX SW radiation monitors are important to safety, and the

licensee stated that procedures should *be revised to provide

instructions for loss of the radiation monitor power supply.

The

analysis also concluded that the RSHX SW radiation monitors were

appropriately classified as Regulatory Guide 1.97 instruments and

their power supply met the requirements of Regulatory Guide 1.97.

C.

(Closed) URI 50-280/93-05-04, Effects of MSVH Inlet Air Louver on

Operation of the AFW Pumps.

During the previous inspection

period, the Unit 2 MSVH air inlet louver actuator arm failed which

disabled the ability of the louvers to automatically operate.

When this failure occurred, engineering instructed operations that

the AFW pumps were operable but that the louvers should be

manually opened when operating the AFW pumps.

As a result of this

8

failure, the inspectors questioned if operating the AFW pumps was

dependent on opening the MSVH air inlet louvers to maintain the

required ambient air temperature.

In a memorandum from the

Supervisor of System Engineering to the Superintendent of

Engineering, dated March 23, 1993, the effect of the MSVH air

inlet louvers on the AFW pumps was addressed.

In this memorandum,

engineering concluded that there is no operability tie between the

louvers and the AFW pumps for outside air temperature in the range

of the ventilation system destgn.

The inspectors agreed. with the

licensee's conclusion.

Within the areas inspected, no viGlations were identified.

8.

Licensee Event Review

The inspectors reviewed the LER listed below and evaluated the adequacy

of the corrective action.

The inspector's review also included followup

of the licensee's corrective action implementation.

(Closed) LER 50-280, 281/93-003, Containment Air Recirculation System

Shutdown Renders Containment Radiation Monitors Inoperable During

Refueling Operations-Violation of TS.

A review which was concluded on

February 13, 1993, of the containment air particulate and gaseous

radiation monitors operability requirements revealed that the monitors

are rendered inoperable when the containment air recirculation system is

shut down.

This condition also applied to North Anna Nuclear Station.

The design functions of these monitors are to monitor airborne

radioactivity levels in containment, activate an alarm when airborne

exceeds an established level, automatically stop the containment purge

ventilation supply fans, and close the containment purge isolation

valves.

A licensee review of the previous Unit 1 outage (February-May

1992) indicated that the containment air recirculation system was

shutdown during refueling. Therefore, Unit 1 radiation monitors

l-RM-RMS-159 and 160 were not operable during refueling operations as

required by TS 3.10.A.2 and 3.10.A.4.

The manipulator crane area

radiation monitor was operable during this event and performs a similar

function as these two monitors.

In addition, continuous air monitors

equipped with audible alarms were operating during this period.

The root cause for this event was that inadequate design documentation

resulted in developing operating procedures that provided insufficient

  • direction to ensure that the subject monitors were operable during the

refueling operation.

The inspectors reviewed operations surveillance procedure

l/2-0SP-ZZ-004, Safety Systems Status List for Cold Shutdown/Refueling

Conditions, dated March 19, 1993, which has been modified as one of the

corrective actions to ensure that the manipulator crane is operable.

Another corrective action will be to change the TS (ref. CTS no. 2039)

to allow the securing of containment purge dtiring refueling operations

if the automotive isolation functions become inoperable.

9

This violation of TS requirements is identified as NCV

50-280, 281/93-07-02, Containment Air Recirculation System Shutdown

Renders Containment Radiation Monitors Inoperable During Refueling

Operations.

This violation will not be subject to enforcement action

because the licensee's efforts in identifying and correcting the

violation meet the criteria specified in Section VII.B of the

Enforcement Policy.

9.

Exit Interview

The results were summarized on April 5, 1993, with those individuals

i dent ifi ed by an asterisk in Paragraph 1.

The fa 11 owing summary of

inspection activity was discussed by the inspectors during this exit:

Item Number

Status

50-280,281/P2191-09

Closed

Part 21

LER 50-280,281/93-003

Closed

URI 50-280/93-05-03

Closed

- URI 50-280/93-05-04

Closed

URI 50-280,281/93-07-0l

Open

NCV 50-280,281/93-07-02

Closed

Descri ptfon

(Paragraph No.)

Nuisance Tripping of Heater

Coils used in Cutler-Hammer

C300 Overload Relays

(paragraph 7).

Containment Air Recirculation

system Shutdown Renders

Containment Radiation Monitors

Inoperable During Refueling

Operations-Via of TS

(paragraph 8).

Operability of Containment

Recirculation Spray System

With Radiation Monitor Cabinet

1-2 Inoperable (paragraph 7).

Effects of MSVH Inlet Air

Louver on Operation of the AFW

Pumps (paragraph 7).

Evaluation of DBD Program

(paragraph 3.c).

Containment Air Recirculation

System Shutdown Renders

Containment Radiation Monitors

Inoperable During Refueling

Operations (paragraph 8).

Proprietary information is not contained in this report.

Dissenting comments

were not received from the licensee .

.,.

10.

Index of Acronyms and Initialisms

AFW

ASME

-

CLS

CTS

DBD

DR

ECCS

-

EOG

ERFCS -

ESF

GL

l&C

  • LER

LHSI

-

MDAFW -

MOV

MSVH

-

NCV

NRC

PMT

PSIG

-

QA

RSHX

-

SALP

-

SGR

SI

SNSOC -

SW

TS

URI

WO

AUXILIARY FEEDWATER

AMERICAN SOCIETY.OF MECHANICAL ENGINEERS

CONSEQUENCE LIMITING SAFEGUARDS

COMMITMENT TRACKING SYSTEM

DESIGN BASE DOCUMENTATION

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

EMERGENCY RESPONSE FACILITY COMPUTER SYSTEM

ENGINEERED SAFETY FEATURE

GENERIC LETTER

INSTRUMENTATION AND CALIBRATION

LICENSEE EVENT REPORT

LOW HEAD SAFETY INJECTION

MOTOR DRIVEN AUXILIARY FEEDWATER

MOTOR OPERATED VALVE

MAIN STEAM VALVE HOUSE

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

POST MAINTENANCE TEST

POUNDS PER SQUARE INCH GAUGE

QUALITY ASSURANCE

RECIRCULATION SPRAY HEAT EXCHANGER

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

SWITCHGEAR ROOM

SAFETY INJECTION

SURRY NUCLEAR SAFETY AND OPERATING COMMITTEE

SERVICE WATER

TECHNICAL SPECIFICATION

UNRESOLVED ITEM

WORK ORDER