ML18152A534

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Insp Repts 50-280/92-20 & 50-281/92-20 on 920905-1003. Violations Noted,Not Subj to Enforcement Action.Major Areas Inspected:Operations,Maint,Surveillance,Quality Verification & Licensee Event Review
ML18152A534
Person / Time
Site: Surry  Dominion icon.png
Issue date: 11/02/1992
From: Branch M, Fredrickson P, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A535 List:
References
50-280-92-20, 50-281-92-20, NUDOCS 9211180143
Download: ML18152A534 (13)


See also: IR 05000280/1992020

Text


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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/92-20 and 50-281/92-20

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

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Inspection Conducted:

September 5 through October 3, 1992

Inspectors:

Accompanying

Approved by:

M.~~i~dent Inspector

J.W~~t~or

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~

S. G. Ting~ent Inspector

Intrl~---,,

P. E. Fredrickson, Section Chief

Division of Reactor Projects

SUMMARY

Scope:

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Dat'e Sined

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Date S1gned

This routine resident inspection was conducted on site in the area of

operations, maintenance, surveillance, quality verification, licensee event

review, and action on previous inspection items.

During the performance of

this inspection, the resident inspectors conducted review of the licensee's

backshifts or weekend operations on September 6, 7, 16, 26, 27 and October 1,

and 3.

Results:

In the operations area, the following items were noted:

The noise level in the control room has been reduced through a

modification to the Gaitronic system and the control room is much

quieter (paragraph 3.a).

9211180143 921102

PDR

ADDCK 05000280

8

PDR

2

Management's sensitivity to recent operator errors was noted.

A recent

increasing performance trend of operator errors indicates a low problem

identification threshold and appears to warrant the current level of

management attention in order to turn around this trend (paragraph 3.b).

In the maintenance/surveillance functional area, the following item was noted:

Communications between operations and I&C was considered good while

troubleshooting the Unit 1 rod control urgent failure alarm (paragraph

4.a).

In the safety assessment/quality verification area, the following items were

noted:

The post-trip review process clearly has a positive effect on the safe

return of the plant to power operation (paragraph 6).

The licensee identification of a steam flow scaling error during

special testing resulted in the correction of a safety issue associated

with steam flow trip setpoints that had gone unnoticed since a 1977

modification.

The safety significance of the issue was somewhat

mitigated since the actual setpoints, although not in accordance with TS

limits, were bound by the accident analysis.

The failure to satisfy the

TS limits for the steam flow setpoints was identified as a non-cited

violation (paragraph 7.a).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

  • R. Allen, Supervisor, Operations
  • W. Benthall, Supervisor, Licensing

R. Bilyeu, Licensing Engineer

H. Blake, Superintendent of Site Services

  • B. Bryant, Licensing

R. Blount, Superintendent of Engineering

  • H. Collar, Supervisor, Quality Assurance
  • D. Christian, Assistant Station Manager
  • J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

  • R. Gwaltney, Superintendent of Maintenance
  • M. Kansler, Station Manager

A. Meekins, Supervisor, Administrative Services

J. McCarthy, Superintendent of Operations

  • R. MacManus, Supervisor, System Engineering
  • A. Price, Assistant Station Manager
  • R. Saunders, Assistant Vice President, Nuclear Operations

E. Smith, Site Quality Assurance Manager

  • B. Stanley, Supervisor, Station Procedures

J. Swientoniewski, Supervisor, Station Nuclear Safety

G. Thompson, Supervisor, Maintenance Engineering

A. Wheeler, Shift Supervisor, Nuclear

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Other licensee employees contacted included control room operators,

shift technical advisors, shift supervisors and other plant personnel.

On September 11, the inspectors accompanied Dr. Thomas Murley, Director

of NRR, on a tour of the Surry facility. The major emphasis of the tour

was a familiarization of plant equipment vulnerability to internal

flooding that was identified during the NRC IPE review.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status

Unit 1 began the reporting period with the reactor at approximately 5% *

power with the main turbine off-line to repair a leaking transformer

bushing on the C station service transformer.

The main generator was

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reconnected to the grid on September 6, and the unit was at power at the

end of the inspection period, day 27 of continuous operation.

Unit 2 began the reporting period in power operation.

The unit was at

power at the end of the inspection period, day 77 of continuous

operation.

Both units periodically ramped power to allow cleaning of condenser

water boxes.

The water boxes were being clogged by hydroids and other

marine life.

3.

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operations safety and

compliance with TSs and to maintain awareness of the overall operation

of the facility.

Instrumentation and ECCS lineups were periodically

reviewed from control room indication to assess operability. Frequent

plant tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping. Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Control Room Environment Improvement

b.

The gaitronics is utilized for colllllunications throughout the

plant. During the inspection period, the licensee modified the

operation of the gaitronics colllllunication system in order to

decrease the overall noise level in the control room.

Prior to

the modification, paging personnel over the gaitronics would be

broadcasted throughout the plant including the control room.

This

created a lot of unnecessary background noise in the control room.

The licensee modified the gaitronics so that paging of only

control room personnel would be heard in the control room.

This

resulted in a significantly decreased noise level in the control

room.

Operational Errors

On October 2, the inspectors met with the Surry Operations

Superintendent to discuss what appeared to be an increasing trend

in the number of operational errors.

Errors occurring during the

period September 14 through September 29 which resulted in

deviation reports were evaluated by the inspectors. The

inspectors discussed the following four station deviations with

the Superintendent:

-OR No. S-92-1514 - The lA CC heat exchanger was returned to

service with its CC side outlet valve (valve no. l-CC-583)

still closed. Procedure O-MOP-51.17 step 5.1.3 was signed

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off for valve l-CC-583 being open.

Another operator noticed

the error. Operations management discussed the error with

the operator and discussed the necessity to think about the

procedural instructions.

-DR No. S-92-1578 - The remote alarm cutout switch was found

in the silenced position which would prevent the control

room from receiving indications of an alarm condition on TS

heat trace circuits. The probable cause was human error by

operations or maintenance. A check showed that maintenance

had been performed two weeks previously but did not identify

the responsible department.

To correct this potential

problem, a check for the position of this switch has been

added to the operators' check list.

-DR No. S-92-1610 - The Unit 2 outside RS train was tagged

out for repair of the service water pump 1-SW-P-SB return

line. The operator closed MOV-SW-205C instead of

MOV-SW-205B for isolation purposes.

The on-shift RO

researched the prints, but the SRO did not independently

review the decision as required by the OPS guidelines. The

error was identified through the second check process prior

to release of work.

-DR No. S-92-1617 - The Unit 1 SRO and the shift supervisor

erroneously decided that opening~ particular valve

(l-CH-98) would bypass the boric acid filter.

The shift

supervisor decided it was not necessary to use the

maintenance procedure, l-HOP-8.27, Removal of Boric Acid

Filter from Service, to remove the filter from service .

. This alignment resulted in the flow from the B to the A BAST

and later in the shift a high level alarm in the A BAST was

received.

The error was realized and the correct valve

line-up was performed using the MOP.

While none of the events caused a serious safety concern, the

number of errors over the two week period seemed to indicate an

increasing trend in operational errors.

The concern was discussed

with the Operations Superintendent who indicated that operations

management had also noted the trend.

The inspectors confirmed

that meetings had been held with the shift supervisors and that

operations management was in the process of briefing all of the

shift personnel concerning these events and the trend.

Management's sensitivity to recent operator errors was noted by

the inspectors.

Recent performance trends denoting an increase in

operator errors indicate a low problem identification threshold

and appears to warrant the current level of management attention

in order to turnaround this trend.

The inspectors will continue

to follow the licensee's activities in this area .

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c.

Evaluation of Opening in Charging Pump Cubicle Walls

While touring the auxiliary building, the inspectors noted that

the concrete walls that enclosed the charging pumps contained

unsealed penetrations. Several holes approximately six inches in

diameter and other openings existed around piping or ventilation

ducting that passed through the walls.

The inspectors reviewed

Chapter 10, Section 8, of the licensee's 10 CFR 50 Appendix R

Report and concluded that the charging pump cubicle concrete walls

were classified as non-rated fire barriers.

The issue of openings

in non-rated fire barriers was discussed in detail with the

licensee.

The inspection concluded that these openings were

acceptable, since the charging pump cubicle concrete walls were

not classified as fire rated boundaries, and an alternative means

of safe plant shutdown was available in the event of a fire in

this area.

Within the areas inspected, no violations were identified

4.

Maintenance Inspections (62703) (42700)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the appropriate procedures.

On October 2, a Unit 1 control rod urgent failure alarm occurred while

the inspectors were in the control room.

Upon receipt of the alarm

operators placed the rod control system in manual and entered a TS LCO

to restore the control rods to an operable status within the next two

hours or be in Hot Shutdown within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

The inspectors witnessed troubleshooting activities associated with

urgent failure alarm.

The troubleshooting was accomplished by l&C

technicians in accordance with IMP-C-EPCR-46, Maintenance of Rod Control

System, dated June 26, 1989, and WO 3800133273.

Troubleshooting

identified faults in the moveable-phase-control card and moveable-

firing-circuit card.

These cards were replaced and the urgent failure

alarm cleared.

The control rods were satisfactorily tested and the LCO

was exited. Testing of the control rods is further discussed in

paragraph 6.b.

The inspectors attended the prejob brief and reviewed

the completed work package and post-maintenance test requirements.

The

inspectors noted that col11llunications between operations and l&C was

good.

Also, the inspectors noted that there were operator aids in the

form of uncontrolled vendor drawings taped to the interior of the rod

control power cabinet doors.

The drawings were not used during these

troublshooting activities. A recent QA audit, 92-11, identified the use

of operator aids as inappropriate, and as a result, corrective actions

are scheduled to be implemented to remove and restrict the use of

operator aids.

Within the areas inspected, no violations were identified.

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5.

Surveillance Inspections (61726, 42700)

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

The following surveillance activities were reviewed:

a.

Calibrations of Pressure Indicators

On September 27, the inspectors observed the partial calibration

of pressure indicator 2-CH-Pl-1104 which is the discharge pressure

indicator for boric acid transfer pump l-CH-P-2D.

The l&C

technicians were using procedure 2-IMP-CH-Pl-001, Charging System

ASME Section XI Pressure Indicator Calibrations, dated July 18,

1991.

The technicians took the as-found readings on this pressure

indicator. These readings were within the acceptable range for

the instrument, but at the high end.

The indicator was later

adjusted to the mid-range and another set of satisfactory as-left

readings were taken.

The inspectors later reviewed the

calibration documentation.

No discrepancies were identified.

b.

Unit 1 Rod Control System Testing

On October 2, the inspectors witnessed testing of the rod control

system in accordance with l-PT-6.0, Control Rod Partial Movement,

dated July 23, 1992. This testing was performed as a result of

maintenance on the rod control system that effected shutdown bank

B, and control rod banks Band D. In order to prove operability,

the affected control rods were moved 18 steps in and then back out

18 steps.

The inspectors witnessed the testing from the control

room.

No discrepancies were identified.

Within the areas inspected, no violations were identified.

6.

Review of Unit 1 Reactor Trip Report (40500)

VPAP-1404, Reactor Control, Revision 0, requires that a formal

report be prepared for each reactor trip. The purpose of the

report is to confirm the preliminary findings, and sulllllarize or

identify corrective actions associated with the reactor trip. The

report is required by YPAP-1404 to be approved by SNSOC within

thirty days following a reactor trip. The inspectors reviewed the

trip report, dated June 16, 1992, for the Unit 1 automatic reactor trip that occurred on May 7, 1992. This Unit 1 automatic reactor

trip was previously discussed in NRC IR 280,281/92-11.

The

inspectors noted that although the report was not approved by

SNSOC within thirty days, it was thorough and accurate.

Several items associated with the reactor trip were identified as

needing further review in the trip report. These items involved the

turbine driven AFW pump response time and emergency procedure guidance

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for ensuring adequate TS shutdown margin.

The inspectors reviewed the

licensee's actions to resolve these issues and concluded that the issues

were satisfactorily resolved or that the licensee was satisfactorily

pursuing this issues. The licensee's post-trip review process clearly

has a positive effect on the safe operation of the plant, in that

transient response characteristics were verified and the thoroughness of

the process was considered a strength.

Within the area inspected, no violations were identified.

7.

Licensee Event Review (92700)

The inspectors reviewed the LERs li~ted below and evaluated the adequacy

of corrective action. The inspector's review also included followup on

the licensee's implementation of corrective action.

a.

(Closed) URI 280,281/91-21-02 and LER 280,281/91-014, Steam Flow

Transmitter Scaling Errors. This issue involved the licensee's

discovery that TS limits associated with steam flow protection

setpoints were violated due to personnel errors associated with a

1977 modification that rescaled the steam flow instruments. The

initial discovery of this issue is documented in detail in NRC IR

50-280,281/91-21.

In that report the inspectors documented that

the licensee investigated the effect of the incorrectly scaled

steam flow transmitters on the overall accuracy of the steam flow

instrumentation and on reactor protection and ESF setpoints.

Midway through the investigation for Unit 2, the licensee

concluded that the Unit 1 MS flow transmitters were also

incorrectly scaled.

The licensee determined that the incorrectly

scaled transmitters affected the MS flow reactor protection and

ESF setpoints in a nonconservative direction. The magnitude of

this error was unknown, but the current settings were within the

limits of the safety analysis.

On July 22, 1991, the bias on each of the Unit 2 ESF MS flow

channels was adjusted to compensate for the nonconservative error

introduced by the improperly scaled transmitters.

On July 24,

1991, the bias on the Unit 1 ESF MS flow channels was adjusted for

the same reason. The magnitude of the ESF MS flow channel bias

adjustments was based on engineering judgment to ensure that the

settings were within the TS limits.

On July 24, 1991, as a result

of an investigation, the licensee concluded that prior to the

July 22, 1991, setting adjustments, the Unit 2 ESF high steam flow

setpoints exceeded the limits specified in TS, but were within the

design safety analysis.

The special flow measurements (ST-302) in 1991 that provided the

basis for the Unit 2 bias was not conducted for Unit 1.

At the

end of that inspection period documented in NRC IR 50-280,

281/91-21, the licensee was investigating the magnitude of the

error introduced by the incorrectly scaled steam flow transmitters

b.

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on the Unit 1 ESF setpoints. Since ST-302 was not performed on

Unit 1, in the interim, on July 26, 1991, the bias on each of the

Unit 1 ESF MS flow channels was adjusted based on the worst case

Unit 2 setpoints error.

The licensee also concluded that the

effect of the scaling error on the MS flow transmitters did not

adversely affect the low SG water level with a steam/feedwater

flow mismatch reactor trip circuitry.

To develop steam flow instrument setpoint scaling valves for Unit

1, the licensee conducted special testing during the 1992

scheduled refueling outage.

The inspectors reviewed the licensee

test results conducted on February 3, 27, 28 and 29, 1992.

The

testing was performed using the Combustion Engineering's CHEMTRAC

feedwater flow tracer process.

The results of the test were

reviewed by engineering, and calculations were performed to

translate the test results into instrument scaling and setpoint

changes.

The inspectors reviewed calculation EE-0419 which

assigned correction factors that were applied to the indicated

feed flow values.

The instrument accuracy was corrected by the

performance of the feed flow calibration PT which was revised

prior to accomplishment based on the new values provided by

engineering.

The inspectors consider the licensee actions

acceptable and this item is closed.

Since the LERs discussed above identified that the original

setpoints were nonconservative in respect to the TS required

values the licensee was in violation of TS 3.7.D.

The licensee

identification of the steam flow scaling error during special

testing resulted in the correction of a safety issue associated

with steam flow trip setpoints that had gone unnoticed since a

1977 modification.

The safety significance of the issue was

somewhat mitigated since the actual setpoints, although not in

accordance with TS limits, were bounded by the accident analysis.

This licensee identified violation (NCV 50-280,281/92-20-01) is

not being cited because criteria specified in Section VII.b of the

NRC Enforcement Policy were satisfied.

(Closed) LER 280/91-012, Pressurizer Level Channel Not Placed in

Trip Within Six Hours Due to Personnel Error. This issue involved

the failure to place pressurizer level indicator l-RC-Ll-1461 in

trip because its indicated value exceeded channel check acceptance

criteria specified in the surveillance procedure.

The TS allows

six hours to place the channel in trip.

The operations trainee

did not recognize that the value exceeded the acceptance criteria

and neither the reactor operator responsible for the surveillance

nor the shift supervisor reviewed the PT.

The reactor operator

was counseled on his responsibility for the accuracy of recorded

data and for the proper supervision of assigned trainees. Further

corrective actions taken included providing the description of the

event and lessons learned to the class of RO/SRO's that were being

trained at the time of the event and developing enhanced

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instructions for future classes. All of the corrective actions

have been implemented.

c.

(Closed) LER 280/91-009, Technical Specifications Surveillance

Requirements Violated for Inservice Inspection of Unit 1 Reactor

Vessel Due to a Cognitive Personnel Error.

This issue involved a

missed ASME Section XI ISi inspection. Unit 1 was at 100 percent

power on May 9, 1991, when the licensee discovered that a visual

inspection of the reactor vessel partial penetration welds and the

bottom of the reactor were not performed during the 1990 refueling

outage.

An administrative oversight, whereby the inspections were

inappropriately removed and not returned to the ISi plan, was

identified as the cause of the event. The intent of this test is

to monitor the reactor vessel integrity. Daily leak rates were

calculated for Unit 1 to ensure that TS allowed unidentified

leakage was not exceeded.

Containment air sampling was increased

from weekly to daily to assist in leak detection.

On January 8,

1992, during an unscheduled outage, the visual examination, VT-2,

was performed on the bottom of the reactor vessel and the partial

penetration welds.

The inspectors examined the ISi program for

Unit 1 and noted that the visual examination had been returned to

the program.

d.

(Closed) LER 280/92-001, Dropped Rod Due to Personnel Error

Followed by a Required Manual Reactor Trip. This event occurred

after control rod E-5 dropped into the core.

(It was later

determined that its coil stack failed.)

As a result, trouble

shooting was performed.

The trouble shooting guide required the

removal of fuses.

One of the removed fuses was co11111on to the

movable coils of E-5 and H-2.

When the control rods were manually

stepped to control delta flux, H-2 dropped into the core because

its stationary coil deenergized and its movable coil did not

energize.

The reactor was manually tripped in accordance with

procedure. This event is discussed more fully in NRC IR

50-280,281/91-37.

The dropping of the second rod was attributed

to an inadequate trouble shooting guide procedure.

The licensee's

corrective action to prevent recurrence of this type of event

included changes to procedures and training.

An evaluation

sampling was performed of the corrective actions by reviewing

procedure changes and various training lesson plans. Corrective

actions that are not complete, such as some craft training and

development of a new electrical maintenance procedure for rod

control trouble shooting, are being tracked by the licensee's CTS.

Procedures reviewed were AP-1.01, Control Rod Misalignment, and

IMP-C-EPCR-46, Maintenance of Rod Control System.

Steps and

caution notes concerning ramification and actions required for

stepping control rods with control rod trouble shooting in process

were incorporated into these procedures.

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Lesson plans reviewed were TSMT-92.1-LP-l, TSCT-92-LP-1,

ECT-1-LP-8 and NITCTP-l-LP-14.

These lesson plans covered the

subjects of test controls, conduct of infrequently performed tasks

and root cause determinations, and included the above event, its

cause, and lessons learned.

Within the areas inspected, no violations were identified.

8.

Action on Previous Inspection Items (92701,92702)

a.

(Closed) VIO 280/91-37-01, Failure to Follow the Requiremenis of

10 CFR 50.SSa(g). This issue involved whether it was necessary

for the licensee to request that the Co11111ission grant relief for

the repair or return to service of a Class 2 letdown line with a

leaking weld.

The licensee denied the violation and, after

further NRC review, the subject violation was withdrawn.

The

licensee had concluded that it was not necessary to request NRC

relief based upon the Surry TS and an ASME Code Inquiry.

The NRC

is continuing to review the adequacy of this interpretation.

b.

(Closed) P21 280,281/91-06, Overspeed Trip Tappets For

Terry Steam Turbine Pump Drivers in AFW Systems. This issue

involved Terry turbines equipped with a molded head type tappet.

Under high temperature and humidity, parts of the tappet would

swell preventing the tappet from reseating following a trip of the

Terry turbine.

The inspectors reviewed the design of the turbine

driven AFW pumps overspeed trip tappets utilized at Surry and

concluded that they were not the molded head type discussed in

this notice.

The Surry turbine driven AFW pumps utilize the ball

type tappets.

9.

Exit Interview

The results were summarized on October 7, with those individuals

identified by an asterisk in Paragraph 1.

The following suRVnary of

inspection activity was discussed by the inspectors during this exit:

Item Number

NCV 280,281/92-20-01

VIO 280/91-37-01

P21 280,281/91-06

Status

Closed

Closed

Closed

Description

Failure to Satisify TS Limits

Associated with Steam Flow Setpoints

(para 7.a).

Failure to Follow the Require-

ments of 10 CFR 50.SSa(g)

(para. 8.a}.

Overspeed Trip Tappets For

Terry Steam Turbine Pump

Drivers in AFW Systems (para 8.b).

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URI 280,281/91-21-02

Closed

Steam Flow Transmitter Scaling

Errors (para 7.a).

LER 280,281/91-014

Closed

Steam Flow Transmitter Scaling

Errors (para 7.a).

LER 280/91-012

Closed

Pressurizer Level Channel not Placed

in Trip Within Six Hours Due to

Personnel Error (para 7.b)

LER 280/91-009

Closed

Technical Specifications Sur-

veillance Requirements Violated for

ISi of Unit 1 Reactor Vessel Due to

Cognitive Personnel Error

(para 7.c).

LER 280/92-001

Closed

Dropped Rod Due to Personnel Error

Followed by a Required Manual Reactor Trip (para 7.d).

Proprietary information is not contained in this report. Dissenting comments

were not received from the licensee.

10.

Index of Acronyms and Initialisms

AFW

ASME

-

BAST

-

cc

CFR

CTS

DR

ECCS

-

ESF

GL

I&C

IPE

IR

LCO

LER

MOP

MS

NCV

NRC

NRR

OPS

PT

QA

RO

RS

SNSOC -

SOER

-

AUXILIARY FEEDWATER

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

BORIC ACID STORAGE TANK

COMPONENT COOLING

CODE OF FEDERAL REGULATIONS

COMMITMENT TRACKING SYSTEM

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

ENGINEERED SAFETY FEATURES

GENERIC LETTER

INSTRUMENTATION AND CONTROL

INDEPENDENT PLANT EVALUATION

INSPECTION REPORT

LIMITING CONDITIONS OF OPERATION

LICENSEE EVENT REPORT

MAINTENANCE OPERATING PROCEDURE

HAIN STEAM

NONCITED VIOLATION

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

OPERATIONS DEPARTMENT

PERIODIC TEST

QUALITY ASSURANCE

REACTOR OPERATOR

RECIRCULATION SPRAY

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SIGNIFICANT OPERATING EVENT REPORT

.,

'

SRO

TS

URI

VIO

VPAP -

WO 11

SENIOR REACTOR OPERATOR

TECHNICAL SPECIFICATIONS

UNRESOLVED ITEM

VIOLATION

e

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER