ML18152A503

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Insp Repts 50-280/93-02 & 50-281/93-02 on 930322-26.No Violations Noted.Major Areas Inspected:Review of Unit 2 ISI Program & Plan for Current Outage,Observation of Inprocess NDE Exams
ML18152A503
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/07/1993
From: Blake J, Crowley B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A504 List:
References
50-280-93-02, 50-280-93-2, 50-281-93-02, 50-281-93-2, NUDOCS 9304210152
Download: ML18152A503 (16)


See also: IR 05000280/1993002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 1.1

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

APR - 9 lS93.

Report Nos.:

50-280/93-02 and 50-281/93-02

Licensee:

Virginia Electric and Power Company

Glen Allen, VA 23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection

22 - 26, 1993

Approved

Scope

Blake, Chief

erials and Processes Section

Engineering Branch

Division of Reactor Safety

SUMMARY

Date Signed

~hA3

Date Signed

This routine, unannounced inspection was conducted in the area of Inservice

Inspection (ISi).

The inspettion included a review of the Unit 2 ISi program

and plan for the current outage, as well as overall programmatic controls;

review of nondestructive examination (NOE) procedures; observation of in-_

process NDE examinations; review of NDE p~rsonnel qualifications; and review

of NOE equipment calibration and material certification documentation.

In*

addition, implementation of the licensee's Flow Assisted Corrosion (FAC)

(Erosion/Corrosion) program was inspected. Also, followup inspections were

performed on previously identified inspection findings.

Results

This inspection indicated that, in general, a good ISi program was in place

with good implementation.

Examination procedures meeting Code requirements

were being used and inspections were being performed by qualified personnel.

The procedures, examinationtechniques used to conduct the examinations, and

documentation of examination results were good .

9304210152 930409

PDR

ADOCK 05000290

G

PDR

2

In the area of Flow Assisted Corrosion (FAC), the licensee has a strong,

program implemented.

The program has strong corporate and site support with

dedicated resources and is well documented in corporate standards and site

procedures.

Degraded piping is being routinely identified and replaced with

upgraded materials.

In the areas inspected, no violations or deviations were identified .

l.

Persons Contacted

Licensee Employees

-

REPORT DETAILS

W. Benthall, Supervisor, Licensing

  • R. Blount, Superintendent, Engineering
  • D. Grady, Supervisor, NDE

T. Huber, Supervisor, ISI/NDE and Engineering Programs

L. Humphrey, Senior Inspector

  • M. Kansler, Station Manager

D. Phelps, Engineer

  • J. Price, Assistant Station Manager,

D. Rogers,. Lead ISI Engineer

  1. R. Saunders, Assistant Vice President, Nuclear Operations
  • E. Smtth, Manager, Quality Assurance

D. Woodyard, Senior Inspector

Contractor Personnel

P. McFadden, NDE Supervisor, Virginia Corporation of Richmond (VCR)

J. Sombo, Steam Generator Eddy Current Coordinator,Westinghouse

(li) - Nuclear Services Division (NSD)

Other licensee employees contacted ~uring this inspection included

craftsmen, engineers, quality control personnel, security force members,

technicians, and administrative personnel.

NRC Resident Inspectors*

  • J. York, Resident Inspector

S. Tingen, Resident Inspector

  • Attended exit interview
  1. Participated in exit interview via telephone

Acronyms and Initialisms used throughout this report are listed in the

last paragraph.

2.

Inservice Inspection (ISI) (Unit 2)

The tns~ector reviewed documents and records, and observed activities,

as indicated below, to determine whether ISI was being conducted in

accordance with applicable procedures, regulatory requirements, and

licensee commitments.

The applicable Code for ISI (Units~ and 2) is

the American Society of Mechanical Engineers Boiler and Pressure Vessel

(ASME B&PV). Code,Section XI, 1980 Edition, Winter 1980 Addenda .

For Unit 1, the second 10-Year interval started in December 22, 1982,

and ends October 14, 1993.

For Unit 2, the second 10-Year interval

started May 1, 1983, and ends May 10, 1994.

By letters dated July 11,

2

  • and October 1, 1991, VEPCO extended the second interval end dates for

both Units based on extended plant outages.

The new end dates are

July 15, 1994, for Unit 1 and May 9, 1995, for Vnit 2.

The current Unit

2 outage is the first outage of the third period.

Revision O for the Unit 1 second interval program plan and relief

requests was submitted to the NRC by VEPCO letter dated September 21,

1982.

Revision 1 to the Unit 1 plan and revision O of the Unit 2 plan

were submitted on

December 27, 1982. * NRC Safety Evaluation Reports

(SERs) dated January 24, 1984, (Unit 1), and January 24, 1986, (Unit 2),

were issued. Additional submittals, including revision 2 to the Unit l

plan were dated November 26, 1985, and April 17, April 24, May 22,

June 23, and September 30, 1986.

Revision 3 for Unit 1 and Revision 1

for Unit 2 plans were submitted on April 16, 1987.

Additional

-information was provided by VEPCO letters dated June 22, and

September 30, 1988, and February 15, and May 15, 1989.

The NRC SER

covering both units was issued March 14, 1991. * The program plans

. included 14 NDE relief requests. All 14 relief requests were granted,

granted with conditions, or determined to not need approv~l.

Revision 4

to the Unit 1 program and revision 2 to the Unit 2 program were issued

on March 3, 1993, to make administrative changes, incorporate SER

changes, and add additional relief requests (SR-015, 016, 017, 018 and

  • 019).

The licensee's corporate and site ISi organizations are responsible for

the nondestructive examination (NDE) program.

~ontractors furnish NOE

.

examiners and a NDE supervisor with ovefall coordination and supervision

provided by the VEPCO site ISi organization.

For the current outage,

Virginia Corporation of Richmond (VCR) is performing the majority of NDE

examinations.

Westinghouse is performing Eddy Current {ET) examinations

of steam generator tubing.

a.

ISi Program Review (73051) (Unit 2)

The inspector reviewed the following documents related to the ISi

program to determine whether relief requests had been approved by

NRR, the services of an Authorized Nuclear Inservice Inspector

(ANII) had*been procured and was involved. in ISi activities, the

pl an had been approved by the licensee. and to assure that

procedures and plans had been established (written, reviewed,

approved and issued) to control and accomplish the following

applicable activities: program organization including

identification of commitments and regulatory requirements,

preparing plans and schedules, and qualification, training,

responsibilities, and duties of personnel responsible for ISi; *

repair and replacement program requirements; personnel

qualification requirements; and guidance for identifying and

processing relief requests.

Surry Power Station Unit 2 Inservice Inspection Program -

Interval 2 - May 01, 1983 - May 10, 1994

3

Surry Power Station Unit 2 Inservice Inspection Plan For

The Second Inspection Interval Volume 2 - Revision 1 -

February 1991 For Components and Component Supports - May 1,

1983 - May 10, 1994

Inservice Inspection Manual, Revision 36

Augmented Inspection Manual, Revision 6

Surry Unit 2, Interval 2, Period 3, Items Remaining to be

Examined, Revision 3

Work Order (WO) 359816, ISI NOE Inspections (Outage Plan)

SUADM-M-23, dated 6/8/89, Disposition of ASME Section XI

Inspection and Testing Discrepancies

SUADM-M-25,- Revision 0, ASME Documentation Control and

Reporting Requirements

SUADM-M-26, Revision 1, ASME Section XI Inspection and

Examination Control

VPAP-307, Revision 2, Repair and Replacement of ASME Section

XI Components

VPAP-0502, Revision 3, Procedure Process Control

SSES-1.05, Revision 3, Controlling Procedure For Engineering

Assignment Schedule

SSES-6.01, Revision 1, Controlling Procedure For ISi

Engineering

SSES-6.02A, Revision 1, Controlling Procedure For Repair and

Replacement Follower

SSES-6.02B, Revision 1, Controlling Procedure For Logging

ASME XI Reports

SSES-6.06, Revision 0, Controlling Procedure For The Review

of ISi Related Issues/Checklists Prior to Unit Startup

Following A Refueling Outage

SSES-7.01, Revision 1, Controlling Procedure For Surry NOE

Services

SSES-7.02, Revision 0, Controlling Procedure For the Review

& Routing of Completed NOE Reports

NDE-3.1, Revision 6, Preparation, Issue and Control of

Nondestructive Examination Procedures

4

NOE-4.1, Revision 11, Virginia Power Written Practice For

Certification of Nondestructive Examination Personnel

NOE-6.2, Revision 2, Review of Contractor Nondestructive

Examination Interpretation By Virginia Power Personnel

NOE-6.3, Revision 1, Storage and Control of NOE Calibrated

Equipment, Calibration Standards & Consumable NOE Materials

NOE-6.4, Revision 0, Selection of Calibration Blocks For PSI

and ISI Ultrasonic Examination

NOE-7.2, Revision 5, General Requirements For ISi

Nondestructive Examination

Many of the documents and procedures listed above and in paragraph

b. below were reviewed during the inspection documented in NRC

Report 50-280, 281/92-09.

Only changes since that inspection were

reviewed.

As noted in report 92-09, procedures did not clearly

iterate the controls required for the inspection plans provided by

corporate.

The above review revealed that the plans are now

formally issued and controlled.

b.

Review of NOE Procedures (73052) (Units 1 and 2)

The inspector reviewed the procedures listed below to determine

whether these procedures were consistent with regulatory

requirements and licensee commitments.

The procedures were

reviewed in the areas of procedure approval, requirements for

qualification of NOE personnel, compilation of required records,

and division of responsibility between the licensee and contractor

personnel.

In addition, the procedures were reviewed for

technical adequacy and conformance with ASME, Sections V and XI,

and other licensee commitments/requirements.

NOE-PT-201, Revision 2, Liquid Penetrant Examination

NDE-MT-202, Revision 2, Magnetic Particle Examination of

Bolting

NDE-UT-201, Revision 3, Manual Ultrasonic Examination Of

Piping Welds

NOE-UT-204, Revision 2~ Inservice Ultrasonic Examination of

Cla~s 1 Bolting.

SUAOM-M-20, Revision 2, ASME Section XI Visual Examination

Program (VT-1, 2, and 3)

MRS 2.4.2 VEP-1, Revision 5, Eddy Current Inspection of

Preservice and Inservice Heat Exchanger Tubing at Surry

Power Plant

I

,

5

SGPMS-002, Revision 2, Plant Specific Guidelines Eddy

Current Data Analysis, Training, and Testing

DAT-GYP-001, Revision 6, Data Analysis

c.

Observation of Work and Work Activities {73753) {Unit 2)

The inspector observed work activities, reviewe~ NDE personnel

qualification records, and reviewed certification records of NDE

equipment/materials, as detailed below.

During the examinations,

the inspector verified: availability of and compliance with

approved NDE procedures, use of knowledgeable NDE personnel, and

use of NDE personnel qualified to the proper level.

{1)

Liquid Penetrant Examination {PT)

{2)

The inspector observed the in-process PT examinations as

indicated below.

The observations were compared with the

inspection attributes of the applicable procedure and the

ASME B&PV Code to verify the performance of acceptable

examinations.

Examinations Observed

Drawing

Item

Welds/Component

11548-WMKS-0127G2

MC-112

w.:1-WF

11548-WMKS-0127G2*

MC-113

W-1-VF

11548-WMKS-0127C2

MC-079

W-4-KS

Magnetic Particle Examination {MT)

The inspector observed in-process MT inspection of the

following weld and compared the inspection with the

applicable procedure and the ASME code to verify performance

of an acceptable examination:

Drawing 11548-WMKS-RC-R-1.2 - Weld W-1-01 {Item MC-252) {RV

.Head to Flange Weld, 358" to 537")

  • *

(3)

Ultrasonic Examination (UT)*

The inspector observed calibration activities and portions

of the in-process UT examination for the weld indicated

below:

The weld was inspected using 0°, 45°, and 60°

transducers. The inspector compared the examination with

the applicable procedures and the ASME B&PV Code to verify

that an acceptable examination.was performed.

Drawing 11548-WMKS-RC-R-1.2 - Weld W-1-01 {Item MC-252) {RV

6

(4)

Visual Examinations (VT)

The inspector observed the in-process VT examination of the

pipe supports noted below.

The observations were compared

with the applicable procedure and the ASME B&PV Code to

verify performance of acceptable inspections.

Examinations Observed

Drawing

11548-WMKS-OlOlGl

11548-WMKS-OlOlGl

(5)

Eddy Current Examination (ET)

HG-303

HG-304

Welds/Component

HOOlA

HOOlB

For the current outage, only tubes in steam generator (S/G)

B were being examined.

All tubes in the S/G were being

inspected full length using a 720BPRMS BOBBIN coil probe.

BOBBIN coil data was being collected at 400, 200, 100, and

10 KHz.

In addition, Rotating Pancake Coil (RPC)

inspections will be performed in the low flow area for 301

tubes and for evaluating BOBBIN coil inspection results as

needed.

As of March 24, 1993, the BOBBIN coil inspection

had been completed for approximately 40% of the tubes.

Seventeen (17) indications

(5 hot leg and 12 cold leg) of

tube wall degradation of 20-29% of wall thickness had been

identified. Three (3) indications (2 hot leg and 1 cold

leg) of tube wall degradation of 30-39% of wall thickness

had been identified.

No indication greater than 40% wall

degradation had been identified.

The inspector observed data acquisition for the following

tubes:

ROW

COLUMN

ROW

COLUMN

11

64

3

52

14

64

3

51

9

64

3

50

8

64

3

49

(6)

7

In addition, the analysis process was observed for the

following tubes:

ROW

COLUMN

ROW

COLUMN

19

13

11

46

18

13

12

46

17

13

13

46

16

13

14

46

15

13

9

13

8

13

Personnel Qualifications

The inspector reviewed personnel qualification documentation

as indicated below for examiners who performed the

examinations detailed in paragraphs (1), (2), (3), (4), and

(5) above.

These personnel qualifications were reviewed in

the following areas: employer's name; person certified;

activity qualified to perform; current period of

certification; signature of employer's designated

representative; basis used for certification; and, annual

visual acuity, color vision examination, and periodic

recertification.

Method

PT

MT

UT

VT

ET

ET

ET

PT

MT

UT

Examiner Records Reviewed

Level

Employer

I I

VCR

I I

VCR

I I

VCR

I I

VCR

I I

.kl

!{Trainee) .W

I II

.kl

I I

VEPCO

I I

VEPCO

II

VEPCO

Number

6

6

6

1

2

1

2

2

2

2

In addition, qualification records for one VEPCO level III

(PT, MT, VT, ET, RT, and UT) examiner was reviewed.

(7)

Equipment Certification Records

Equipment certification records as listed below, for

equipment used in the inspections detailed in paragraphs

(1), (2), (3) and (5) above, were reviewed to ensure

compliance with all applicable requirements.

RESULTS

Equipment Type

Penetrant Cleaner

Penetrant

Penetrant

Penetrant Developer*

UT Couplant

UT Transducer

UT Transducer

UT Transducer

UT Instrument

MT Particles

ET MIZ-18A RDAU

ET MIZ-18A RDAU

ET Cal Standard

ET Cal Standard

ET Cal Standard

ET Cal Standard

8

Equipment

Identification

Batch 36A4

Batch 130A47

Batch 919Y47

Batch 216K6

Batch 092031

Serial M02103

Serial J29303

Serial Ll9134

Serial 9286704

Batch 9ID016

Serial W03101

Serial W05052

MGT-012-92

MGT-016-90

AD-021-89

AB-010-91

In the areas inspected, no violations, or deviations were identified.

In ~eneral, a good lSI program was in place with good implementation.

Examination procedures meeting code requirements were being used and

inspections were being performed in a conscientious manner by qualified

personnel.

3.

Flow Assisted Corrosion (FAC) (Erosion/Corrosion) Program (49001)

The inspector performed a review of the licensee's FAC piping inspection

program.

The program is detailed in the following documents:

General-Nuclear Standard STD-GN-0033, Revision 3, Secondary Piping

and Component Inspection Program

VPAP-0807, Revision O, Secondary Piping and Component Inspection

Program.

Mechanical Engineering Implementing Procedure ME-022, Revision 3,

Engineering Evaluation Procedure for UT Inspected Components

Mechanical Engineering Implementing Procedure ME-023, *Revision 0,

Change Notice 1, CHEC-NDE Software Control

SSES-2.12, Revision 0, Controlling Procedure for Design

Engineering Evaluation of UT Inspected Components

NDE-UT-104, Revision 1, Ultrasonic Thickness Examination

a.

9

The following describes various aspects of the licensee's program:

A long term FAC program has been implemented at Surry.

The

licensee's method of predicting which systems are most

susceptible to FAC is EPRI CHECMATE Codes.

The licensee's FAC program includes the systems that have

been predicted to be susceptible to FAC.

The model ranks

each system's components according to their FAC

susceptibility.

The licensee's primary basis for selecting components for UT

inspection at the next outage is the results from the

predictive analysis.

Engineering judgement, results of

predictive analysis, industry experience and results from

previous UT inspections are used to select supplemental

inspection locations.

The following systems are included in the licens~e's FAC

program:

Feedwater

Condensate

Feedwater Heater Drains

Moisture Separator Drafns

_

Moisture Separator Reheater Drains

Extraction Steam

,

Steam Generator- Slowdown

Main Steam

Main Steam Drains

Auxiliary Steam

Auxiliary Feedwater Pump Steam Supply

Crossover and Crossunder Piping

The following components are included in the E/C program:

Control Valves/Check Valves

Tees and Branches

Expanders and Reducers

Flow Nozzles and Orifices

Exit Nozzles

Elbows and Reducing Elbows

Strai~ht Pipe Sections

Heater Drain Tanks

Reheater Drain Tanks

Pump Casings (heater drain and condensate pumps)

Main condenser (internal sparger, expansion joints)

UT thickness measurement procedures are approved in

accordance with the licensee QA program.

Procedures define

methods for: performing UT measurements, grid spacing

criteria, ensuring that followup inspections are taken at

I

I

10

the same locations as the previous inspections, ensuring the

use of certified inspection personnel, analYzing the results

of UT measurements, and establishing acceptance criteria.

Minimum wall thickness (tmin) requirements for safety-

related and non-safety related piping are based on code

allowable minimum wall thickness.

The licensee's method of analyzing UT data includes:

calculating the wear rate (wr) based on point to point

measurements, .band method, area method, and average method;

predicting the thickness (t) at the next refueling outage

based on tpredicted = tmeasured - wr X current operating eye le

time; determination of current acceptance based on tmeasured >

tminimum and tpredicted > tminimum; and calculation of remaining

life based on remaining life= (tmeasured - tminimum) divided by

the wr.

Repair and replacement of safety-related and balance of

plant eroded components is covered by the licensee's R&R

program meeting ASME Section XI.

Welding and NDE of repairs

and replacements are accomplished by qualified personnel and

suitable procedures for safety-related and balance of plant

piping.

Corporate

program.

program.

Committee

Engineering has responsibility for the FAC

The program is covered by the licensee's QA

The licensee's Management Safety and Review

(MSRC) reviews the FAC program.

b.

In addition to review of the program, as detailed in the documents

listed above, and discussion of the program with the responsible

engineer,- the inspector reviewed the fo 11 owing outage documents:

Seconda~y Piping and Component Inspection Program dated

October 2, 1992 and updated on March 3, 1993

Design Change Number 92-67-2, MI Secondary Piping

Replacements Surry Unit 2, including Field Changes 1

through 5

The Inspection Program (Outage Plan) included 80 piping components

from l" to 24" in diameter.

In addition the plan included a

number of other* components such as, mairi condenser, crossunder

piping, valves, steam generator "B" feedring, etc. The Design

Change was for replacement of a number of piping runs and

components in the Feedwater, Condensate, Steam Drains, and

Extraction Steam systems because of FAC.~ The piping was being

upgraded to Chromium - Molybdenum (CR-MO) steel.

11

The inspector also observed the following field activities to

verify inspection grid layout and UT wall thickness measurements

were being accomplished in accordance witb procedures:

Results

UT inspection of Component 2-CN-PPS-110 on drawing 11548-

WFPD-12 *

UT inspection and grid layout of components 2-SD-PSF2-284

and 2-SD-PPS-605 on drawing 11548-WFPD-104

Grid layout of components 2-SD-PSF2-299 and 2-SD-PPS-623 on

drawing 11548-WFPD-106

Personnel certification records were reviewed for NOE

examiners performing the above activities.*

The licensee has a very strong, pro-active FAC program with strong

corporate and site support and dedicated resources.

EPRI developed

computerized programs CHECMATE and CHEC-NDE are used for in the

selection of susceptible components and evaluation of inspection

results. Over SOOO_components per unit are included in the program.

FAC degraded piping components are being routinely identifi~d and

replaced with upgraded CR-MO steel.

In the areas inspected, np violations or deviations were identified.

4.

Steam Generator (S/G) Feedwater Nozzle Inspections

See NRC Report 50-280, 281/92-09 for documentation of a previous

inspection of this area.

A number of PWR plants have identified thermal fatigue cracking of

piping at the S/G Feedwater nozzle.

The tracking was attributed to

thermally induced fatigue caused by introducing relatively cold

feedwater into the main feedwater pipe upstream of the S/G.

This

cracking problem was identified in 1979 and NRC Bulletin 79-13 was

issued to require inspection and replacement of defective feedwater

piping components.

B~~ed on the currently identified cracking, the pipi~g components at

North Anna steam generator nozzles were inspected and cracks were found

in loops "A" and "C".

The following actions were performed by the

licensee:

Other utilities were surveyed to determine industry experience.

A history" of inspections and pipe replacement activities, since

issue of NRC Bulletin 79-13, for the affected piping was compiled

for North Anna and Surry.

12

A metallurgical analysis was performed on the cracks found at

North Anna.

Based on the track depth at North Anna, a crack growth rate was

established.

Based on a projected crack growth rate and the previous

replacements of the affected piping at Surry, a scheduled

augmented inspection was developed for Surry and North Anna.

Licensee Report, Thermal Fatigue Cracking of Feedwater Piping North Anna

Power Station- Unit 1, dated February 12, 1993, documents the above

actions.

The inspector reviewed the report and found it to be a very

thorough appraisal of the problem with realistic future inspection

schedules recommended.

In the areas inspected, no violations or deviations were identified.

5.

Safety Related Pipe Welding (55050)

The applicable code for safety-related pipe welding observed is USA

Power Piping Code 831.1.0 - 1967.

The inspector observed in-process

welding and reviewed in-process records as indicated below to determine

whether these activities were being performed in accordance with

applicable codes, standards and regulatory requirements.

The inspector observed fitup, in-process welding, and the final weld

surface for welds 1, 2, 3, 4, 5, 9, 11, 13, 14, and 16 on drawing

DCP-12-E237.

In add.ition, final weld surfaces were observed for non-

safety-related welds 3, 4, 5, 7, 8, and 10 on drawing DCP-67-E210.

For

these welds, the inspector reviewed in-process weld records and examined

weld appearance, weld material control, use of correct weld material,

use of correct welding procedure, and welder qualification and general

knowledge and ability.

In the areas inspected, no violations or deviations were identified.

6.

Licensee Action on Previous Inspection Findings

(Closed) Violation 280/92-09-01, Failure to Follow Procedures and

Instructions for NDE of Piping

This violation involved failure to perform ISI (VT and PT) inspections

of a Recirculation Spray Ring in accordance with Technical Specification

and procedure requirements.

Only 9" bands around the header, in lieu of

100% of the surface, were VT inspected.

In addition, PT testing was

being performed without removing blotches of paint and other foreign

material .

13

The licensee's letter of response, dated June 8, 1992, was reviewed and

found to be acceptable.

The inspector discussed the corrective-actions

with responsible licensee personnel and reviewed documentation of the

following corrective actions:

All examinations on the ring header were re-performed.

The NOE examiner who performed the PT inspections without removal

of foreign materials was re-trained and re-tested.

All. contract NOE personnel were instructed on the importance of

following procedures and were required to re-review the

requirements of the surface examination NOE procedures.

All inspections performed by the individual were reviewed and a

random sample of his inspections were re-performed by licensee

qualifted NOE examiners ~ith no problems being identified.

Records for the Spray Ring VT inspection performed during the last

outage were reviewed and no problems were identified.

In

addition, a licensee NDE examiner recalled observing part of that

inspection and indicated the inspections were performed correctly.

Based on review of the above corrective actions, this item is closed.

7 .. Exit Interview

The inspection scope and results were summarized on March 26, 1993, with

those persons indicated* in paragraph 1.

The inspector described the

areas inspected and discussed in detail the inspection results.

Proprietary information is not contained in this report.

Dissenting

comments were not received from the licensee.

8.

Acronyms and Initialisms

ANII

ASME

B&PV

CN

CR-MO

-

EPRI

ET

FAC

ISI

MS

MSRC

MT

NOE

NRC

NRR

PSI

PT

Authorized Nuclear Inservice Inspector

American Society of Mechanical Engineers

Boiler and Pressure Vessel

Condensate System

Chromium Molybdenum

Electric Power Research Institute

Eddy Current Test

Flow Assisted Corrosion

Inservice Inspection

Main Steam System

Management Safety and Review Committee

Magnetic Particle Testing

Nondestructive Examination

Nuclear Regulatory Commission

Nuclear Reactor Regulation

Preservice Inspection

Liquid Penetrant Testing

.,

PWR

QA

QC

RC

. RDAU

RII

RPC

_R&R

RV

SD

SER

S/G

SSES

SUADM

-

UT

VT

VCR

VEPCO

-

VPAP

-

tl

WO

wr 14

Pressurized Water Reactor

Quality Assurance

Quality Control

Reactor Coolant

Remote Data Acquisition Unit

Region 2

Rotating Pancake Coil

Repair and Replacement

Reactor Vessel

Steam Drains

Safety Evaluation Report

Steam Generator

Surry Site Engineering Services

Surry Administrative Procedure

Ultrasonic Testing

Visual Testing

Virginia Corporation of Richmond

Virginia Electric and Power Company-

Virginia Power Station Administrative Procedure

Westinghouse

Work Order

Wear Rate