ML18152A416

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Insp Repts 50-280/89-11 & 50-281/89-11 on 890515-19.No Violations or Deviations Noted.Major Areas Inspected:Plant Chemistry,Radwaste,Effluent Monitoring,Environ Monitoring & Review of Semiannual Annual Release & 1988 Environ Repts
ML18152A416
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/09/1989
From: Dan Collins, Stoddart P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A417 List:
References
50-280-89-11, 50-281-89-11, NUDOCS 8906280121
Download: ML18152A416 (12)


See also: IR 05000280/1989011

Text

UNITED STATES

NUCLEAR R EGU LATO RY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

JUN i 2. 1989

Report Nos.:

50-280/89-11 and 50-281/89-11

Licensee:

Virginia Electric and Power Company

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.: DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

May 15-19, 1989

Inspector: riY' /J? ' ~

-~ P. G. Stoddart

Approved by: .£2, //1 '~

Scope:

D. M; Collins, Acting Chief

Radiological Effluents and Chemistry Section

Emergency Preparedness and Radiological

Protection Branch

Division of Radiation Safety and Safeguards

SUMMARY

Date Signed

(,-'Y-if9

Date Signed

Thj s routj ne, unannounced inspection was in the areas of pl ant chemistry,

radwaste, effluent monitoring, environmental monitoring, and review of

Semiannual Annual Radioactive Effluent Release Reports and 1988 Environmental

R~port.

Results:

Review of the Semiannual Effluent Release Reports for 1988 indicated that the

licensee continued to release radioactivity in liquid effluents and radioactive

iodines and particulate~ in gaseous effluents at a rate among the highest of

licensees in Region U.

There appeared to be signs of progress in the

replacement of process* and effluent radioactivity monitors which had been

either out-of-service or radi cacti vely contaminated for over six years.

An

oxygen monitor in the waste gas system had been authorized for a design change

after being out-of-service for approximately two years.

The plant chemistry

program was functioning well and chemistry technician training was adequate;

the chemistry program and the chemistry technician training program were

considered to be licensee strengths.

Sludge lancing results from the 1988

shutdowns indicated continuing problems with system piping corrosion,

especially in Unit 2.

In the areas inspected, violations or deviations were not identified .

8906280121 890612

PDR

ADOCK 05000280

G

PNV

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1.

Persons Contacted

Licensee Employees

REPORT DETAILS

A. Brown, Instructor, Licensed Operator Training

J. Carson, Engineer, Instrumentation and Electronics

  • D. Erickson, Superintendent, Health Physics
  • B. Garber, Supervisor, Health Physics
  • M. Kansler, Site Manager

C. Mehalie, Instructor, Training Center

L. Morris, Engineer Maintenance

  • E. Swindell, Supervisor, Chemistry

Other licensee employees contacted during this inspection included

engineers, operators, security force members,

technicians, and -

administrative personnel.

NRC Resident Inspector

  • W. Holland
  • Attended exit interview

2.

Status of Inspector Followup Items and Information Notices (84750)

(Closed) Information Notice (IN) 50-280, 281/88-IN-31:

Steam generator

tube rupture analysis defj ci ency.

The inspector determined that the

licensee had received the IN and had initiated remedial action.

On the

basis of conservative analyses, the licensee*determined that the Exclusion

Area Boundary (EAB) doses would be within 10 CFR Part 100 dose limits but

would exceed the Standard Review Plan (SRP) 15.6.3 criteria. The licensee

also determined that, on the basis of conservatisms in the above analyses,

the radiological consequences of the postulated event would be less than

calculated.

The licensee concluded that, while the analysis using

conservative assumptions produced radiological results higher than

SRP 15.6.3 criteria, the licensee would actively participate in the

Westinghouse Owners Group (WOG) program, along with other util'ities, to

seek a generic resolution of this potential safety concern.

When the WOG

work is finalized, the licensee intended to reevaluate the plant's steam

generator tube rupture accident analysis and would then submit the results

of NRR for review.

On the basis of the foregoing discussion, this matter

was considered closed for tracking purposes.

(Closed) IN 50-280, 281/88-IN-22:

Disposal of sludge from onsite sewage

treatment facilities.* Inspection Report (IR) No. 50-280, 281/88-13,

Section 3, page 2, described the method used to dry sludge for packaging

for shipment to the Surry County (VA) landfill.

Shipments were normally

2

made about twice a year in volumes of 20 to 30 cubic feet (ft3) per

shipment.

During this inspection, the inspector reviewed the licensee's

procedure for monitoring of shipments of dried sludge to the Surry County

(VA) landfill.

The licensee's procedures for preventing the inadvertent

shipment of radioactive material to the county landfill were considered to

be adequate.

On the basis of the foregoing discussion, this matter is

considered closed.

(Open) Inpsector Followup Item (IFI) 87-02-03:

Resolve the inoperability

pro bl em of component cooling service water monitor RM-SW-107.

The

existing monitor had been out-of-service since approximately 1978, when

fouling of pumps and pump intakes precluded reliable automated sampling.

As

built,

the

monitor

took

samples

from ,four

separate

service-water-to-component-cooling-water heat exchangers by means of four

pumps.

Debris in the service water (river water) caused plugging of

sampling lines and jamming of pumps on a frequent basis and made the

monitor essentially useless, at which time the licensee opted for periodic

sampling and analysis of the service water.

During this inspection, the

inspector was informed that this monitor problem had recently been

elevated to "Type 3" engineering study status the licensee's most urgent

priority.

Consideration was being given to installing a detector in a

"well". on the manway cover of one of the service water heat exchangers;

however, no firm solution or date had been established.

Since this matter

had not been fully resolved, it remained open for tracking purposes.

3.

Chemistry:

Primary and Secondary Cool ant Chemistry and Radiochemistry

(84750)

At the time of this inspection, both units had been shut down for over six

months.

A number of chemistry-related operations had taken place during

the shutdown and in the interval si nee the chemistry inspection of

February 16-19, 1988 (IR No. 50-280, 281/88-06).

Pipe-thinning continued to be a major concern and the licensee was

participating actively in industry efforts to minimize the problem.

Sludge lancing of Unit 1 steam generators in the Spring of 1988 produced

43 pounds of sludge from A steam generator, 35 pounds from B steam

generator and 58 pounds from C steam generator.

Lancing of Unit 2 steam

generators in Fall of 1988 produced 440 pounds from A steam generator,

170 pounds from B steam generator and 180 pounds from C steam generator.

These quantities were consistent with the sludge removed from Units 1 and

2 during the 1986 outages

(see

IR

No.

50-280,

281/88-06,

Paragraph 4.a.(2)) and were indicative of continued piping thinning. The

licensee's chemistry program had been able to monitor plant chemistry

within the owner's group guidelines but this appeared to have had little

effect on the amount of corrosion material removed * from the steam

generators.

-

The licensee contracted with an outside company to evaluate corrosion

product transport in the secondary systems of both units as a result of an

increase in secondary coolant pH from 8.8 to 9.16 and to identify, if

3

possible, differences in plant chemistry which occurred over the history

of the Surry units.

The change in pH resulted in no apparent improvement

in iron transfer, but transport of nickel and copper was found to have

jncreased.

A decrease in the concentration of dissolved oxygen in the

secondary coolant as the result of increased water purity control was seen

as the only apparent change in water chemistry since about 1980.

The inspector reviewed logs and records of completed chemical analyses and

reviewed trending graphs for principal plant chemical parameters.

The licensee had installed an on-line monitoring system for principal

plant parameters and was in the process of testing and calibrating the

system prior to formal acceptance.

The system was to provide essentially

continuous on-line monitoring and to provide computerized data logging.

The system will be backed up by frequent grab sampling and analysis as a

quality control measure.

Approximately five percent of condenser tubes were eddy current tested

during the last shutdowns.

This was up from four percent in previous

inspections but did not reach the eight percent level forecasted in IR No.

50-280, 281/88-06.

The condenser tubes were hydrolased during the last

shutdowns (1988).

The licensee employed a private consultant to review plant chemistry data

to determi~e if any significant changes had taken place in the chemistry

of the secondary coolant since 1980.

A licensee representative stated

that the only apparent change was in a lowered concentration of dissolved

oxygen.

Graphic trending was being employed extensively by the chemistry

department and by other licensee groups.

Employment of trending was

anticipating to increase when the on-line chemistry monitoring system

became operational.

Licensee chemistry representatives stated that the biggest chemistry

problem recently had been sulfate throw from the condenser demineralizers.

A system was being installed to separate resins for better regeneration

and less fragmenting of resin beads.

The licensee estimated that anion

resins would be regenerated every second cycle, or one bead every 10 days.

Cation resins were expected to be regenerated about once each five days.

It was considered that such a program would reduce sodium concentrations

in the secondary system to about 1 ppb.

The licensee had not seen

problems with silica to date.

Some calcium was apparently being

introduced into the system from makeup but was seen primarily as hideout

return during startup and shutdown.

The licensee had experienced very little river water intrusion since

titanium condenser tubes were installed.

Based on the above, the licensee's chemistry program was a licensee

strength .

4

No violations or deviations were identified.

4.

Chemistry: Training and Staffing (84750)

The chemistry staffing level, as of the time of this inspection, was 22,

including the Chemistry Supervisor.

The Chemistry Supervisor reported to

the Superintendent of Technical Services, who reported to the Assistant

Station Manager for Operations and Maintenance, who, in turn, reported to

the Station Manager.

The inspector was informed that, as a result of

increased attention to plant chemistry, authorization had recently been

given to add three new positions to the chemistry staffing level.

Training of chemistry personnel was coordinated through the licensee's

onsite training center.

The inspector inspected the chemistry training

facilities, discussed chemistry training with members of the training

center staff, and reviewed selected portions of chemistry lesson plans,

self-study materials, training aids and visuals, and reviewed typical

examinations and ~xamihation results.

The two chemistry instructors were

former plant chemists and appeared to have a good background in the

various phases of chemistry applicable to nuclear power plants.

Special chemistry training facilities included a full equipped chemistry

laboratory and an operating mockup of the licensee's High Range Sampling

System (HRSS) or Post-Accident Sampling System (PASS).

Formal training requirements were divided into eight modules or

11 steps,

11

with chemists-in-training expected to complete each

11 step

11 within a

nominal six-month period.

The licensee had been generally successful in

biring new chemistry staff members with a minimum of a Bachelor's degree

in chemistry or a related field such as biology.

In each step, an

individual would be assigned to one week in training status in each

six-week segment, with each week of training devoted to 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> formal

classroom training,

11 on-the-job

11 training or a combination of both.

The

fully qualified chemists subsequently received a minimum of 96 ho~rs of

continued training annually.

A low turnover of chemistry personnel was demonstrated by the training

status, with only five out of 22 not having completed the full four-year

training program.

A 1 i censee representative stated that no contractor

chemistry personnel were employed at the site.

The low turnover rates and the resultant continuity of s'taff, backed up by

a commendable training program and adequate management support, were

licensee strengths.

No violations or deviations were identified.

5.

Post Accident Sampling System (PASS) (84750)

The licensee's PASS was designated by the licensee as the HRSS and will be

referred to in this inspection report as HRSS.

The inspector discussed

~ -;,c;:;;.*

'----:,

5

the HRSS with licensee representatives of the Chemistry Department and of

the Training Department.

The Chemistry Department had principal

responsibility for operation of the HRSS, while the Training Department

had responsibility for training and periodic training of Chemistry

technicians in HRSS operation.

Licensee's administrative procedure ADM 9.7 required a monthly status

report on the operational availability of the HRSS.

The ADM 9.7 status

report of May 16, 1989, showed the PASS at an overall availability rating

of 75 percent(%).

For reactor coolant analyses, the boron analyzer had

been inoperable since May 16, 1989, because of a failed memory board;

however, the licensee retained the alternative of procuring a diluted grab

sample for local analysis.

The status report incorrectly showed the

availability of the containment air sampling module of the HRSS as 100%;

however, the report details showed TV'."'HC-208B, as inoperable since

February 9, 1989, which prohibited sampling from the Unit 2 containment

and availability should have been 55%, not 100% as stated.

The Unit 1

containment sump sampling was reported to have been out-of-service since

May*of 1987; repairs were to have been made during the current outage of

Unit 1, but licensee representatives indicated that the needed repairs had

not been completed as of, the time of this inspection.

The. inspector discussed HRSS training of Chemistry technicians with

licensee representatives and reviewed training plans and self-study

-material. Training plans and self-study material appeared to be adequate.

It was noted by the inspector that revision of this material had been

undertaken and was in a near-final draft form.

No violations or deviations were identified.

6.

Semiannual Effluent Release Reports (84750)

The inspector reviewed the licensee's Semiannual Radioactive Effluent

Release Reports for January-June 1988 and July-December 1988.

The reports

appeared to be complete and were submitted on a timely basis.

The

contents of the reports were discussed with licensee representatives.

In a comparison of site radioactive effluents with other Region II sites,

on a "per unit" release basis, with 22 other operating pressurized water

reactor (PWR) units, it was observed that releases of noble fission

product gases and gaseous and liquid tritium were below Region II averages

for 1988 unit releases.

However, releases of radioiodines and

particulates in gaseous (airborne) releases were a factor of 8.4 greater

than Region I I unit averages and were the highest in Region I I.

The

inspector and licensee representatives discussed these releases and

concluded that most of the activity was probably the result of fuel

defects.

The licensee shut one unit down after a short run because of

fuel 1 eaks, and took action to remove the defective fuel.

The unit had

not been restarted as of the end date of this inspection .

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6

Liquid radioactive releases of fission and activation products for 1988

were lower than.licensee's releases in any year since 1980.

This was

considered to be partially attributable to improvements in radioactive

waste processing and partially to extended plant shutdowns during 1988.

The licensee had previously recognized that there was room for improvement

in the areas of radwaste processing and* radwaste management and at the

time of this inspection was in the process of contracting an extensive

radwaste building designed to provide improvements in several areas of

radwaste processing, including a

11 super compactor

11 for dry wastes, a

solidification system for resins and high activity liquids, and improved

capacity for demineralizer treatment of liquid wastes.

The licensee

tentatively projected a December 1990 completion date for that facility.

Other compensatory measures already in place to minimize or reduce liquid

effluents included a plant-wide leak reduction program, administrative

control measures to eliminate introduction of orqanics into the radio-

active drains system, and the installation of larger capacity

demineralizers in the liquid radwaste treatment system.

While the liquid

radwaste treatment system normally operated with one filter vessel and two

demineralizers in series, the system had the capability of adding two more

demineralizers in series.

Gaseous effluent releases occurred from two principal paths; the-gaseous

radwaste treatment system and the ventilation effluent high efficiency

particulate air* (HEPA) filter and charcoal absorber systems.

The gaseous

radwaste treatment system processed off gases from the pl ant primary

coolant system by holdup to allow for radioactive decay of short-lived

fission product noble gases and gaseous neutron activation products.

The

ventilation exhaust treatment system used HEPA fi 1 tration to remove

radioactive particulate material from ventilation exhaust treatment

systems and absorption of gaseous radioiodine on activated charcoal beds.

The 1 i censee al so reported that there were no unplanned releases of

radioactive materials for the period January through December 1988.

Operability of radioactive liquid and gaseous process and effluent

monitoring instrumentation was also reported by the licensee.

The

Component Cooling Service Water Monitor ( RM-SW-107) continued to be

out-of-service.

The inspector noted and discussed with the licensee that

this monitor had been out-of-service essentially continuously since

approximately 1978.

In the interim, the licensee had performed alterative

surveillance of this potential release pathway through regular sampling

and analysis, as provided by the Technical Specifications.

Licensee

representatives were reminded that the purpose of the alternative

surveillance provisions of the Technical Specifications (TSs) was to

provide the licensee with a reasonable but unspecified period of time in

which to repair or replace the monitor.

The licensee was informed that it

was not the intent of the TSs to permit the 1 i censee, in effect, to

permanently change the design basis of the monitor and circumvent the

basic function of the monitor indefinitely.

The licensee was also

reminded that two related monitors (RM-SW-105/106) were, for practical

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7

purposes, out-of-service as the result of high radiation background

readings for approximately the same time period as the result of

radioactive co-ntamination of the Component Cooling Water Circulatory

System; these were not TS monitors and were not requfred to be reported.

The inspector was notified that a high priority level Design Change had

been initiated for installation of redesigned monitors to replace all

' three monitors (RM-SW-105/106/107).

No specific date was defined for

placing the redesigned monitors in service.

Since an existing IFI

(50-280, 281/87-02-03) was already in place for tracking resolution of the

inoperability of RM-SW-107, the licensee was notified that IFI 50-280,

281/87-02-03 would remain as an open item for tracking purposes.

The licensee also reported that the Waste Gas Holdup System oxygen

monitor, which has the function of assuring that an explosive mixture of

hydrogen and oxygen gases does not develop in the Waste Gas Holdup System

by verifying that the percentage of oxygen in the system does not exceed

four percent, continued to be out-of-service.

The inspector was notified

that the replacement of the oxygen monitor had been assigned a high

priority for design change, but no completion date was committed to by the

licensee.

No violations or deviations were identified.

7 .

Audi ts ( 84 7 5 0)

The inspector reviewed licensee audit files for audits concerning matters

within the scope of this inspection and conductd or issued since the

previous inspection (IR No. 50-280, 281/88-13, issued May 26, 1988).

Audit S88-19, dated August 22, 1988, was concerned with Health Physics and

Radiological Environmental Monitoring.

Four findings, three concerns and

two comments were identified and the auditor noted that the discrepancies

indicated an overall weakness in the effectiveness of the Radiation

Protection Program.

The licensee's responses to the audif findings

appeared to be timely and were considered to be adequate to meet the

specified concerns.

Audit S89-17, dated March 28, 1989,

11Qua 1 i ty Assurance Chemistry Audit,

11

and Audit S89-ll,

11 Process Control Program Audit,

11 dated April 18, 1989,

were also reviewed by the inspector.

Audit S89-ll had three findings

relating to purchasing, procurement, and onsite storage of shipping

containers for radioactive resins and the use of forms in radwaste

processing.

Two findings had been evaluated and corrected at the time of

the inspection, while resolution of the thi.rd matter was due after the end

date of this inspection.

No adverse findings were reported in

Audit S89-17, but two

11 observations

11 were dismissed.

Licensee's

responsiveness and timeliness of responses were considered adequate.

No violations or deviations were identified.

-*--::. .:.:.::-:-.;.~-::..,

.. , -----*

8

8.

Liquid and Gaseous Radwaste Processing (84750)

In Paragraph 6 of this report pertaining to the Semiannual Radwaste

Effluent Re 1 ease Reports, it was noted that certain effluents were in

excess of annual averages for operating PWRs in RII.

A summary of past

years' experience at Surry is illustrative.

Year

1988

1987

1986

1985

1984

1983

1982

1981

Effluent Releases, Curies Per Year (for 2 Units)

Liquids - Fission and

Activation Products

2.41E+OO

5.lOE+OO

8. 77E+OO

8.50E+OO

9.73E+OO

1. 45E+Ol

6.70E+OO

6. llE+OO

Gases

NobTe"Gases

3.66E+02

3.08E+02

1. 99E+03

2.07E+03

6.96E+03

5.49E+03

2.10E+04

1.40E+04

It should be noted that releases for 1987 and 1988 were lower than in

previous years; however, this could be largely due to the ongoing extended

plant shutdowns.

The licensee had earlier recognized that lower releases were practicable

and had developed a long-term plan for reducing the curie content of both

liquid and gaseous effluents.

One major feature of that plan was the new

consolidated radwaste processing facility, which was in an early

construction stage at the time of this inspection.

The present liquid radwaste processing system was based on five stainless

steel demineralizer vessels, each having a capacity of 30 ft 3 of resin and

a nominal flow rate of 50 gpm.

A typical operating configuration was

three vessels in series, the first containing a combination of activated

charcoal, cation resin and a mechanical filter, the second containing

cation resin, and the third containing mixed anion and cation resins.

Processing was normally on a once-through basis to a sampling or

monitoring task where the processed water was sampled and analyzed prior

to discharge under a radwaste release permit system.

Discharge from the

sampling or monitoring task was to the plant circulating water system

which in turn discharged to the James River.

Final control of discharge

in the event of error was provided by the waste release monitor,

RM-LW-108, an in-line scintillation monitoring system which in the event

of alarm would signal for the automatic termination of flow through

closure of the discharge control valve.

Post operational experiences with demineralizer resins as the method of

choice for plant-generated liquid radwaste had shown the present system to

be capable of operating within the permissible discharge limits of the

plant TSs and of other applicable State and Federal regulations and

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9

guidelines.

While the demineralizer system was technically capable of

reducing discharges by as much as a factor of 10 below the actual

discharges, the in-plant control of resin-depleting wastes such as oils,

sol vents, and detergents had been inadequate to prevent premature

aepletion of the demineralizer resins, thus reducing the effective

decontamination factor of the radwaste processing system.

To alleviate

this situation, the licensee implemented an action plan to eliminate or

minimize the introduction of resin-fouling materials.

Drains were

specially labelled, sinks were posted with signs restricting use, and

plant-wide indoctrination programs were held.

Parallel programs for

minimizing leaks plant-wide*were also initiated.

The new radwaste faci 1 ity, under construction at the time of this

inspection, was to have added capacity for holdup and reprocessing, and

for additional flexibility in processing methods.

Leak reduction programs were al so established for waste gas systems.

Reduction of leaks would permit use of longer decay times for gas holdup

tanks, thus reducing the concentration of short-lived noble gases in decay

tank releases and could also reduce the fraction of short-lived noble

gases being discharged via the system and to maintain the subatmospheric

containment pressure used for the licensee

1 s reactor units.

No violations or deviations were identified.

9.

Radiological Environmental Report (84750)

The inspector reviewed the licensee

1s Radiological Environmental Report

for 1988 and discussed the report with licensee representatives.

The

report appeared to be complete and to contain the necessary information.

Analyses of river water samples taken near the plant discharge at

downstream locations failed to show any gamma-emitting fission products in

excess of the Lower Limit of Detection (LLD); however, tritium, above

anticipated background levels-of approximately 300 pCi/1, was measured in

16 of 24 quarterly composite samples, with an average of 411 pCi/1 and a

range of 150 to 820 pCi /1.

The 820 pCi /1 sample, taken at the Surry

Stition water intake, was confirmed by reanalysis.

The average tritium

activity of the Surry Station liquid effluent was 450 pCi/1, with a range

of 420 to 490 pCi/1.

For control stations, the average concentration was

280 pCi/1, with a range of 140 to 440 pCi/1.

All of the samples were

analyzed at sensitivity levels well below the required LLD of 2E+03 pCi/1.

Analyses of shoreline sediments indicated the presence of one man-made

nuclide Cs-137 in one sample.

The activity of the sample was 16.3 pCi/kg

(dry weight).

All other samples showed only anticipated levels of the

naturally-occurring nuclides.

Analyses of milk from local dairies did not indicate the presence of I-131

in any of 60 samples. * Naturally-occurring K-40 was detected in all

samples.

Cs-137 was identified in two out of 60 samples, with an average

~* * .. '*? ::~~-

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10

activity of 7.5 pCi/1 and a range of 6.3 to 8.8 pCi/1; required LLD was

18 pCi/1.

The CS-137 was considered to be a remnant of past atmospheric

global weapons testing.

Twelve milk samples were collected in participation with the State split

sampling program and analyzed for Sr-89 and Sr-90;

Sr-89 was not detected

in any samples.

Sr-90 was detected in 10 of 12 samples at an average

level of 2.45 pCi/1 and a range of 0.71 to 4.5 pCi/1.

It was noted that

during the preoperational radiological monitoring program for the

licensee's site, Sr-90 was routinely detected in milk samples at levels of

5.2 to 13 pCi/1.

Direct radiation in the plant environs was monitored by a thermoluminscent

dosimetry (TLD) array placed in two concentric rings around the plant

site, one ring at the site boundary and the other at approximately five

miles distance in each of 16 sectors. Supplemental TLDs were also placed

in special interest locations such as population areas and nearby

residences and at distant locations for control purposes.

Dose

measurements for the sited environs averaged 6.3 mR/standard month; with a

range of 4.2 to 9.2 mR/standard month.

Control station doses were

reported at an average 5.7 mR/standard month, with a range of 5.1 to 6.6

mR/standard month.

Natural radiation background at seal level has been

reported at 80 to 100 mR/year or approximately 6.7 to 8.3 mR/standard

month.

The licensee's plant TS 6.6.B.2 requires that a Land Use Census be

conducted annually within a five-miles radius of the plant.

The 1988 Land

Use Census reported that no changes had occurred which would require

changes to the Monitoring Program or to the dose calculational model.

Based on the inspector's review of the licensee's Environmental Report for

1988, it appeared that no significant environmental input had occurred as

a result of 1988 plant operations, that the report contained sufficient

information to meet regulatory guidelines for reporting, and that the

report was considered to be adequate.

No violations or deviations were identified.

10.

Exit Interview

The inspection scope and results were summarized on May 19, 1989, with

those persons indicated in Paragraph 1.

The inspector described the areas

inspected and discussed in detail the inspection results listed above.

Although proprietary information was reviewed during this inspection, none

is contained in this report.

Dis sent i ng comments were not received from

the licensee.

The Semiannual Radioactive Effluent Release Reports and the Radiological

Environmental Report for calendar year 1988 were reviewed and discussed.

The reports were determined to be adequate.

Releases of mixed fission and

activation products in liquid effluents and iodine 131 and particulates in

.... ::;::.

11

gaseous effluents were higher than average releases from all PWRs in

Region II for 1988.

The plant chemistry program appeared to be

functioning well and chemistry technician training- was adequate; the

chemistry program and the chemistry technician training program were

considered to be licensee strengths.

Sludge lancing results from 1988

shutdowns indicated continuing problems with system corrosion, especially

with respect to Unit 2.

In the areas inspected, violations or deviations were not identified.

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