ML18152A399

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Insp Repts 50-280/94-24 & 50-281/94-24 on 940807-0902.No Violations Cited.Major Areas Inspected:Plant Status, Operational Safety Verification,Maintenance & Surveillance Insps,Ler Followup & Action on Previous Insp Items
ML18152A399
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/09/1994
From: Belisle G, Branch M, David Kern, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A400 List:
References
50-280-94-24, 50-281-94-24, NUDOCS 9409270088
Download: ML18152A399 (15)


See also: IR 05000280/1994024

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

Report Nos.:

101 MARIETIA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/94-24 and 50-281/94-24

Licensee: Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

August 7 through September 2, 1994

Inspectors: /..u..; ~

~

M. W. Branc,Seniorlfusident Inspector

rW -<ii

fu.

S. G. Tingen~nt Inspector

D. M. Kern, Resident Inspector

Accompanying Personnel:* D. M. Tamai, Intern

Scope:.

D. R. Taylor, Resident

  • Inspector North Anna

. B 1 s e, Chi e

Reacto

Projects Section 2A

Division of Reactor Projects

SUMMARY

?/!' /9<1

Date -Signed

9/FP'f

DaeSigned

4fo~1

~

This routine resident inspection was conducted on site in the areas of ~lant

status, operational safety verification, maintenance and surveillance

inspections, Licensee Event Report fol.lowup, and action on previous inspection

items.

Inspections of backshift and weekend activities were conducted on

August 11, 18 and 26 and September 2.

~~9270088 940912

Q

ADOCK 05000280

PDR

2

Results:

Plant Operations functional area

The operator's prompt response to the August 20 Unit 2 C steam generator main

feed regulating valve closure prevented an automatic reactor trip

(paragraph 3.2).

Maintenance functional area

The licensee responded to a turbine driven auxiliary feedwater pump trip with

the appropriate amount of management attention and reasonable corrective

actions (paragraph 4.1).

The corrective action audit performed by the licensee identified an area that

warranted improvement.

The audit identified that root cause evaluations were

not always effective in preventing equipment problems from recurring

(paragraph 4.2).

An apparent violation with two parts was identified for failure to promptly

identify and implement effective corrective actions' for conditions adverse to

quality. The first part of the apparent violation involved not promptly

sampling both the auxiliary ventilation exhaust filter system trains following

a chemical release that occurred in the Unit 2 containment on June 16, 1994.

The second part of the apparent violation involved not promptly correcting a

condition adverse to quality when an engineering review identified that

certain circuits were not fully being functionally tested on a monthly basis

(paragraphs 6.1 and 6.2).

1.

REPORT DETAILS

Persons Contacted

1.1

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • H. Blake, Jr., Superintendent of Nuclear Site Services

R. Blount, Superintendent of Maintenance

  • D. Boone, Quality Assurance
  • D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

  • A. Friedman, Superintendent of Nuclear Training
  • B. Garber, Licensing

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Superintendent of Administrative Services

M. Kansler, Station Manager

C. Luffman, Superintendent, Security

  • J. McCarthy, Assistant Station Manager
  • D. Miller, Radiation Protection
  • A. Price, Assistant Station Manager
  • R. Saunders, Vice President, Nuclear Operations
  • K. Sloane, Operations

E. Smith, Site Quality Assurance Manager

T. Sowers, Superintendent of Engineering

  • B. Stanley, Station Procedures

J. Swientoniewski, Supervisor, Station Nuclear Safety

  • G. Thompson, Supervisor, Maintenance Engineering
  • E. Turko, Engineering

G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics,

security force members, and office personnel.

1.2

Management Changes

The following personnel changes were effective September 1:

W. Wigley, Manager, Nuclear Operations Support - Corporate, was

reassigned to a special project.

M. Kansler, Surry Station

Manager, replaced W. Wigley.

D.* Christian, Assistant Station

Manager, replaced M. Kansler. J. McCarthy, Superintendent of

Operations, replaced D. Christian. S. Sarver, Quality Assurance

Supervisor, Plant Operations, replaced J. McCarthy.

2

1.3

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • D. Kern, Resident Inspector
  • D. Tamai, Intern

D. Taylor, Resident Inspector, North Anna

  • S. Tingen, Resident Inspector
  • D. Verrelli, Branch Chief, Region II
  • Attended Exit Interview

Acronyms and initialisms used throughout this report are listed in

the last paragraph.

2.

Plant Status

Units 1 and 2 operated at power for the entire inspection period.

Condenser water box fouling from hydroids and eels increased during this

period necessitating water box cleaning and power reduction.

3.

Operational Safety Verification (71707, 42700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved.

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Biweekly ESF Inspections

3.1.1 EDG Fuel Oil System

The inspectors walked down the EOG fuel oil transfer system

located in the EOG rooms and diesel fuel oil transfer pump

buildings. Correct breaker position and valve alignment

were verified. Completed procedures for monthly fuel oil

system tests for 1994 were reviewed for completeness and

adequacy.

Equipment appeared to be in good overall

condition and housekeeping was acceptable.

3.1.2 Control Room Bottled Air System

The inspectors walked down the control room bottled air

system located in MER 3, Unit 1 cable vault and control room

stair well. Correct valve alignment, PCV regulator pressure

and bottled air pressure were verified.

Equipment was in

good overall condition and housekeeping was adequate.

3

3.2

Operator Response to Unit 2 C MFRV Closure

On August 20, the Unit 2 C MFRV failed closed. The MFRV's

controller was in the automatic mode of control when the valve

failed shut. Steam flow/feed flow mismatch and SG level error

annunciator alarms and closed position indication on the control

board for the C MFRV alerted the operator that an abnormal

condition existed. The operator immediately analyzed the

condition and placed the MFRV controller in manual and opened the

MFRV.

The lowest level noted in the C SG was 22%.

Failure of the

steam flow/feed flow signal comparator was determined to have

caused the MFRV to close. The signal comparator was replaced and

the C MFRV controller was returned to the automatic mode of

operation. The inspectors concluded that the operator's prompt

response to this event prevented the unit from automatically

tripping.

Within the areas inspected, no violations or deviations were identified.

4.

Maintenance and Surveillance Inspections (62703, 61726, 40500)

During the reporting period, the inspectors reviewed the following

maintenance and surveillance activities to assure compliance with the*

appropriate procedures.

4.1

TDAFW Pump Turbine Overspee~ Trip

On August 22, the Unit 2 TDAFW pump tripped on overspeed during

monthly surveillance test, 2-0PT-FW-003, Turbine Driven AFW

2-FW-P-2, revision 3.

The turbine operated for approximately

13 seconds and tripped on overspeed.

WO 297664-01 was initiated

to investigate/repair the governor valve.

The valve bonnet, stem

and packing were replaced.

The cause of the trip was determined

to be corrosion buildup on the stem in the area of the stuffing

box adjacent to the valve disc.

As immediate corrective action, the licensee initiated a new

surveillance for both units. Procedure O-MPM-1403-03, Terry

Turbine Governor Valve Stem Movement Check, revision 0, provided

instructions to manually exercise the governor valve stem in each

unit on a weekly interval. The procedure required the governor

power cylinder shaft pin and nut to be disconnected, and

measurements taken of the initial movement (breakaway) torque,

full stroke torque and full stroke length. These measurements

were followed by additional strokes to ensure free stem movement

and by linkage reconnection. The inspectors witnessed this

surveillance test performance on August 31.

Unit 1 tested

satisfactory.

On Unit 2, some governor valve stem binding was

exhibited.

Five pounds of torque greater than the breakaway

torque was required during stem travel. The licensee determined

that the governor had sufficient margin to overcome the binding.

However, the licensee reduced the time interval for the next

4.2

4

surveillance performance on Unit 2.

The next surveillance was

performed September 2 in lieu of waiting an entire week.

The

inspectors witnessed the surveillance on September 2.

Some

corrosion was evident; however, stem binding was not exhibited.

The inspectors reviewed the safety evaluation for this new

surveillance and attended the SNSOC meeting that approved it. The

SNSOC members also determined that a station JCO was needed to

adequately track the corrective action progress for governor valve

stem binding.

The surveillance procedure was effective for 30

days. After 30 days, SNSOC will review the effectiveness of the

corrective action.

As part of the longer term corrective action, the licensee ordered

chrome plated valve stems.

The chromed plated stems do not

exhibit the same corrosion as the nitrated stainless steel stems

which are currently utilized. Previously, the licensee had not

considered this as appropriate corrective action because these

stems are subject to blistering and peeling.

However, the

licensee determined that the chrome plated stems will provide a

greater assurance of pump availability than the nitrated stainless

steel stems are currently providing.

The licensee has experienced previous TDAFW pump trips. The

corrective actions are addressed in NRC Inspection Report Nos.

50-280, 281/94-17, 93-26 and 93-07.

The licensee's task team is

continuing to evaluate the trips to determine the root cause.

Differences have been identified in manufacturing the valve parts.

However, the consequences of these differences have not be

determined.

Due to recurring TDAFW pump trips, the licensee

performed a Substantial Safety Hazard Evaluation in accordance

with VPAP 2802, Notifications and Reports, revision 4.

As a

result of the evaluation, the licensee determined that a 10 CFR 21

report was necessary due to the recent TDAFW pump overspeed trips

that were attributed to corrosion in the governor valve which

caused the stem to bind.

The inspectors concluded the licensee was giving the issue the

appropriate amount of management attention and that corrective

.actions were reasonable.

The inspectors will continue to monitor

the licensee's long term and short term corrective actions.

QA Corrective Action Audit Review

The inspectors reviewed QA Audit 93-15, Corrective Action, dated

February 2, 1994.

This audit satisfied TS requirement

6.1.C.2.h.3. Areas inspected during the audit were the corrective

action associated with work requests, DRs, human performance,

operating experience, RCEs, nonconformance reports, potential

problem reports, LERs, JCOs, 10 CFR 21 reports and records.

The

audit concluded that with the exception of RCEs, the corrective

action program was effectively implemented.

5

The audit concluded that the RCE program was not always effective

in preventing recurring equipment problems.

Control Rod Urgent

Failures, Kaman Radiation Monitors, Appendix R emergency lighting

and !RPI were identified as examples of ineffective corrective

actions. The following criteria were utilized in determining if

corrective actions were effective:

The deficiency was two or more years old.

The deficiency had been identified and corrected three or

more times.

The deficiency was significant based on TSs or UFSAR

requirements and/or the high number of occurrences.

Corrective actions had been completed and closed but had not

prevented recurrence.

As corrective ~ction, the licensee generated a Corporate Level 1

assignment to evaluate current methods for identifying recurring

problems. Additionally, a review of the existing RCE program and

self-assessment of the station corrective action program was

performed .

The inspectors concluded that QA corrective action audit was

effective in identifying an area that needed improvement and was

identified as a strength.

Within.the areas inspected, no violations or deviations were identified.

5.

Licensee Event Report Followup (92700)

The inspectors reviewed the LER listed below and evaluated the adequacy

of the corrective action.

The inspectors' review also included followup

of the licensee's corrective action implementation.

(Closed) LER 50-281/92-09, Engineering Safety Feature (ESF) Actuation,

Auxiliary Feedwater MOVs Receive an Open Signal.

The details of this event were described in NRC Inspection Report Nos.

50-280, 281/92-17.

Because the event involved several equipment

problems and human performance errors, the licensee initiated a formal

root cause evaluation.

The results of RCE 92-06 and proposed corrective

action were reviewed and found to be adequate in NRC Inspection Report

50-280, 281/92-25.

The inspectors reviewed implementation of the RCE proposed corrective

actions.

The inspectors verified that revisions and training related to

several non-safety related procedures associated with the mechanical

chillers and power supplies were complete.

In addition, the chiller's

operating logic was verified and adequately documented by the licensee.

6

The inspectors concluded that actions recommended by the RCE were

satisfactorily implemented.

Within the areas inspected, no violations or deviations were identified.

6.

Action on Previous Inspection Items (92702)

6.1

(Closed) URI 50-280, 281/94-21-01, Time Constraints For

Sampling/Testing AVEF System Following Exposure To Chemicals

6.1.1

6.1.2

The Event

On June 16, 1994, a hydrazine concentration of 6 ppm

and an ammonia concentration of 30 ppm were detected

in the Unit 2 containment. These fumes were

identified after a manway was removed from the A SG

which had just completed chemical cleaning. Trains A

and B of the AVEF system were operated in order to

remove the hydrazine and ammonia fumes from

containment.

Containment was evacuated as a

precaution.

The supplier of the charcoal utilized in

the AVEF system was contacted by the licensee to

evaluate potential effects of these chemicals on the

charcoal.

The charcoal supplier informed the licensee

that exposing charcoal to the measured concentration

of fumes should not be not detrimental to the

charcoal.

AVEF Surveillance Performed

On June 28, 1994, charcoal samples were obtained from

the train A AVEF system and sent to a contractor for

analysis. This sample was obtained to meet the

TS 4.12.A.8.d requirements.

TS 4.12.A.8.d requires

that laboratory analysis on charcoal samples be

performed following painting, fire, or chemical

release in an area communicating with the AVEF system.

On July 15, 1994, the licensee was notified that the

sample's methyl iodide removal efficiency was 93.43%.

The minimum acceptable methyl iodine removal

efficiency specified in TS 4.12.B.4 was 96%.

Train A

of the AVEF system was declared inoperable on that

same day.

The charcoal was replaced and DOP and

halogenated hydrocarbon leakage tests were performed

as post-maintenance testing prior to returning the

train to service on July 20.

On July 28, 1994, charcoal samples were obtained from

the train B AVEF system and sent to a contractor for

analysis.

On August 4, 1994, the licensee was

notified that the sample's methyl iodide removal

efficiency was 90.7%.

This was below minimum TS

6.1.3

7

requirements. Train B of the AVEF system was declared

inoperable on that same day.

The charcoal was

replaced and DOP and halogenated hydrocarbon leakage

tests were performed prior to returning the train to

service on August 5.

Event Evaluation and AVEF Testing Performed

Without extensive testing of the charcoal removed from

the AVEF trains, the licensee was unable to positively

identify what caused the AVEF system charcoal to

degrade.

However, the licensee did conclude that the

cause was associated with the chemical release event

in the Unit 2 containment that occurred on June 16.

As previously stated, both trains of the AVEF system

were aligned to take a suction from containment in

order to remove the ammonia and hydrazine fumes.

At

that time the manway had just been removed from the

secondary side of the A SG and the manway from the C

SG had been removed several days earlier. Operating

both trains of the AVEF system decreased pressure in

the containment which allowed fumes from residual SGCC

chemicals to be exhausted from the SGs via the removed

manway covers into containment and then discharged

from the containment to the atmosphere via the AVEF

system.

Based on conversation with the charcoal

supplier, the licensee concluded that the noted

concentrations of ammonia and hydrazine should not

have damaged the charcoal in the AVEF system but that

other residual SGCC chemical may have degraded the

charcoal. The licensee determined that if fumes from

SG cleaning chemical EDTA were drawn through the AVEF

system, the fumes could have degraded the charcoal.

TS 4.12.A.8.d required that laboratory analysis on

charcoal samples be performed following painting,

fire, or chemical release in an area communicating

with the AVEF system.

After the A train AVEF system

charcoal sample results were identified as not meeting

minimum TS acceptance criteria, the inspectors

questioned the licensee what time constraints were

associated with TS 4.12.A.8.d.

The inspectors were

informed that there were no time constraints specified

in TSs and

II fo 11 owing

II meant when pr act i cal .

The inspectors also noted that the A train was sampled

and returned to service before the B train was

sampled.

The AVEF system is common to both units and

is required by TSs to be operational prior to RCS

temperature and pressure exceeding 350 degrees F and

450 psig respectively in either unit.

TSs allow one

train of the AVEF system to be inoperable for a period

8

not to exceed seven days.

Once the A train was

decl.ared inoperable on July 15, sampling of the B

train would have required the B train to also be

declared inoperable.

TSs do not recognize both trains

of the AVEF system being inoperable and entry into TS 3.0.1 would have been required.

The licensee's policy

is not to enter TS 3.0.l on a voluntary basis. The

inspectors determined that the B train sample was not

promptly taken after the A train was returned to

service.

TS 4.0.4 specifies that entry into an operational

condition shall not be made unless the surveillance

requirements associated with a LCO have been performed

within the stated surveillance interval or as

otherwise specified. The inspectors noted that on

June 23, Unit 2 entered the mode where the AVEF system

was required to be operable.

The inspectors

questioned the licensee why a mode change was made in

Unit 2 prior to sampling/testing the AVEF system in

accordance with TSs 4.12.

The inspectors were

informed that the AVEF system was operable to support

operation of Unit 1 and therefore operable to support

Unit 2 operations as well .

The inspectors reviewed the licensee's basis for

determining sampling priorities for the charcoal

trains. The A train of the AVEF system was sampled

and returned to service prior to sampling the B train.

Station policy is to test one train at a time. Also,

the A train operated for most the time (approximately

484 hours0.0056 days <br />0.134 hours <br />8.002645e-4 weeks <br />1.84162e-4 months <br />) during the Unit 2 SGCC outage.

The

operating time on the B train during the outage was

significantly less (approximately 117 hours0.00135 days <br />0.0325 hours <br />1.934524e-4 weeks <br />4.45185e-5 months <br />).

On

June 16, the day of the chemical release in Unit 2 the

A train of the AVEF system operated approximately 23

hours and the B train operated for approximately 8

hours.

The licensee thought that if there was a

problem, it would show up on the A train because it

was operated the most during the outage and on the day

of the chemical release.

The inspectors reviewed previous test results for the

charcoal trains to determine if there were any trends

that would indicate chronic charcoal degradation.

TSs

requires that the AVEF system charcoal be sampled

every 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of operation.

The results of the last

charcoal samples obtained to meet the 720 hour0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />

sampling requirement were reviewed.

The A train was

sampled on February 2, 1994.

The sample results

indicated a methyl iodide removal efficiency of

99.73%.

The A train had operated for approximately

6.1.4

9

657 hours0.0076 days <br />0.183 hours <br />0.00109 weeks <br />2.499885e-4 months <br /> between February 2 and June 28, 1994.

The

B train was sampled on March 6, 1994.

The results of

this sample indicated a methyl iodide removal

efficiency of 96.57%.

The B train had operated for

approximately 360 hours0.00417 days <br />0.1 hours <br />5.952381e-4 weeks <br />1.3698e-4 months <br /> between March 6 and July 28,

1994.

The inspectors concluded that the A train had

operated more than the B train but noted that the

initial methyl iodide removal efficiencies obtained

from the previous samples were lower in the B train

than the A train. A lower initial methyl iodide

removal efficiency in the B train may not have been

considered by the licensee when determining which

train should be sampled first following the chemical

release.

Following the chemical release in the Unit 2 *

containment on June 16, it was 12 days before the

A train AVEF system charcoal was sampled and 42 days

before the B train charcoal was sampled.

The

inspectors concluded that the amount of time taken to

obtain these samples was excessive in that the TS 4.12.A.8.d requirement to sample following a chemical

release was not expedited.

As a result, Unit 1 was

operated from June 16 through June 28 with the A tr~in

and through July 28 with the B train AVEF system

degraded.

Unit 2 operated from June 23 through

June 28 with the A train and July 28 with the B train

degraded.

Safety Consequence of the Event

Although the AVEF system charcoal did not meet minimum

TS methyl iodide removal efficiency acceptance

criteria and was therefore degraded, the licensee's

analysis concluded that the AVEF system was still

capable of mitigating the consequences of the design

basis accidents.

The inspectors reviewed engineering analysis

NAF-94063, Explanation of Filter Efficiency Used in

FHA and LOCA Analysis Surry Power Station, Units 1

and 2, revision 0, which the licensee provided to

address the inspectors' concerns as to whether the

function of the system was compromised.

This analysis

addressed the radiological consequences of several

accident scenarios which provide the design basis for

the AVEF system.

The LOCA scenario resulted in the

most severe off-site radiological consequences.

However, station accident analysis*do not credit the

AVEF system for methyl iodide removal following a

LOCA.

The most limiting scenario for which the AVEF

system is credited for methyl iodide removal is the FHA.

6.1.5

10

Engineering analysis NAF-94063 assumed filter removal

efficiencies of 70% for methyl iodide and 90% for

elemental iodide following a FHA.

The inspectors

independently confirmed that the assumptions used in

NAF-94063 were consistent with those specified in NRC

Regulatory Guide 1.25, Assumptions Used for Evaluating

the Potential Radiological Consequence of a FHA in the

Fuel Handling and Storage Facility for Boiling and

Pressurized Water Reactors.

The licensee evaluation

concluded, that based on 30 days of AVEF system

operation following a FHA, both off-site and on-site

exposures would remain within 10 CFR 100 regulatory

limits.

The results of the A and B train AVEF charcoal filter

efficiency analysis, measured under laboratory test

conditions, were above the 70% value used in

NAF-94063.

However, the inspectors observed that TS 4.12 states that the laboratory test conditions are

less severe than the design accident environment.

The

TS further state that 96% methyl iodide removal

efficiency provides assurance that the AVEF will

function sufficiently under accident conditions to

meet regulatory requirements for protection of the

public.

The inspectors questioned whether the

measured AVEF charcoal filter efficiencies of 90% and

93% were sufficient to assure design requirments.

Engineering analysis NAF-94063 did not specifically

.correlate laboratory test conditions to the

environment present following a design accident.

The

inspectors expressed concern that the AVEF system was

degraded in that the charcoal filters did not meet TS

required performance criteria. The licensee

maintained that the AVEF system remained functional

and indicated that further technical assessment of

this issue was in progress at the end of this report

period.

Regulatory Issues

In summary, samples were not promptly taken after a

chemical release; when sampling was performed, it was

sequential, not simultaneously; and, the B train was

not sampled promptly after the A train's sample

results were known nor after the A train was returned

to service.

10 CFR 50, Appendix B, Criterion XVI, Corrective

Action, requires that measures be established to

assure that conditions adverse to quality are promptly

identify and implement corrective action following the

chemical release that damaged the AVEF system charcoal

11

on June 16, 1994, was identified as part 1 to Apparent

Violation 50-280, 281/94-24-01, Failure to Identify

and Promptly Correct Conditions Adverse to Quality.

6.2

(Closed) URI 50-280, 281/94-21-02, TS Monthly Testing That

Requires Installation of Jumpers or Disconnection of Leads.

During the licensee's review of TS surveillance compliance,

engineering identified three instances where reactor

protection/ESF circuits were not being fully tested on a monthly

basis with the unit at power because testing required the use of

jumpers or disconnecting leads to complete.

The licensee

concluded that the following circuits were not designed to test at

power and therefore not required to be tested monthly:

Between 10% and 35% power, low RCS flow on two out of three

loops automatically opens the reactor trip breakers.

TS

Table 4.1-1, Minimum Frequencies For Check, Calibrations And

Test Of Instrument Channels, Items 5 and 26 require that .

this circuit be functionally tested on a monthly interval.

The review identified that the circuit was being tested on a

RFO interval but the entire circuit was not tested monthly.

The inspectors noted that without modification, lifting of

leads/installation of jumpers would be required to

completely test this circuit at power.

Low-low level on two out of three SGs automatically start

the respective unit's TDAFW pump.

TS Table 4.1-1, Item

32.a, requires that this circuit be functionally tested on a

monthly interval. The review identified that the circuit

was being tested ~n a RFO interval but not monthly.

The

inspectors noted that without modification, testing at power

. would render two of the three AFW pumps inoperable. This

condition would require entry into TS 3.0.1.

Undervoltage on two out of the three RCP buses automatically

starts the respective unit's TDAFW pump.

TS Table 4.1-1,

Item 32.b, requires that this circuit be functionally tested

on a monthly interval. The review identified that the

circuit was being tested on a RFO interval but not monthly.

The inspectors noted that without modification, testing this

circuit would render the TDAFW pump inoperable during the

test.

The licensee concluded that a clarification to TSs would be

requested in the future and that a TS change was not immediately

required.

The licensee did implement changes to the surveillance

intervals for the above circuits as a result of the review.

In

addition to testing the circuits during RFOs, the circuits are

required to be tested prior to starting a unit up if the circuit

was not tested during the previous 30 days.

The inspectors

discussed the requirements of TS Table 4.1-1, Items 5, 26 and 32.a

1---

!

12

and b with the cognizant NRC staff and concluded that TSs required

each of the above circuits to be tested on a monthly interval.

Through a review of the circuits in question the inspectors noted

that it was not practical to test these circuits monthly at power

and that this issue had minor safet1 significance.

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires

that measures be established to assure that conditions adverse to

quality such as deviations and nonconformances are promptly

identified and corrected. The failure to promptly correct a

condition adverse to quality when an engineering review identified

that certain circuits were not fully being functionally tested on

a monthly basis was identified as part 2 to Apparent Violation

50-280, 281/94-24-01, Failure to Identify and Promptly Correct

Conditions Adverse to Quality.

Within the areas inspected, one apparent violation with two parts was

identified.

7.

Exit Interview

The inspection scope and findings were summarized on September 2, 1994,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the inspection results

addressed in the Summary section and those listed below.

Item Number

EEI

50-280, 281/94-24-01

URI 50-280, 281/94-21-01

URI 50-280, 281/94-21-02

LER 50-281/92-09

Status

Open

Closed

Closed

Closed

Description/(Paraqraph No.)

Failure to Identify and

Promptly Correct Conditions

Adverse to Quality

(paragraphs 6.1 and 6.2)

Time Constraints for

Sampling/Testing AVEF System

Following Exposure to

Chemicals. (paragraph 6.1).

TS Monthly Testing That

Requires Installation of

Jumpers or Disconnection of

Leads (paragraph 6.2)

Engineering Safety Feature

(ESF) Actuation, Auxiliary

Feedwater MOVs Receive an Open

Signal (paragraph 5).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

13

8.

Index of Acronyms and Initialisms

AFW

AUXILIARY FEEDWATER

AVEF

AUXILIARY VENTILATION EXHAUST FILTER

CFR

CODE OF FEDERAL REGULATIONS

DOP

PENETRATION OF DIIOCTYL PHTHALATE

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

EOG

EMERGENCY DIESEL GENERATOR

EDTA

ETHYLENE DIAMINE TETRA-ACETIC ACID

ESF

ENGINEERED SAFETY FEATURE

F

FAHRENHEIT

FHA

FUEL HANDLING ACCIDENT

IRPI

INDIVIDUAL ROD POSITION INDICATION

JCO

JUSTIFICATION FOR CONTINUED OPERATION

LER

LICENSEE EVENT REPORT

LCO

LIMITING CONDITIONS OF OPERATION

LOCA

LOSS OF COOLANT ACCIDENT

MER

MECHANICAL EQUIPMENT ROOM

MFRV

MAIN FEEDWATER REGULATING VALVE

MOV

MOTOR OPERATED VALVE

NRC

NUCLEAR REGULATORY COMMISSION

PCV

PRESSURE CONTROL VALVE

PPM

PARTS PER MILLION

PSIG

POUNDS PER SQUARE INCH GAGE

QA

QUALITY ASSURANCE

RCE

ROOT CAUSE EVALUATION

RCP

REACTOR COOLANT PUMP

RCS

REACTOR COOLANT SYSTEM

RFO

REFUELING OUTAGE

SG

STEAM GENERATOR

SGCC

STEAM GENERATOR COMPONENT COOLING

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

TDAFW

TURBINE DRIVEN AUXILIARY FEEDWATER

TS

TECHNICAL SPECIFICATION

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

URI

UNRESOLVED ITEM

VIO

VIOLATION

VPAP

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WO

WORK ORDER