ML18152A357

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Insp Repts 50-280/95-14 & 50-281/95-14 on 950702-0805.No Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint Insp,Surveillance Insp & LER Followup
ML18152A357
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/28/1995
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A358 List:
References
50-280-95-14, 50-281-95-14, NUDOCS 9509070215
Download: ML18152A357 (16)


See also: IR 05000280/1995014

Text


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Report Nos.:

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/95-14 and 50-281/95-14

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:. July 2 through August 5, 1995

Lead Inspector: ;t;LJ ~

,__

M. W. Branch,_ Senior Resident Inspector

Other Inspectors:

Approved by:

Scope:

D. M. Kern, Resident Inspector

W. K. Poertner, Resident Inspector

S. G. Tingen, Resident Inspector

~~e*

G.~Beisction Chief

Reactor Projects Section 2A

  • Division of Reactor Projects

SUMMARY

8-/2-r/?J-

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, and Licensee Event Report followup, and action on previous

inspection items.

Inspections of backshift and weekend activities were

conducted.

Re-sults:

Plant Operations

Sufficient self contained breathing apparatus (SCBA) equipment was available

and operations and control room personnel were properly trained to respond to

9509070215 950828

PDR

ADOCK 05000280

G

2

a toxic gas event.

The recent decision to SCBA certify all Shift Technical

Advisors (STA) was a positive initiative to improve STA availability to the

control room staff during certain events (paragraph 3.1).

With the Unit 1 control room annunciators degraded, operators implemented

appropriate compensatory actions.

Management involvement and compensatory

_measures taken during corrective maintenance were good (paragraph 3.2).

Maintenance

On July 20, Unit 1 annunciators became degraded when an electrician

inadvertently .shorted the annunciator power supply during troubleshooting

activities (paragraph 3.2).

Engineering

Fire brigade composition and responsibilities, methods used to alert the fire

brigade, and fire fighting methods established for electrical fires were

consistent with NRC fire protection program guidance (paragraph 5.1).

Engineering calculations for a cask drop within the fuel building, were

technically accurate and sufficiently bounded current dry fuel storage cask

handling practices.

The inspectors noted that fuel handling procedures did

not specify a maximum height* at which dry storage casks could be moved above

the fuel building operating floor or the spent fuel pool. Appropriate actions

were taken to strengthen procedures in this area (paragraph 5.2).

Plant Support

Highly radioactive Na-24 sources were used during moisture carryover tests

performed on July 12 and July 14.

Controls for the unusual radiological

conditions were good.

Information gained from other utilities was effectively

integrated into the radiological work plan. Radiological protection

technicians provided close oversight and incorporated lessons learned from the

Unit 1 test into the Unit 2 test. Minor radiological control and

communication discrepancies were properly addressed.

Liquid radioactive

releases were effectively managed (paragraph 6.2) .

e

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2.

  • W. Benthall, Supervisor, Licensing
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance

D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

  • D. Erickson, Superintendent of Radiation-Protection
  • B. Garber, Licensing
  • R. Garner, Outage and Planning

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Supervisor of Administrative Services

C. Luffman, Superintendent, Security

J. McCarthy, Assistant Station Manager

  • S. Sarver, Superintendent of Operations

R. Saunders, Vic~ President, Nuclear Operations

  • B. Shriver, Assistant Station Manager

K. Sloane, Superintendent of Outage and Planning

  • E. Smith, Site Quality Assurance Manager
  • T. Sowers, Superintendent of Engineering
  • B. Stanley, Supervisor, Procedures
  • J. Swientoniewski, Supervisor, Station Nuclear Safety
  • N. Urquhart, Supervisor, Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector

D. Kern, Resident Inspector

  • K. Poertner, Resident Inspector

S. Tingen, Resident Inspector

  • Attended Exit Interview

Acronyms used throughout this report are listed in the last paragraph.

Plant Status

During this *report period Mr. Brice Shriver replaced Mr. Alan Price as

Assistant Station Manager, Safety and Licensing.

Mr. Price is currently

on temporary assignment to INPO for two years.

2

On July 8, Unit 1 reactor power was reduced to 85% to allow turbine

valve freedom testing.

Power was returned to 100% after the test and

the unit remained at full power until August 3 when refueling coast down

commenced.

The unit was at 97% power at the end of the report period.

Unit 2 operated at full power for most of the report period.

On July

14, power was reduced to 98% and returned back to 100% for SG moisture

carryover testing.

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

3.1

Self Contained Breathing Apparatus

A toxic gas release near another nuclear power facility recently

necessitated control room personnel to don SCBAs to permit them to

continue performing their duties in the control room.

The

inspectors reviewed the Surry UFSAR, station procedures, and

interviewed personnel to determine the degree to which Surry

Station control room operators rely upon SCBAs to cope with a non-

radio~ctive toxic gas release.*

The inspectors reviewed UFSAR section 2.1, and confirmed that no

serious on-site or off-site hazardous material threats to Surry

Station were identified. The last potential on-site source of

poisonous gas which could effect control room habitability,

bottled chlorine gas, was removed in 1988.

The TS were

subsequently amended to eliminate. the requirement for control room

chlorine gas monitors.

In addition, the control and relay room

ventilation system is equipped with tight redundant seismic

category I isolation dampers and weatherstripped doors which

permit control room pressurization with bottled air following an

accident.

The inspectors concluded that the introduction of toxic

gas to the control room was highly improbable.

Abnormal operating procedures O-AP-20.00, Main Control Room

Inaccessibility, revision 3 and O-AP-20.01, Main Control Room

Oxygen Monitor - Alarm or Malfunction, revision 1, discuss use of

SCBA in the control room.

Procedure O-AP-20.00 conservatively

lists poisonous gas as a possible cause for degraded control room

air. Fire and fire extinguishing system (carbon dioxide or Halon)

3.2

3

actuation are listed as the most probable events for which control

room operators would don SCBA.

The inspectors noted that these

procedures provided clear instruction regarding when to don SCBAs

in the control joom.

Five SCBAs are maintained in the control room for use by control

room personnel.

The inspectors observed that this number was

sufficient for the TS 6.1 required compliment of on-shift ROs(3)

and SROs(2) and that all RO/SRO personnel were SCBA qualified.

The inspectors questioned whether a SCBA was needed in the control

room for the STA, a TS required member of the shift. The STA

performs most of his duties from the STA office, but may be

requested to augment the control room staff during event response.

The fire protection coordinator informed the inspectors that there

are numerous SCBAs readily available to the STA along the main

turbine hallway.

The inspectors visually verified that a

sufficient number of SCBAs were available for the STA in close

proximity to the control _room.

The inspectors observed that some

STAs are not currently SCBA qualified. This could limit their

availability to the shift during certain events.

The SNS

Supervisor noted that while not required to perform duties from

the control room, SCBA qualification could improve STA ability to

respond to certain events.

He further stated that a schedule

would be developed by which all STAs would be SCBA certified

within the next.couple of months.

The inspectors noted that this

was a positive initiative to improve STA availability to the

control room staff. The inspectors concluded that personnel were

adequately trained and SCBA equipment was available for control

room personnel to respond to a toxic gas event.

Degraded Unit 1 Control Room Annunciators

On July 20, ~lectricians were checking voltage readings to verify

the condition of a suspected failed Unit 1 control room alarm

annunciator power supply.

The electricians inadvertently shorted

across a fuse holder and propagated a fault to the remaining eight

parallel power supplies. All annunciators on the A through E*

annunciator panels actuated. All, with the exception of two,

cleared when acknowledged.

Operators promptly adjusted selected

monitored parameters (i.e. containment partial pressure) and

verified that the A-E alarm circuits would still light to indicate

when an alarm condition was present.

However, the audible

annunciator horn and the alarm lock in feature were not working

properly.

The _licensee determined that the A-E annunciator panels

were degraded, but remained operable.* The shift implemented

abnormal operating procedure O-AP-10.13, Loss of Main Control* Room

Annunciators, revision 0, and directed the third RO to

continuously monitor the A-E annunciator panels.

The inspectors

concluded that operator response was appropriate .

The inspectors observed control room operators between July 20 and

23 and determined that augmented monitoring was effective. The

. *

4

inspectors discussed emergency plan entry conditions with the

shift supervisor.

The A-E annunciator panels represented 50

percent of the Unit 1 control room alarm annunciators.

The

emergency plan specified Unusual Event entry upon loss of >75

percent of control room alarms.

The operations shift properly

reviewed the emergency plan for implementation in the event the

annunciators further degraded.

Initial troubleshooting failed to identify the specific components

which caused the annunciator degradation.

Vendor assistance was

requested and troubleshooting activities were halted pending

arrival of the vendor.

SNSOC reviewed and approved further

annunciator corrective maintenance activities prior to

implementation. Certain maintenance activities required the A-E

annunciator panels to be fully inoperable.

Further compensatory

measures were established during this period. Critical parameters

were continuoµsly monitored on the ERF computer and the sequence

of events recorder was frequently reviewed.

Additionally, a

fourth RO was assigned to the shift to directly monitor related

plant parameters.

Electricians determined that three of the nine

parallel power supplies had failed. *Two power supplies .were

replaced and the A-E annunciator panels were returned to service

on July 23.

DR S-95-1694, including a human performance

evaluation, was initiated to determine the root cause of the ~vent

and verify follow-up corrective actions.

The inspectors

determined that management involvement and compensatory measures

taken were good.

Within the areas inspected, no violations or deviations were identified.

4.

Maintenance and Surveillance Inspections (62703, 61726)

During the reporting period, the inspectors reviewed the following

maintenance and surveillance activities to assure compliance with the

appropriate procedures and TS requirements.

4.1

Component Cooling Water Heat Exchanger Cleaning

4.2

On August 3, the inspectors witnessed work activities associated

with cleaning the A CC heat exchanger.

The work activity was

accomplished in accordance with WO 32139901 and procedure

O-MCM-0812-01, BC and CC Heat Exchanger Cleaning, revision 1.

The

inspectors reviewed the work package and verified that procedures

were followed.

The inspectors also verified that the isolation

boundary was adequate.

Control Room Chiller Flow Data

On August 3, the inspectors witnessed the performance of temporary

operating procedure O-TOP-4062, Obtaining Flow Data for 1-VS-P-18,

revision 1. This temporary procedure obtained service water flow.

data associated with control room chiller l-VS-E-48.

The

5

inspectors noted that service water flow dropped when control room

chiller 1-VS-E-4C came on.

This observation was discussed with

the system engineer who indicated that 1-VS-E-4C would not

normally be operated in parallel with 1-VS-E-4B.

Thus, the flow

data without 1-VS-E-4C in operation was the desired flow data.

The evolution was performed in accordance with approved

procedures.

Within the areas inspected, no violations or deviations were identified.

5.

On-Site Engineering Review (37551, 64704)

5.1

Fire Protection

The inspectors reviewed station fire brigade response activities.

The fire protection program is described in procedure VPAP-2401,

Fire Protection Program, revision 2.

The fire brigade is composed of three personnel from the

operations department (one of which is the scene leader), and two

security officers.

None of the fire brigade members share TS

licensed duties.

VPAP-2401 requires that the fire brigade be

activated upon notification in the control room of a fire, *

suspected conditions that could result in a fire, or at the

discretion of the SS.

The licensee's policy is not restricted to

fire or smoke.

VPAP-2401 states that if a fire is suspected,

notify the control room.

Neither VPAP-2401 or AP-48, Fire

Protection, Operations Response, revision 3, describe any delays

associated with activating the fire brigade.

Discussion with SS

and security personnel indicate that fire brigade responsibility

takes precedence over other duties.

However, security personnel

on the fire brigade would be relieved prior to abandoning their

security post.

The inspectors also reviewed the fire alarms available in the

control room and other areas of the station. The station fire

alarm which alerts fire brigade personnel is audible in the plant

during other alarms. Additionally, in high noise areas a red

alarm light is installed to alert.personnel of off-normal

conditions.

The station alarm system and Gai-Tronics used to

announce the fire emergency are powered from the semi-Yital bus.

The control room alarm which sounds when plant detectors sense

smoke or heat is faint but audible in the control room and it has

a distinct sound.

Based on conversation with operators, they

believe that they could hear the alarms during other events.

Additionally, there is a control room vertical panel annunciator

that also lights and sounds when a fire system alarm is received.

The inspectors questioned whether the licensee would combat an

electrical switchgear fire with water fog and under what*

conditions.

The stated licensee's policy leaves this decision up

to the scene leader .. The fire strategy plans indicate that

5.2

6

electrical systems should be deenergized if possible or practical.

Backup fire suppression is a water hose and procedures contain a

caution note about electrical shock hazard if water is used on

electrical fires.

Fire brigade-training addressed water usage on

electrical fires in the event that the power source can not be

deenergized.

The inspectors determined that fire brigade manning is the same

for all shifts. At least once per year each operating crew has a

back* shift drill. The criteria used to request off site

assistance is left to at the discretion of the scene leader and

the control room SS.*

Additionally, the inspectors reviewed the licensee EPIPs in the

area of fire related events.

Per EPIP-1.01 Tab I, Emergency

Managers Controlling Procedures, revision 34, a fire in the PA or

switchyard which is not under control within 10 minutes after the

fire brigade is dispatched is designated as an NOUE.

An Alert is

declared when a fire has the potential for causing a safety system

to become jnoperable when the plant is above cold shutdown

conditions. A Site Area Emergency exist when a fire causes major

degradation of a safety system function required for protection of

the public and affected systems are rendered inoperable .

Based on the inspectors review, fire brigade composition and

responsibilities, *methods used to alert the fire brigade, and fire

fighting methods established for electrical fires were consistent

with NRC fire protection program guidance.

Dry Fuel Storage Cask Drop Analysfs

The inspectors reviewed various engineering calculations to

determine whether current spent fuel storage cask loading

practices were bounded-by existing cask drop accident analysis.'

Engineering calculation 194, Fuel Cask Drop Crash Pad Design and

Analysis, dated September 23, 1982, postulated a cask drop into

the SFP from 1 foot above the refueling building operating floor~

The calculation was later updated to analyze a cask drop from

5 feet 8 inches above the operating floor.

In each case, the

postulated cask drop caused a tear in the SFP stainless steel

liner, but no significant structural damage to the surrounding six

foot concrete SFP wall or floor.

The resulting SFP leakage was

minor and well within the capacity of makeup sources. A

postulated radioactive material release due to damaged fuel

assemblies within the SFP was within regulatory limits. The

inspectors concluded that the calculations were technically

accurate and sufficiently bounded current dr~ fuel storage cask

handling practices .

The inspectors observed that procedure OP-4.22, Castor V/21 Cask

Loading and Handling, revision 6, did not specify a maximum height

at which dry storage casks could be moved above the fuel building

7

operating floor or the SFP.

The original license submittal stated*

that casks should not be carried at a height >6 inches above the

operating floor to minimize the chance of a cask roll accident.

Although operators typically minimized cask h~ight above the SFP,

the inspectors questioned whether procedure OP-4.22 provided

sufficient instructions to ensure cask handling was conducted

within the height limitations which had been analyzed.

The

inspectors discussed this observation with. nuclear fuel

performance analysis engineers and the fuel handling supervisor.*

The fuel handling supervisor revised procedure OP-4.22 to

incorporate the height restrictions prior to the next dry cask

load.

The inspectors reviewed the procedure revision and

determined that the handling height considerations were properly

addressed.

Within the areas inspected, no violations or deviations were identified.

6.

Plant Support (71707, 71750}

6.1

Plant Tour Observations

6.2

The inspectors observed radiological control practices and

radiological conditions throughout the plant. Radiological

posting and control of contaminated areas was good.

Workers.

complied with radiation work permits and appropriately used

required personnel monitoring devices.

The protected area

security perimeter was well maintained with no equipment or debris

obstructing the isolation zones.

Installation of new diesel fuel

oil supply lines for the station EDGs involved substantial civil

engineering .activities within the RCA.

Actions to maintain the

integrity of RCA boundaries and the security perimeter during

construction activities were effective.

Moisture Carryover Test

The licensee intends to implement a four percent core power uprate

during the second half of 1995.

MCO tests were performed on July

12 (Unit l} and July 14 (Unit 2} to measure the quality of the

steam currently produced by the SGs at rated power.

Station

engineers plan to use the test results to project the effect of

the core uprate on water impingement to the main turbine.

The MCO

tests involved injection of a highly radioactive Na-24 source into

the feedwater header-and monitoring the amount of sodium entrained

in moistur~ leaving the SGs.

The source vial contained over 1

curie of Na-24 and had a dose rate of over 1600 Rem.per hour on

contact.

The fifteen hour Na-24 decay half-life resulted in

elevated radiation levels at several locations within the turbine

building for several days following the MCO tests. The inspectors

closely observed the MCO tests to determine whether appropriate RP

practices were implemented to minimize personnel radiation

exposure and liquid effluent release.

8

Preparations for the MCO test were good .. Secondary leaks were

identified and repaired to the maximum extent practical. The

surveillance schedule was reviewed to ensure surveillances, such

as periodic TDAFW pump run which could release steam to the

environment, were completed prior to Na-24 injection.

SNSOC test

plan approval and pretest crew briefings were generally good.

The

inspectors toured the turbine building and verified that

appropriate radiological postings were inplace prior to the start

of the test.

The inspectors reviewed RWP-1090, MCO Project - Perform Unit 1 and

2 MCO Test Utilizing Na-24 Source, with the RP supervisor prior to

the test. The licensee had discussed RP precautions with other

utilities who recently performed similar MCO tests. Activities

which had a potential for high personnel exposure, e.g., Na-24

vial handling and injection valve manipulation, were rehearsed

prior to actual Na-24 injection.

The inspectors concluded that

the information gained from the other utilities was effectively

integrated into RWP-1090.

During performance of the Unit 1 MCO test, the inspectors noted

that the prerequisites for plant restoration following test

completion were DOt commonly understood by operations and RP

personnel.

Minor miscommunications resulted in slightly elevated

dose rate levels in the condensate polishing b~ilding before RP

personnel were positioned to survey the area.

The test

coordinator revised procedure 2-ST-0314, Steam Generator Moisture

Carryover Measurement, revision 0, to clarify prerequisites for

plant restoration and clearly communicated these prerequisites

during the prebrief for the Unit 2 MCO.

The inspectors discussed

other observations, including concerns for personnel heat stress

with the test coordinator. Radiological controls and protective

clothing requirements were appropriately modified for the Unit 2

MCO test.

.

.

Continuous RP coverage was provided during transport of the Na-24

sources from a local airport to the site. Security expedited on-

site acceptance of the Na-24 source which further minimized the

personnel radiation exposure received by the transportation crew.

RP personnel closely monitored all handling of the Na-24 source

including injection and sampling activities which had the

potential to spread contamination.

Background radiation levels

were too high, at the established turbine building exit point, for

the RM-14 portable friskers to be accura.te.

The inspectors

observed that some test personnel were using the frisker to exit

the RCA without noting the excessive background radiation level.

The inspectors informed the RP supervisor, who took appropriate

action to reestablish the RCA exit in a lower background radiation

area.

All test personnel properly used whole body monitor~ prior

to exiting the protected area. The inspectors reviewed postings,

surveys, and personnel exposure monitoring and determined that

radiological controls were appropriate and well planned.

9

The inspectors observed that the injection connections to the

Unit 1 feedwater header were not visually checked for signs of

leakage during the first 15 minutes of injection.

The inspectors

expressed concern that the vibration present at these test

connections could cause the connections to become loose and leak

highly radioactive Na-24 solution. Test engineers subsequently

began visual inspections of the connections at periodic intervals.

Chemists had difficulty obtaining representative SG samples during

the Unit 1 MCO test, due to the small sample line purge rate.

The

Unit 2 MCO test procedure was revised to incorporate five to

fifteen minute SG blowdowns directly to the station discharge

canal prior to each of four samples.

The inspectors questioned

whether the resultant liquid releases of .radioactive Na-24 were

within regulatory requirements.

Chemistry personnel informed the

inspectors that effluent release calculations based on the SG

activity measured during the Unit 1 MCO would be below the

regulatory requirements.

The licensee's calculations were

conservative, in that, they assumed no credit for radioactivity

removal in the SG blowdown ion exchanger.

The inspectors

independently performed an effluent release calculation and

confirmed that the release would be below that allowed by TS 6.8,.

10 CFR 20.1302, 10 CFR 20 Appendix B, and 10 CFR 50 Appendix I.

Discharge samples were taken and discharge records were

appropriately completed which confirmed that the.liquid

radioactive effluent releases were within specifications.

Within the areas inspected, no violations or deviations were identified.

7.

Licensee Event Report Followup (92700, 92901)

The inspectors reviewed the LERs listed below and evaluated the adequacy

of the corrective action.

The inspectors' review also included followup

of the licensee's corrective *action implementation.

7.1

(Closed) LER 50-281/93-005, Reactor Trip Due to Parti~l Actuation

of Safety Injection Master Relay During Logic Testing.

On August 21, 1993, technicians were in the final stages of*

completing SI Train B logic testing when Unit 2 tripped.

Subsequent troubleshooting indicated that the Train B SI master

relay was defective and caused the trip. The reactor trip .and

Train B SI master relay replacement were discussed in IR 50-280,

281/93-22.

Following the trip, RCS temperature decreased to 530,°F, i.e.,

less than 547 °F, no load TAvG*

As a result of this overcooling

and other overcooling events the licensee investigated probable

causes.

The inspectors reviewed engineering report NP-3005, Surry

Power Station Post-Trip Over Cooling, dated April 17, 1995.

The

report concluded that long term overcooling could be eliminated by

-~-~-------------------------------

7.2

10

more carefully controlling AFW flow rates to the SGs, minim1z1ng

any secondary steam leakage and prompt removal of auxiliary steam

and TDAFW driven AFW pump steam loads.

The inspectors revie~ed

emergency response procedures and verified that they were revised

to control AFW flow rates. The inspectors also noted that

excessive RCS cooldowns have not occurred following recent Unit

trips.

(Closed) LER 50-281/93-006, Unit 2 Automatic Reactor Trip Due to

Low SG Level in Coincidence With Feed Flow Mismatch Following

Closure of All Three MFRV.

On November 15, 1993, a single circuit breaker failed which caused

all three MFRVs to shut.

When the circuit breaker failed, the SOV

to each MFRV deenergized and the respective MFRV shut as designed.

Unit 2 subsequently tripped due to the loss of flow to SGs.

The

trip and immediate corrective actions were discussed in IR 50-280,

281/93-26'.

When the Unit 2 reactor tripped, the AFW pumps started on low-low

SG level. The packing smoked excessively on the AFW pump 2-FW-P-

3A and the pump was secured and declared inoperable.

The cause

and corrective action associated with the pump packing were also

discussed in IR 50-280, 281/93-26.

Following the trip, RCS temperature decreased to 525 °F, an

overcooled condition.

RCS overcooling corrective actions are

discussed in paragraph 7.1.

The inspectors verified that the

failed breaker was replaced and a PM program was implemented to

periodically replace the breaker and similar type breakers.

7.3

(Closed) LER 50-280, 281/93-004, Condition Prohibited by TS during

Reactor Protection System Logic Testing.

During a procedure review on March 16, 1993, the licensee noted

that monthly procedure l/2~PT-8.l, Reactor Protection System

Logic, revision 1, blocked both trains of SGBD trip valves .from

automatic closure associated with an AFW start signal.

Prior to

February 21, 1993, TS 3.8 listed SGBD trip valves as phase I

containment isolation valves. These valve were required to be

-operable to satisfy containment integrity requirements when RCS

temperature* exceeded 200 °F.

The licensee determined that

performance of 1/2-PT-8.l violated TS 3.8 as written prior to

February 21, 1°993.

The cause was personnel error involving

failure to adequately assess 1/2-PT-8.*1 for TS compliance.

Engineers reevaluated the containment isolation function and

determined that.the SGBD trip valves were not required for

containment integrity.

TS Amendments 172 and 171 removed the SGBD

valves from TS on Units 1 and 2 respectively, effective February

21, 1993.

Engineers further determined that automatic closure of

these valves was not required to assure adequate AFW flow.

The

11

inspectors reviewed the bases for the license amendments and found

them to be technically adequate. Additional corrective actions

included UFSAR updates and a TS surveillance program review to

ensure full TS compliance.

The inspectors verified that

corrective actions were complete.

The LER described the event,

causal factors, *and corrective actions in detail and met the

reporting requirements of 10 CFR 50.72.

7.4

(Closed) LER 50-280/94-010, Missed Emergency Diesel Generator

Battery Surveillance Due to Personnel Error.

On September 29, 1994, engineers identified that procedure

O-EPT-0109-03, Weekly Emergency Diesel Generator Battery Pilot

Cell and Bus Voltage Checks, revision 1, due by September 27, had

not been performed.

The licensee immediately entered a 24-hour

LCO action condition in accordance with TS 4.0.3. Technicians

successfully completed O-EPT-0109-03, which confirmed that the EDG

batteries were operable, and the LCO was exited.

Based on

satisfactory battery surveillance results and the brief missed

surveillance interval, the inspectors concluded that this event

had marginal safety impact.

The licensee determined that the cause of this event was

inadequate post maintenance document review at the supervisor

level.

The electrical supervisors involved with this review were

personally counselled regarding their performance and management

expectations. Additional corrective actions included event

discussion during electrical department crew meetings to reinforce

the importance of self checking and personal accountability for

surveillance scheduling.

The inspectors determined that these

corrective actions were adequate and completed.

The LER

accurately ~escribed-the event and addressed all reporting

requirements.

Within the areas inspected, no violations or deviations were identified.

8.

Previous Apparent Violation Item Identification Number Revisions

To facilitate data trending and retrieval, items identified after 1992

that were considered as either apparent violations or potential

escalated enforcement items were assigned new Inspection Followup System

identification numbers.

For traceability, .these changes and the

associated status of each of the items are provided below.

Apparent Violation (EEI) 50-280, 281/94-24-01 is being

administratively closed in this report. The violation will now be

tracked as VIO 94-173 01014 and is considered open.

Apparent Violation (EEI) 50-281/95-06-0l was closed when tHe

Notice Of Violation, dated May 18, 1995, was issued with two

severity level IV *violations.* The violation, identified in the

NOV as violation A, was previously tr_acked as 50-281/95-06-03, and

9 ..

12

is now being tracked as VIO 95-053 01014.

The violationi

identified in the NOV as violation B, was previously tracked as

50-281/95-06-04, and is now being tracked as VIO 95-053 02014.

Both 50-281/95-06-03 and 50-281/95-06-04 are considered

administratively closed per this report.

Both VIOs95-053 01014

and 95-053 02014 are considered open.

Exit Interview

The inspection scope and findings were summarized*on August 8, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in 'detail the inspection results addressed

in the Summary section and those listed below.

Item Number

LER 50-281/93-005

LER 50-281/93-00~

LER 50-280, 281/93-004 LER 50-280/94-010

EEi 50-280, 281/94-24-01

VIO 94-173 01014

VIO 50-281/95-06-03

Status

Closed

Closed

Closed

Closed

Closed

Open

Closed

Description/(Paraqraph No.}

Reactor Trip Due to Partial

Actuation of Safety Injection

Master Relay During Logic

Testing (paragraph 7.1)

Unit 2 Automatic Reactor Trip

Due to Low SG Level in

Coincidence With Feed Flow

Mismatch Following Closure of

All Three MFRV (paragraph 7.2)

Condition Prohibited by TS

during Reactor Protection

System Logic Testing

{paragraph 7.3)

Missed Emergency Diesel

Generator Battery Surveillance

Due to Personnel Error

{paragraph 7.4)

Failure to Identify and

Promptly Correct Conditions

Adverse to Quality

{paragraph 8)

Failure to Identify and

Promptly Cdrrect Conditions

Adverse to Quality

{paragraph 8)

Minimum Number of PZR Pressure

Instruments Not Operable

During Power Operation *

(paragraph 8)

.

,.

Item Number

VIO 95-053 01014

VIO 50-281/95-06-04

VIO 95-053 02014

13

Status

  • Open

Closed

Open

Description/(Paragraph No.}

Minimum Number of PZR Pressure

Instruments Not Operable

During Power Operation

(paragraph 8)

Failure to Adequately

Establish Measures to Identify

And Correct PZR Transmitter

Calibration Problem

(paragraph 8)

Failure to Adequately

Establish Measures to Identify

And Correct PZR Transmitter

Calibration Problem

(paragraph 8)

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

10.

Index of Acronyms

AFW

AUXILIARY FEEDWATER

BC

BEARING COOLING

CC

COMPONENT COOLING WATER

CFR

CODE OF FEDERAL REGULATIONS

CO2

CARBON DIOXIDE

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

EOG

EMERGENCY DIESEL GENERATOR

EPIP

EMERGENCY PLAN IMPLEMENTING PROCEDURE

ERF

EMERGENCY RESPONSE FACILITY

INPO

INSTITUTE OF NUCLEAR POWER OPERATIONS

IR

INSPECTION REPORT

LER

LICENSEE EVENT REPORT

LCO

LIMITING CONDITIONS OF OPERATION

MCO

MOISTURE CARRYOVER

MFRV

MAIN FEEDWATER REGULATING VALVE

NOUE

NOTIFICATION OF UNUSUAL EVENT

Na

SODIUM

NRC

NUCLEAR REGULATORY COMMISSION

PA

PROTECTED AREA

PM

PREVENTIVE MAINTENANCE

REM

RADIOLOGICAL EQUIVALENT MAN

RCA

RADIOLOGICAL CONTROL AREA

RCS

REACTOR COOLANT SYSTEM

RO

REACTOR OPERATOR

RWP

RADIATION WORK PERMIT

RP

RADIATION PROTECTION

14

SCBA

SELF CONTAINED BREATHING APPARATUS

SFP

SPENT FUEL POOL

SG

STEAM GENERATOR

SGBD

STEAM GENERATOR SLOWDOWN

SI

SAFETY INJECTION

SNSOC

STATION NUCLEAR SAFETY AND OPERATIN~ COMMITTEE

SNS

STATION NUCLEAR SAFETY

SOV

SOLENOID OPERATED VALVE

SRO

SENIOR REACTOR*OPERATOR

STA

SHifT TECHNICAL ADVISOR

SS

SHIFT SUPERVISOR

TAvG

TEMPERATURE - AVERAGE

TDAFW

TURBINE DRIVEN AUXILIARY FEEDWATER

TS

TECHNICAL SPECIFICATION

UFSAR

UPDATED FINAL SAFETY ANALYSIS REPORT

VPAP

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WO

WORK ORDER

~F

DEGREES FAHRENHEIT