ML18152A351

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Notice of Violation from Insp on 950122-0211.Violation Noted:Approved Detailed Written Procedures Were Not Used to Perform Complex Maint & Vendor Related Activities on Unit 1 Tdafwp as Evidenced by Listed Examples
ML18152A351
Person / Time
Site: Surry Dominion icon.png
Issue date: 03/07/1995
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A352 List:
References
50-280-95-03, 50-280-95-3, NUDOCS 9503150013
Download: ML18152A351 (17)


See also: IR 05000122/2002011

Text

NOTICE OF VIOLATION

Virginia Electric and Power Company

Surry 1

Docket No.: 50-280

License No.: DPR-32

During an NRC inspection conducted on January 22 through February 11, 1995, a

violation of NRC requirements was identified.

In accordance with the "General

Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2,

Appendix C, the violation is listed below:

Technical Specifications 6.4.A.7, 6.4.C and 6.4.D require that detailed

written procedures and instructions shall be provided for corrective

maintenance activities which would have an effect on the safety of the

reactor. They also require that these procedures be reviewed and

approved by the Station Nuclear Safety and Operating Committee and that

they be followed.

Virginia Power Administrative Procedure {VPAP)-0801, Maintenance

Program, revision 4, implements these requirements for maintenance

activities.

VPAP-0801, Section 6.3.3.c requires the safety significance of the

maintenance activity, complexity of the maintenance activity and

experience and training of personnel performing the activity be

considered when determining whether a detailed maintenance procedure or

skill of the craft should be utilized to accomplish a maintenance

activity.

VPAP-0801, Section 6.18.2.a requires that maintenance activities

performed by a vendor at the station be accomplished in accordance with

approved procedures.

Contrary to the above, approved detailed written procedures were not

used to perform complex maintenance and vendor related activities on the

Unit 1 turbine drive auxiliary feedwater pump {TDAFWP) as evidenced by

the following examples:

1.

On December 24 and 25, 1994, and January 11, 1995, the

TDAFWP governor was replaced using Work Orders {WOs) 301919

02, 301919 03 and 306913 08 respectively. Approved detailed

maintenance procedures were not u~ed.

2.

On December 24 and 25, 1994, and on January 11, 1995,

vendors performed maintenance/adjustment/testing on the

TDAFWP governor using WOs 301919 01 and 02, 301919 03 and

306913 08 respectively. Approved detailed maintenance

procedures were not used.

9503150013 950307

PDR

ADOCK 05000280

G

POO

ENCLOSURE 1

2

3.

On January 10, 1995, the turbine speed control system

linkage was disassembled and reassembled using WO 306913 01.

An approved detailed maintenance procedure was not used.

This is a Severity Level IV violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Virginia Electric and Power

Company is hereby required to submit a written statement or explanation

to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, D.C. 20555 with a copy to the Regional Administrator, Region

II, and a copy to the NRC Resident Inspector at the facility that is the

subject of this Notice, within 30 days of the date of the letter

.

transmitting this Notice of Violation (Notice). This reply should be

clearly ~arked as a "Reply to a Notice of Violation" and should include

for each violation:

(1) the reason for the violation, or if contested,

the basis for disputing the violation, (2) the corrective steps that

have been taken and the results achieved, (3) the corrective steps that

r

will be taken to avoid further violations, and (4) the date when full

compliance will be achieved.

Your response may reference or include

previous docketed correspondence, if the correspondence adequately

addresses the required response.

If an adequate reply is not received

within the time specified in this Notice, an order or*Demand for

Information may be issued as to why the license should not be modified,

suspended, or revoked, or why such other action as my be proper should

not be taken.

Where gciod cause is shown, consideration will be given to

extending the response time.

Dated at Atlanta, Georgia

This 7th day of March, 1995

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/95-03 and 50-281/95-03

Licensee: Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted: January 22 through February 11, 1995

Inspector:

Other

  • Inspectors:

Approved by:

D. M. Kern, Resident Inspector

S. G. Tingen, Resident Inspector

G.6i. ~Wn.chief

Division of Reactor Projects

SUMMARY

Scope:

.s~ ,-rr

Date Signed

¥.1 lfS-

DaeS1gned

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections, onsite engineering review, plant support and action on previous*

inspection items.

Inspections of backshift and weekend activities were

conducted on January 25, 28, and February 3 and 4, 1995.

Results:

  • operations

Although operators were challenged by equipment problems, Unit 2 was shutdown

and cooled down in a slow and deliberate manner (paragraph 3.1).

Exceeding the Unit 2 pressurizer heatup rate was identified as an unresolved

item pending a fatigue analysis review (paragraph 3.2).

2

Lowering reactor coolant system level was conducted in accordance with

procedures, equipment response was as expected, and operators properly focused

on safety (paragraph 3.3).

Maintenance

Failure to use approved detailed written procedures for maintenance activities

associated with turbine driven auxiliary feedwater pump (TDAFWP) governor

replacement, turbine speed control system linkage assembly and governor post

installation maintenance/adjustment/testing was identified as a violation

(paragraph 4.1).

The pre-evolution briefing for Unit 2 safety bus logic testing was very good.

Safety focus and communications were clearly emphasized. Operations personnel

safely resolved unexpected occurrences and maintained excellent control of the

evolution (paragraph 5.2).

Engineering

Evaluation and initial corrective actions associated with the Unit 2 C high

head safety injection pump motor power requirements were implemented in a

timely manner and were conservati!e (paragraph 5.1).

Procurement, storage, and handling of TDAFWP model PG-PL governors was

acceptable. Warehouse cleanliness, storage, purchase orders, design change

development, and commercial grade dedication processes were generally good.

Two isolated weaknesses regarding design change development and shelf-life

evaluation were identified (paragraph 6.1).

l .

1.

Persons Contacted

Licensee Employees

  • V. Armentrout, Licensing

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing
  • M. Biron, Supervisor, Radiation Engineering

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  • B. Bryant, Licensing
  • D. Christian, Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

D. Erickson, Superintendent of Radiation Protection

  • B. Garber, Licensing

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Supervisor of Administrative Services
  • A. Keagy, Superintendent of Materials

D. Llewellyn, Superintendent of Training

  • C. Luffman, Superintendent, Security
  • J. McCarthy, Assistant Station Manager
  • A. Price, Assistant Station Manager
  • S. Sarver, Superintendent of Operations
  • R. Saunders, Vice President, Nuclear Operations
  • K. Sloane, Superintendent of Outage and Planning

E. Smith, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering
  • B. Stanley, Supervisor, Station Procedures

J. Swientoniewski, Supervisor, Station Nuclear Safety

  • J. Winebrenner, Supervisor, Procurement Engineering

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • D. Kern, Resident Inspector
  • S. Tingen, Resident Inspector
  • Attended Exit Interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph *

..

2.

2

Plant Status

Unit 1 operated at power for the entire inspection period.

On February

10, power was reduced to 60% to repair the B main feedwater pump. The

unit was returned to full power operation on February 12.

Unit 2 was in end of cycle coastdown up to February 2.

The Unit was

shutdown on February 3, from 84% power, to perform a RFD.

The unit was

in a RFD at the end of the inspection period.

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indication to assess operability. Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

DRs were reviewed to assure that potential safety

concerns were properly addressed and reported .

3.1

Unit 2 Shutdown

The inspectors witnessed selected portions of the Unit 2 shutdown

and subsequent cooldown conducted on February 3. Although

operators were challenged by equipment problems the inspectors

noted that the unit was shutdown and cooled down in a slow and

  • deliberate manner.

Communications during plant cooldown were

good.

Pressurizer and RCS cooldown rates were closely monitored

and the inspectors independently verified that TS cooldown rates

were not exceeded.

Unit 2 RCS integrity was good.

Few signs of

leakage were observed during the hot containment walkdown.

The following equipment problems were encountered during the

shutdown:

The steam dump valve master controller stuck at

approximately ten percent demand which resulted in two of

the eight steam dump valves remaining partially open.

This

problem caused operators to deviate from the normal plant

shutdown procedure.

DR S-95-0194 was issued to ensure that

this deficiency was resolved.

Source range nuclear instrument N-31 failed to operate after

being energized. Operators entered 2-AP-4.00, Nuclear

Instrument Malfunction, revision 3, which required that

adequate shutdown margin be verified within one hour and

then every twelve hours.

The inspectors reviewed TS Table

3.7.1, Item 4, Nuclear Flux Source Range, which also

r

'

l

3.2

...

3

required that adequate shutdown margin be verified within

one hour and then every twelve hours.

The licensee verified

the shutdown margin in accordance with TS.

DR S-95-0195 was

issued to ensure that this deficiency was resolved.

Auxiliary spray valve 2-CH-HCV-2311 seat leakage

significantly complicated RCS pressure control. The problem

hampered operators' ability to control pressure throughout

the RCS depressurization process.

The inspectors

independently verified that RCS pressure and temperature

were maintained within the allowable regions of the plant

operation curve.

DR S-95-0206 was issued to ensure that the

spray valve deficiency was resolved.

The inspectors

confirmed that a WO to disassemble, inspect, and repair

2-CH-HCV-2311 was written and scheduled for completion prior

to reactor startup.

The containment particulate radiation monitor indicated an

increased trend in containment radiation level. The

containment gas radiation monitor indicated that radiation

levels were not increasing.

An air sample obtained from

containment indicated normal particulate activity.

Containment sump in-leakage rate was calculated and was

normal. Operators assessed the aggregate indications and

concluded that containment radiation levels were normal. A

deficiency card was issued to investigate and repair the

containment particulate radiation monitor.

Unit 2 Pressurizer Excessive Heatup Rate

On February 4, the licensee degassed the RCS in preparation for

the RFO.

The unit was in cold shutdown with a bubble in the

pressurizer. The evolution required that charging pump flow

rate be increased to compensate for the increased letdown flow

rate. Pressurizer level increased while operators were balancing

RCS inventory during the degas evolution and a decrease of

129 degrees F was noted in pressurizer water temperature.

The TS

allowable cooldown rate is 200 degrees F per hour. Operators were

concerned that they were approaching this limit and adjusted

charging pump flow to slowly decrease pressurizer level. During

the following one hour, water temperature in the pressurizer

increased by 146 degrees F which exceeded the TS allowable heatup

rate of 100 degrees F per hour. The licensee was recording

pressurizer water temperature every 30 minutes and identified that

the TS allowable heatup rate was exceeded.

At the end of the

inspection period, the licensee was performing a fatigue analysis

for the pressurizer. Until the inspectors review the licensee's

fatigue analysis, this is identified as URI 50-281/95-03-01,

Unit 2 Pressurizer Excessive Heatup Rate.

4.

4

3.3

Unit 2 Reactor Vessel Draindown to Flange Level

On February 8, the inspectors witnessed draining the Unit 2 RCS

from a level of 5 percent in the pressurizer (approximately 29

feet) to a level of 17.6 feet on the reactor vessel standpipe.

Draining to this level was required to support refueling

activities. This evolution was accomplished in accordance with

procedure 2-0P-RC-004, Draining the RCS to Reactor Flange Level,

revision 4.

During the initial drain down phase, the pressurizer

level was monitored.

For the three and one-half feet region that

the reactor vessel standpipe level indicator and the pressurizer

level instrumentation do not overlap, an inventory balance was

utilized to monitor the amount drained.

Upon reaching the 24 foot

level, the reactor vessel standpipe was used to monitor level in

the reactor vessel. The inspectors concluded that the draindown

evolution was conducted in accordance with procedures, equipment

response was as expected, and that operators properly focused on

safety.

Within the areas inspected, one URI was identified.

Maintenance Inspections (62703)

NRC Inspection Report Nos. 50-280/94-33 and 50-281/94-33 described the

December 1994 outage work on the Unit 1 TDAFWP and the January Unit 1

reactor trip and failure of the TDAFWP on demand.

At the conclusion of

that inspection the licensee's RCE was not complete and several items

were identified as URI 50-280/94-33-01 for subsequent followup.

The URI

had five parts and this section will address parts 1 and 4, control of

work activities and vendor instructions. Parts 2, 3 and 5 of the URI

are discussed in section 6 of this report.

4.1

Control of Work Activities

Through review of the Unit 1 TDAFWP maintenance activities

conducted on December 24 and 25, 1994, and January 10 through 11,

1995, the inspectors concluded the following:

On December 24 and 25, 1994, and January 11, 1995, the

TDAFWP governor was replaced using WOs 301919 02, 301919 03

and 306913 08 respectively. Approved detailed maintenance

procedures were not used.

On December 24 and 25, 1994, and on January 11, 1995,

vendors performed maintenance/adjustment/testing on the

TDAFWP governor using WOs 301919 01 and 02, 301919 03 and

306913 08 respectively. Approved detailed maintenance

procedures were not used.

On January 10, 1995, the TSCS linkage was disassembled and

reassembled using WO 306913 01.

An approved detailed

maintenance procedure was not used.

I

4.2

5

The inspectors reviewed the station maintenance training program

for the TDAFWP contained in JPM-0-51, Perform Maintenance to Terry

Turbine, revision 4.

The inspectors concluded that details such

as installation of the governor valve lever block and governor

valve control air pressure inlet vent plug were not specifically

addressed. According to the licensee's training department, only

one mairttenance engineer had attended a Woodward governor training

course. The inspectors concluded that TDAFWP governor

installation and TSCS linkage assembly were complex maintenance

activities and that maintenance personnel did not have the

training to perform these activities without detailed procedures.

After reviewing TM 38-W971-00001, Woodward PG-PL Governor,

revision 1, and procedure O-MCM-1403-01, Terry Turbine Overhaul,

l-FW-T-2 and 2-FW-T-2, the inspectors concluded that the TM

instructions for performing governor post installation

maintenance/adjustments/testing were not incorporated into

O-MCM-1403-01.

The inspectors were informed that the post

installation maintenance/adjustments/testing was performed by the

vendor.

The inspectors observed the vendor perform this evolution

on January 11, 1995.

The inspectors concluded that TDAFWP

governor post installation maintenance/adjustments/testing was

performed by the vendor without approved procedures .

TSs 6.4.A.7, 6.4.C and 6.4.D as implemented in part by VPAP-0801,

Maintenance Program, revision 4, require that maintenance

activities which would have an effect on the safety of the reactor

be performed in accordance with detailed written procedures

approved by SNSOC.

VPAP-0801, Section 6.3.3.c requires the safety

significance of the maintenance activity, complexity of the

maintenance activity and experience and training of personnel

performing the ,1ctivity be considered when determining whether a

detailed maintenance procedure or skill of the craft should be

used to accomplish a maintenance activity. VPAP-0801, Section

6.18.2.a requires that maintenance activities performed by a

vendor at the station be accomplished in accordance with approved

procedures.

Failure to use approved detailed written procedures

for maintenance activitjes associated with TDAFWP governor

replacement, TSCS linkage assembly and governor post installation

maintenance/adjustment/testing is identified as Violation

50-280/95-03-02, Failure to Use Approved Detailed Procedures.

Control of Vendor Information

The licensee's initial RCE identified possible concerns with

control of vendor information.

The inspectors reviewed the

control of vendor information that applied to the TDAFWP.

VPAP-0602, Vendor Technical Manual Control, revision 1 and

ENAP-0023, Technical Manual Preparation and Revision, revision 2,

were reviewed and the inspectors concluded that the licensee was

6

maintaining TDAFWP vendor information in accordance with their

program.

Within the areas inspected, one violation was identified.

5.

Surveillance Inspections (61726, 37551}

The inspectors reviewed the following surveillance activities to assure

compliance with appropriate procedure and TS requirements.

5.1

Unit 2 HHSI Pump C Testing

5.2

During a recent engineering review of HHSI pump flow rates, the

licensee identified that Unit 2 HHSI pump C motor power

requirements exceeded the design value of 690 horsepower.

On

January 30 PPR 95-007 was issued documenting this issue.

On

January 31 the PPR was reviewed by the Management Problem Review

Team and DR S-95-0177 was subsequently issued. Unit 2 HHSI pump C

was declared ini>perable and removed from service on January 31.

On February 8 the inspectors witnessed the performance of sections

6.6 and 6.7 of 2-0PT-Sl-006, SI Accumulator Distharge Check Valves

Full Open Test and 2-CH-P-lC Flow Test, dated February 7, 1995.

This procedure was revised to test HHSI pump C.

The inspectors

attended the pre-evolution brief and witnessed the test from the

control and switchgear rooms.

Motor currents and voltages were

measured at seli!cted pump fl ow rates. The 1 icensee calculated

that the motor power requirements were 711 horsepower based on

data obtained during the test.

At the end of the inspection period, the licensee was evaluating

this issue. Resolution of the issue will be addressed during the

unit startup assessment at the end of the RFD.

The inspectors

concluded that the evaluation and initial corrective actions

implemented to resolve this issue were timely and conservative.

Periodic Safety Bus Logic Testing

On February 4, the inspectors observed Unit 2 safety bus logic

testing. Procedure 2-0PT-ZZ-002, ESF Actuation With Undervoltage

and Degraded Voltage - 2J Bus, revision 5, is a complex evolution

which verified proper logic circuit actuation for over twenty

safety related protective signals. A senior operations manager

provided an additional level of test oversight in accordance with

VPAP-0108, Infrequently Conducted or Complex Tests or Evolutions,

revision 0.

Procedure 2-0PT-ZZ-002 had recently been revised to

incorporate TS revisions and eliminate a redundant EOG start. The

test director, a licensed SRO, conducted personal briefings with

over thirty individuals during the prior week specifically

discussing their responsibilities during the test. The pre-

evolution brief emphasized communications and self checking.

7

The inspectors concluded that station preparations for the test

and management oversight were very good.

Two unexpected occurrences were encountered early in the test.

First, during degraded voltage EDG cold start testing, EDG No. 3

did not align to the Unit 2 safety bus as required.

The test

di rector qui ckl:, recognized the cause to be an error in the

recently revised procedure.

The EDG loaded properly for the

switch al i gnmen*: which had been es tab l i shed in the procedure.

The test director temporarily halted the test to ensure the EDG

alignment and p*lant conditions were clearly understood.

Following

discussion with system engineers and the test director, the senior

operations manager directed the test director to proceed with the

test. System engineers initiated an appropriate procedure

revision to correct the EDG alignment problem.

The second problem

occurred when operators experienced difficulty unloading the No. 3

EDG due to an apparent voltage mismatch.

Operations, maintenance,

and engineering personnel conducted non-intrusive troubleshooting

and identified the cause to be a loose connector on a voltage

meter within the remote EDG control cabinet. The connector was

tightened and the test continued. The shift supervisor

appropriately controlled plant activities to ensure operators were

not unduly challenged during conduct of logic bus testing. The

inspectors concluded that operations personnel resolved unexpected

occurrences during the test evolution in a deliberate and safe

manner.

The te;t director maintained clear communication and

oversight throughout the test.

Within the areas inspected, no violations or deviations were identified.

6.

Onsite Engineering Review (37551, 38703)

6.1

Procurement of TDAFWP Governors

On January 8 the Unit 1 TDAFWP tripped on demand due to a turbine

overspeed condition. While the initial licensee's RCE did not

identify a definite cause, degraded governor performance was

postulated to be the most likely cause.

Improved Woodward model

PG-PL governors had previously been installed for Unit 1 (1990)

and Unit 2 {1991) in accordance with DCP 88-16-3, AFW Turbine

Governor Replacement Unit 1&2.

In December 1994, the Unit 1

TDAFWP governor was replaced with a spare governor {serial no.

2435227) which had been stored in the warehouse since procurement

in 1990.

The inspectors reviewed the procurement and CGD of these

governors to determine whether governor quality and performance

had been properly validated for their safety related application.

6.1.1 Purchase Orders and Material Specification

Three PG-PL governors were purchased commercial grade using

PO CNT 299814 and were dedicated by a third party under PO

CNT 301368 for use in safety-related applications. Both POs

8

incorporated material specification NUS-2203/NAP-0007,

revision 3, which detailed the technical and QA requirements

for the fabrication, testing, inspection, documentation, and

shipment of the governors.

The inspectors noted that

responsibility for performing the various specified tests

was not clearly stated in the material specification. Three

tests specified in the POs were not performed by the

vendors.

Project engineers stated that the three tests

which were not performed by vendors were intended to be

post-instilllation licensee tests, not vendor tests. The

licensee *informed the inspectors that responsibility and

scheduling of specific tests were clarified at post award

conferences with the vendors.

The inspectors independently

confirmed that each of the tests listed in NUS-2203/NAP-0007

were satisfactorily completed for the two governors

installed in 1990 and 1991 by DCP 88-16-3.

Both POs were

well writ:en and NUS-2203/NAP-007 was thorough in specifying

governor performance criteria, QA criteria, and support

requirements (i.e., vendor technical manuals, drawings,

material handling information).

6.1.2 Storage and Handling

The inspectors toured material storage facilities,

interviewed personnel, and reviewed receipt records to

determine whether the model PG-PL governors were properly

stored after procurement.

The POs specified Level C

packaging and storage requirements consistent with ANSI

N45.2.2 - 1972, Packaging, Shipping, Receiving, Storage, and

Handling of items for Nuclear Power Plants.

No special

packaging or storage instructions were specified by the

vendor.

Governor 2435227 was stored in a Class B storage

area, which fully satisfied the requirements of Level C

storage, upon receipt in 1990.

The storage warehouses were

clean, dry, and properly monitored for temperature extremes.

In November 1994, governor 2435227 was directly transported

by a company employee to and from a test facility in a

clean, climate controlled vehicle.

The inspectors noted

that the governor had not been packaged in a waterproof

enclosure which would be typical for Level C shipments.

Materials management stated that in this instance, delivery

under the direct control of a company employee provided

equivalent protection from the environment as would have

been obtained by using Level C packaging and shipping the

governor via contract carrier. The inspectors determined

that packaging/handling of the spare governor during

delivery to the test facility was acceptable.

Management

subsequen~ly initiated appropriate action to ensure that

packaging requirements for direct off-site deliveries of

material, which bypass the normal contract carrier shipment

process, are evaluated on a case-by-case basis. The

9

inspectors determined that storage and handling of the spare

governor was acceptable based on licensee's program

controls.

Subsequen~ to the January 1995 TDAFWP failure, the licensee

obtained additional storage recommendations from the vendor

which had not been provided under the original PO.

The

licensee *is reviewing this information for future

applications. Governor 2435227 was disassembled and

visually inspected after the January 1995 failure. Material

condition appeared good with no indications of improper

storage. The inspectors concluded that storage and handling

of model PG-PL governors was acceptable.

6.1.3 Test Records

Test requirements for the PG-PL governors were specified in

NUS-2203/NAP-0007.

Initial vendor testing was performed at

the manufacturer's facility under the oversight of licensee

QA personnel and third party engineers. Seismic testing to

support the third party CGD was performed at an independent

safety related test facility. The inspectors reviewed the

third party CGD test plan performed under PO CNT 301368 and

verified ~hat critical component characteristics such as

dimension:; and testing were identified for model PG-PL

governor and that these had been successfully demonstrated.

Post installation testing of the model PG-PL governor was

performed on Unit 1 and Unit 2 while implementing

DCP 88-16-3.

The DCP was generally well written. However,

the inspectors noted that the Functional Testing

Requirements and Acceptance Criteria section did not include

two of the tests specified in NUS-2203/NAP-0007.

This was a

weakness in the development of the DCP.

The inspectors

discussed this observation with project engineers who stated

that recent improvements in the DCP process have clarified

what items are to be listed as functional test requirements

and there!~ reduced the likelihood of similar omissions.

The inspectors reviewed STD-GN-0001, Instructions for DCP

Preparation, revision 13, and noted that the current

procedure provides good instruction for identifying

functional test requirements.

VPAP-0301, Design Change Processes, revision 4, specifies

that the post modification test plan be developed based upon

the functional test requirements section of the DCP.

System

engineers recognized that although not listed in the DCP, a

post installation system stability test was needed.

Engineers added the speed regulation and maximum speed rise

tests as described in NEMA SM 23-1985, Steam Turbines for

Mechanical Drive Service. These were the same two tests

identified in NUS-2203/NAP-0007 which were not listed in the

~.

..

10

DCP functional test section. The inspectors reviewed DCP

88-16-3 test records and determined that all tests specified

in the original material specification, were successfully

completed by the final post modification test plan.

The

inspectors noted that the post installation stability

testing performed on Units 1 and 2 during implementation of

DCP 88-16-3 was not performed when the Unit 1 governor was

replaced in December 1994.

The inspectors specifically

questioned why the speed rise test was not performed for

governor 2435227.

Project engineers stated that governor

2435227 had been dedicated for safety related use by

PO CNT 301368 and that critical component characteristics of

the governor type were verified. Additionally, engineers

indicated that the post installation testing specified in

DCP 88-16-3 was intended to be a design validation test.

Therefore, similar testing of a l i ke-for-1 i ke replacement

governor was not necessary as part of the PMT.

The

inspectors agreed with the licensee's position.

6.1.4 Governor Shelf-life

The CGD test report from a safety-related vendor recommended

a 10 year PG-Pl governor design life based on the presence

of Buna-N materials internal to the governor.

Project

engineers evaluated the recommendation and determined that

the PG-Pl governor should not be assigned a design or shelf-

life of less than 40 years. This conclusion was based upon

oral communications with the vendor who indicated that the

Buna-N components had most likely been upgraded to Viton

material which has a longer design life. The manufacturer

had begun using Viton in place of Buna-N in the 1990

timeframe.

The material list provided with the governor and

the CGD test report indicated that the components were made

of Buna-N.

The inspectors questioned whether the licensee

had sufficient assurance that the governors were upgraded to

Viton internal components.

The inspectors determined that

absence of documentation to support the governor shelf-life

determination was an isolated weakness.

VPAP-0704, Shelf

life Evaluation and Control, revision 2, provided good

instructions for shelf-life evaluations. Procurement

engineers requested that the vendor provide an updated

governor material list and report the material type

identified during the recent (February 1995} diagnostic

disassembly of governor 2435227.

The inspectors determined

that these actions were appropriate to verify the correct

material composition of the govetnors.

6.1.5 Commercial Grade Dedication

The model PG-Pl governors were commercially grade dedicated

in 1990 by a third party vendor under PO CNT 301368.

The

inspectors confirmed that the licensee had properly

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certified the third party vendor to perform safety-related

services. The governors were received as safety-related

material.

In November 1990 the licensee issued PO BNT 484751 to a

non-safety related vendor to adjust the governor 2435227

high speed stop and perform associated governor performance

testing. The inspectors reviewed procurement documents and

interviewl!d licensee personnel to determine whether vendor

services were appropriately dedicated.

PTE SSEROOI9.002 and

CGIE SSEROOI9.002 were developed to identify critical

performance characteristics to be tested and specify

acceptance criteria. The PTE and CGIE were detailed and

properly \\iritten in accordance with station procedures. The

licensee provided QA and technical oversight at the vendor's

test facility. The QA VFIR properly documented successful

verification of each critical characteristic listed in

CGIE SSEROOI9.002.

No parts were replaced on governor

2435227 at the vendor's facility. Procurement engineers

demonstrated indepth knowledge regarding the CGD processes.

The inspectors concluded that the licensee appropriately

commercial grade dedicated the vendor services provided

under PO BNT 484751 .

6.1.6 Summary

Model PG-PL TDAFWP governors were purchased commercial grade

and were commercially grade dedicated for use in safety-

related applications by a third party.

Procurement

documents including the material specification were

detailed. Isolated weaknesses regarding DCP development. and

shelf life evaluation were identified. Appropriate actions

to addres:; these weaknesses were initiated. Storage,

handling, and CGD of the vendor services were appropriate.

6.2

Effectiveness of RCE Process

The licensee's RCE for the January 8, Unit I TDAFWP failure was

discussed in NRC Inspection Report Nos. 50-280/94-33 and

50-281/94-33.

The licensee's RCE team concluded that the most

probable causal factors were "Equipment Condition" and

"Maintenance/Testing Practices." The team's findings indicated

that governor 2435227, which was in-place during the January 8

overspeed trip was suspect since diverging oscillations were only

experienced with that governor. Additionally, the team determined

that maintenance/testing was a causal factor because of inadequate

vendor TM instructions and PMT instructions.

In this area the

team concluded ~hat the vendor had critical information to set-up

the governor and linkage in the field. This information was not

contained in a written procedure or available to the Virginia

Power personnel who performed governor replacement and linkage

refurbishment during the December 1994 SGCC outage.


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12

Based on review of the RCE team's log book and meeting with team

members, the inspectors noted that although their efforts were

extensive the RCE failed to determine why governor 2435227 behaved

as it did on January 8.

Within the areas inspected, no violations or deviations were identified.

7.

Plant Support (71750)

The inspectors observed radiological control practices and radiological

conditions throughout the plant. Radiological posting and control of

contaminated areas was good.

Workers complied with radiation work

permits and appropria~ely used required personnel monitoring devices.

The protected area security perimeter was well maintained with no

equipment or debris obstructing the isolation zones.

Within the areas inspected, no violations or deviations were identified.

8.

Action on Previous Inspection Items (92702)

(Closed) URI 50-280/94-33-01, Issues Relating to Unit 1 TDAFWP Failure.

This item resulted from the NRC's review of the January 8, 1995,

overspeed trip of the TDAFWP.

The inspectors identified the following

topics as part of URI 50-280/94-33-01:

1.

Acceptability of controlling work activities using WOs in

lieu of detailed SNSOC approved procedure.

2.

. Possible *impact of CGD process used for governor

procurement, repairs and testing conducted by the vendor.

3.

Storage requirements for the governor in the warehouse.

4.

Control of vendor information and vendor activities.

5.

Effectiveness of root cause process.

The inspectors' review of these items is discussed in sections 4.1, 4.2,

6.1 and 6.2 of this report.

Within the areas inspected, one violation as .discussed in section 4.1

was identified.

9.

Exit Interview

The inspection scope and findings were summarized on February 15, 1995,

with those persons indicated in paragraph 1. The inspectors described

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the areas inspected and discussed in detail the inspection results

addressed in the Summary section and those listed below.

Item Number

URI 50-281/95-03-01

Status

Open

Description/(Paraqraph No.)

Unit 2 Pressurizer Excessive

Heatup Rate (paragraph 3.2).

VIO 50-280/95-03-02

Open

Failure to Use Approved

Detailed Procedures

(paragraph 4.1).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

10.

Index of Acronyms and Initialisms

AFW

ANSI

CFR

CGD

CGIE

DCP

DR

ECCS

EDG

ESF

F

HHSI

NEMA

NRC

PMT

PO

PPR

PTE

QA

RCE

RCS

RFO

SGCC

SI

SNSOC

SRO

TDAFWP

TM

TS

TSCS

URI

VFIR

VIO

VPAP

WO

%

AUXILIARY FEEDWATER

AMERICAN NATIONAL STANDARDS INSTITUTE

CODE OF FEDERAL REGULATIONS

COMMERCIAL GRADE DEDICATION

COMMERCIAL GRADE ITEM EVALUATION

DESIGN CHANGE PACKAGE

DEVIATION REPORT

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

FAHRENHEIT

HIGH HEAD SAFETY INJECTION

NATIONAL ELECTRICAL MANUFACTURES ASSOCIATION

NUCLEAR REGULATORY COMMISSION

POST MAINTENANCE TESTING

PURCHASE ORDER

POTENTIAL PROBLEM REPORT

PROCUREMENT TECHNICAL EVALUATION

QUALITY ASSURANCE

ROOT CAUSE EVALUATION

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

STEAM GENERATOR CHEMICAL CLEANING.

SAFETY IN,JECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SENIOR REACTOR OPERATOR

TURBINE DRIVEN AUXILIARY FEEDWATER PUMP

TECHNICAL MANUAL

TECHNICAL SPECIFICATION

TURBINE SPEED CONTROL SYSTEM

UNRESOLVED ITEM

VENDOR FINAL INSPECTION REPORT

VIOLATION

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER

PERCENT