ML18152A271

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Insp Repts 50-280/98-01 & 50-281/98-01 on 971228-980207. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML18152A271
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/05/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18152A272 List:
References
50-280-98-01, 50-280-98-1, 50-281-98-01, 50-281-98-1, NUDOCS 9803180111
Download: ML18152A271 (21)


See also: IR 05000280/1998001

Text

Docket Nos:

License Nos:

Report Nos:

Licensee: *

Facility:

Location:

Dates:

Inspectors:

Approved by:

9803180111 980305

PDR

ADOCK 05000280

G

PDR

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

50-280. 50-281

DPR-32. DPR-37

50-280/98-01. 50-281/98-01

Virginia Electric and Power Company (VEPCO)

Surry Power Station. Units 1 & 2

5850 Hog Island Road

Surry. VA 23883

December 28. 1997 - February 7. 1998

R. Musser. Senior Resident Inspector

K. Poertner. Resident Inspector

R. Gibbs. Reactor Inspector (Sections M8.l through

M8.7 and X2)

H. Whitener. Reactor Inspector (Sections Ml.2 and

Ml.3)

R. Haag, Chief. Reactor Projects Branch 5

Division of Reactor Projects

Enclosure 2

EXECUTIVE SUMMARY

Surry Power Station. Units 1 & 2

NRC Inspection Report Nos. 50-280/98-01. 50-281/98-01

This integrated inspection included aspects of licensee operations.

engineering, maintenance. and plant support.

The report covers a six-week

period of resident inspection; in addition. it includes the results of

announced inspections by two regional reactor inspectors.

Operations

Unit 1 plant response following an automatic reactor trip was normal and

plant systems operated as designed. Subsequent startup activities were

conducted in accordance with approved procedures and in a controlled

manner.

Operator actions during initial power escalation and placing

the generator on line were well coordinated (Section 01.2).

The licensee was unable to identify the cause of the Unit 1 voltage

regulator failure that resulted in a reactor trip. The voltage

regulator was in manual at the time of the trip. The unit was returned

to service with the voltage regulator in automatic (Section 01.2).

Cold weather preparations were adequately implemented and were in

accordance with approved procedures (Section 01.3).

Adequate procedural controls were implemented to ensure the Number 3

Emergency Diesel Generator fuel oil supply was adequate to meet design

basis requirements (Section 01.4).

A review of the Institute of Nuclear Power Operations operating plant

evaluation report was performed and no further follow-up is planned

(Section 01.5).

The Unit 2 high head safety injection system was properly aligned and in

generally good condition (Section 02.1).

Maintenance

A violation of 10 CFR 50. Appendix B. Criterion XVI was identified for

failure to promptly correct a degraded Number 3 Emergency Diesel

Generator auxiliary oil pump motor (Section Ml.1).

Replacement of a gamma-metrics excore power supply was performed

successfully.

The technicians demonstrated attention to detail and a

questioning attitude while following up on the cause of the power supply

failure (Section Ml.2).

Surveillance activities involving the analog rod position system .

charging pump operability and the reactor trip portion of the reactor

protection system were completed in a thorough and professional manner.

Personnel were knowledgeable of the assigned tasks.

Procedures were

detailed and actively used (Section Ml.3).

2

  • The licensee has made significant improvements since the original

Maintenance Rule baseline inspection and now has a very comprehensive

Maintenance Rule program (Sections MB.1 through MB.7).

Engineering

Temporary Modification Sl-98-02 to install a temporary resistance

temperature detector in the C main feedwater line was adequately

implemented and the associated safety evaluation justified

implementation of the temporary modification (Section El.1).

Plant Support

Health physics practices were observed to be proper (Section Rl).

Security and material condition of the protected area perimeter barrier

were acceptable (Section Sl) .

Report Details

Summary of Plant Status

Unit 1 operated at power until February 2. 1998 when the unit automatically

tripped from 100 percent power (See Section 01.2). The unit*was returned to

service on February 4. 1998.

The unit operated at power for the remainder of

the inspection period.

Unit 2 operated at power the entire reporting period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707. 40500)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness. and adherence to approved procedures.

The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

CTSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping.

Deviation Reports (DRs) were reviewed to assure that potential safety

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

01.2 Unit 1 Reactor Trip and Restart

a.

Inspection Scope (71707)

The inspectors reviewed the plant response following a reactor trip and

monitored licensee activities during the unit restart.

b.

Observations and Findings

On February 2. 1998. at approximately 5:26 a.m. with the unit at 100

percent power. Unit 1 experienced a reactor trip following a main

generator trip. The generator trip resulted in a turbine trip and

subsequent reactor trip on turbine trip. The unit was stabilized at hot

shutdown with temperature being maintained via the steam dumps to the

main condenser.

At the time of the reactor trip the generator voltage regulator was

being operated in base adjust (manual) due to failure of the automatic

portion of the voltage regulator earlier in the cycle. Approximately

one minute after the main generator voltage was adjusted by an operator.

a low voltage alarm was received in the control room and the generator

C.

2

tripped on a differential lockout signal. Voltage had dropped from

approximately 22.5 Kilovolts (kV) to 18.5 kV just prior to the unit

trip.

The inspectors reviewed the plant response following the unit trip. All

systems functioned as designed. Auxiliary feedwater actuated on low

steam generator level following*the trip as required and no primary or

secondary relief valves actuated. All control rods indicated less than

10 steps following the trip and all rod bottom lights lit. The

inspectors attended the post trip review meeting conducted after the

unit was stabilized.

The licensee initiated troubleshooting of the generator voltage

regulator to determine the cause of the generator trip. A vendor

representative assisted in the troubleshooting effort. Testing of the

voltage regulator did not identify a specific failure mechanism.

however. a bad relay in the automatic portion of the circuity was

identified and replaced. This relay prevented operation of the voltage.

regulator in automatic.

The troubleshooting effort also identified a

loose wire in an alarm circuit that was repaired prior to restart. The

licensee (with vendor assistance) performed checks of the voltage

regulator in automatic and manual and determined that the regulator was

operating properly .

The unit was returned to service on February 4. 1998. with* the generator

voltage regulator in automatic.

The inspectors reviewed the trip report

and diicussed the voltage regulator troubleshooting efforts with plant

management prior to restart of the unit.

The inspectors observed

portions of the unit restart. Activities observed were conducted in

accordance with approved procedures. and operator actions during initial

power escalation and placing the generator on line were well coordinated

and performed in a controlled manner.

Conclusions

Unit. 1 plant response following an automatic reactor trip was normal and

plant systems operated as designed.

Subsequent startup activities were

conducted in accordance with approved procedures and in a controlled

manner.

Operator actions during initial power escalation and placing

the generator on line were well coordinated (Section 01.2).

The licensee was unable to identify the cause of the Unit 1 voltage

regulator failure that resulted in a reactor trip. The voltage

regulator was in manual at the time of the trip. The unit was returned

to service with the voltage regulator in automatic (Section 01.2).

01.3 Cold Weather Preparations

a . Inspection Scope (71714)

The inspectors reviewed the licensee's program to protect safety related

systems against extreme cold weather.

3

b.

Observations and Findings

The licensee implements cold weather protection from October through

March.

The program is controlled by procedure O-OSP-ZZ-001. "Cold

Weather Protection." and procedure O-EPM-1303-01. "Freeze Protection

Inspection." Procedure O-OSP-ZZ-001 is performed by operations

personnel to walk down systems and components and procedure O-EPM-1303-

01 is performed by electrical maintenance personnel to verify proper

operation of heat tracing and strip heaters.

The licensee also

implements cold weather protection utilizing Operations Checklist-21.

"Severe Weather." The checklist is implemented based on outside air

temperature.

The inspectors verified that procedures O-OSP-ZZ-001 and O-EPM-1303-01

had been implemented as required.

The procedures are performed monthly

during the time period that cold weather protection is required.

The

inspectors reviewed the procedures and verified that identified

discrepancies were addressed prior to the onset of cold weather.

During

periods of cold weather the inspectors performed tours of station areas

and equipment to verify cold weather preparations were effective and

discussed cold weather preparation activities with cognizant licensee

personnel.

No discrepancies were identified during these reviews.

c. Conclusions

Cold weather preparations were adequately implemented and were in

accordance with approved procedures.

01.4 Emergency Diesel Generator (EOG) Number 3 Fuel Oil Supply

a.

Inspection Scope (71707)

The inspectors reviewed licensee actions associated with a 50.72

(b)(l)(ii)(C) one-hour non-emergency event report concerning the

Number 3 EOG fuel oil capacity requirements.

b. Observations and Findings

On February 6, 1998. the licensee identified a condition where the

Number 3 EOG would not meet the design basis fuel ciil supply

requirements.

The Updated Final Safety Analysis Report and Technical

Specifications require that a minimum of 35,0000 gallons of fuel oil be

available.

The 35,000 gallon requirement is based on full load

operation of one EOG for seven days.

The safety related portion of the

fuel oil transfer system consists of two 20,000 gallon underground

storage tanks that are not cross connected under normal operation.

The

underground storage tanks provide fuel oil to all three EDGs.

Each EOG

is provided with two fuel oil transfer pumps that take a suction on a

separ~te underground storage tank and discharge to the associated EOG

day tank .

4

One fuel oil transfer pump for the Number 3 EOG is powered from the Unit

1 J emergency bus and the other fuel oil transfer pump is powered from

the Unit 2 J emergency bus.

During a loss of offsite power to the

station the Number 3 EOG will automatically start and energize either

the Unit 1 or Unit 2 J emergency bus.

This results in one unit's J

emergency bus not being energized and one fuel oil transfer pump not

. being available to supply fuel oil to the Number 3 EOG.

With only one

fuel oil transfer pump available. a seven-day supply of fuel oil would

not be available to the Number 3 EOG unless actions were taken to cross

connect the fuel oil storage tanks or to cross connect the non-energized

J emergency bus with the H emergency bus for that unit.

Neither of

these actions were addressed in the Emergency Operating Procedures

(EOPs).

Based on the potential to have less than a seven-day supply of

fuel oil available to'the Number 3 EOG. the licensee declared one of the

two fuel oil flow paths to the Number 3 EOG inoperable and entered a 24-

hour TS limiting condition of operation to return the flow path to an

operable status or declare the Number 3 EOG inoperable.

The licensee

notified the NRC via a one-hour non-emergency event report that the

plant was operating in a condition not covered by the plant's operating

or emergency procedures.

The licensee revised the EOPs to require that power on the J emergency

buses be verified following entry into the EOPs.

If a unit's J

emergency bus is not energized. the EDP requires entry into an Abnormal

Operating Procedure to transfer oil from the above ground fuel oil

storage tank to the underground fuel oil storage tanks if available or

to cross connect the deenergized J emergency bus to the unit with the

energized H emergency bus after stripping unnecessary loads. After

implementation of the procedural controls. the licensee declared both

fuel oil flow paths operable.

The procedural controls were implemented

prior to exceeding the 24-hour TS limiting condition of operation.

The inspectors reviewed the licensee's safety evaluations and

corresponding procedure changes and found them adequate to control the

operation of the Number 3 EOG fuel oil transfer pumps following a loss

of offsite power to the station. The inspectors were still reviewing

this item at the end of the inspection period and further review of EOG

fuel oil requirements is identified as Inspection Followup Item (IFI)

50-280, 281/98001-01.

c. Conclusions

Adequate procedural controls were implemented to ensure the Number 3 EOG

fuel oil supply was adequate to meet design basis requirements.

An

Inspection Followup Item was identified to review EOG fuel oil

requirements .

5

01.5 Institute of Nuclear Power Operations (INPO) Operating Plant Evaluation

Report

a.

Inspection Scope (71707)

The inspectors reviewed the INPO evaluation report dated January 7.

1998. for the evaluation conducted during April 1997.

b.

Observations and Findings

On January 13-14. 1998. the inspectors reviewed the INPO operating plant

evaluation report for the review conducted in April. 1997.

Based on

this review of the INPO evaluation. no further follow-up is planned.

c . Cone l us i oris

A review of*the Institute of Nuclear Power Operati*ons operating plant

evaluation report was performed by the inspectors and no further follow-

up is planned.

02

Operational Status of Facilities and Equipment

02.1 High Head Safety Injection

a.

Inspection Scope (71707)

During the inspection period the inspectors performed a walkdown of the

Unit 2 high head safety injection system.

b.

Observations and Findings

The inspectors performed a walkdown of accessible components associated

with the Unit 2 high head safety injection system.

The walkdown

encompassed the pump suction piping from the refueling water storage

tank and the pump discharge piping up to the containment penetrations.

The inspectors referenced the system piping and instrument diagrams and

procedures 2-0P-SI-OOlA. "Safety Injection System Alignment." and 2-0P-

CH-OOlA. "CVCS Valve Alignment." for proper system alignment and

component descriptions.

The inspectors checked system hangers and supports. general

housekeeping, valve positions. and labeling.

The inspectors determined

that the system was properly aligned and in generally good condition.

The inspectors verified that the valve alignment procedures adequately

aligned the system for normal operation.

c.

Conclusions

The Unit 2 high head safety injection system was properly aligned and in

generally good condition.

6

II. Mai'ntenance

Ml

Conduct of Maintenance

Ml.1 Inadequate Evaluation of Number 3 EOG Auxiliary Oil Pump Motor Vibration

Data

a.

Inspection Scope (62707)

b.

The inspectors conducted a review of the circumstances leading to and

following the failure of the Number 3 EOG auxiliary oil pump.

Observations and Findings

On January 29. 1998, operators in the control room received a Number 3

EOG trouble alarm. Operators were dispatched to the Number 3 EOG room

and determined that the auxiliary oil pump had failed.* Earlier in the

shift. operations personnel performing a tour of the diesel room noted a

noise coming from the auxiliary oil pump motor.

The noise was

indicative of metal to metal contact on the outboard side of the pump

motor.

The shift was in process of planning the replacement of the

motor when the failure occurred.

The EOG was declared inoperable and a

72-hour limiting condition for operation was entered.

The pump motor

was replaced and the EOG was returned to service later that same day .

The following day, the auxiliary oil pump was noted to have vibration

readings greater than those observed the previous day following the

motor replacement.

The EOG was again taken out of service. and the pump

was replaced.

Vibration readings were acceptable and the EOG was

returned to service.

An examination of the Number 1 and 2 EOG auxiliary

oil pump vibration readings did not indicate that their failure was

eminent.

The licensee continues to monitor all the EOG auxiliary oil

pumps and motor vibrations at an increased frequency.

A category 2 root cause evaluation. performed by the licensee. developed

proposed corrective actions to address the vibration issue.

Proposed

corrective actions included preparing a design change to allow the

installation of the auxiliary oil pump and motor as a skid and to change

the suction and discharge piping to flexible metal hose.

Approximately 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> following the Number 3 EOG auxiliary oil pump

motor failure. the inspectors toured the EOG room and observed a work

request tag (number 070525) in the vicinity of the failed pump.

The tag

stated that the vibration of the pump motor was at higher than normal

levels and that the motor bearings were degraded.

The tag was dated

January 14, 1998, which was fifteen days prior to the failure of the

motor.

The work request was initiated following discovery that the pump

motor vibration readings had increased. The increased vibration

information was not forwarded to or reviewed by cognizant technical

personnel. Therefore, the significance of the increased vibration was

not adequately assessed and the repair work effort was only given a

normal priority classification. Further review of the pump vibration

7

data indicated that the auxiliary oil pump had been operating at

increased vibration levels for several months prior to the increase that

was measured on January 14. 1998. Discussions with cognizant licensee

personnel revealed that the auxiliary oil pump motor's increased

vibration readings were a valid indication of the motor's degrading

condition which should have been acted upon.

The licensee's failure to

act upon this information is considered an example of inadequate

corrective action and is a violation of 10 CFR 50. Appendix B. Criterion

XVI. Corrective Action. This matter will be tracked as Violation (VIO)

50-280, 281/98001-02.

c.

Conclusions

A violation of 10 CFR 50. Appendix B. Criterion XVI was identified for

failure to promptly correct a degraded Number 3 Emergency Diesel

Generator auxiliary oil pump motor.

Ml.2 Power Supply Replacement for Gamma-Metrics Monitoring System

a.

Inspection Scope (62707)

The inspectors observed the corrective maintenance to replace a failed

low voltage power supply for the Gamma-Metrics Excore Neutron Monitoring

System.

b.

Observations and Findings

On January 6, 1998, the inspectors observed the replacement of the low

voltage power supply for excore detector indicators in accordance with

1-CAL-510. *Gamma-Metrics Excore Neutron Flux Monitoring System White

Channel NFD 1270.* Revision 7. This was corrective maintenance

performed under Work Order (WO) 00380561.

The problem was that the

channel monitoring indicators failed to zero.

The inspectors verified that breaker tagout SI 98-NI-001 was performed

and verified by technicians prior to starting the job.

The technicians

were methodical and precise in lifting and landing leads.

Each lead was

entered into the lifted lead log and double verified before proceeding

to the next wire.

Independent verification was performed after all

leads were lifted or landed.

When all leads had been lifted. taped.

logged and verified. the technicians removed the hard wired board

containing the low voltage power supply from the control cabinet.

The

cause of the failure was overheating of a shorted transformer which had

released gas and ruptured the casing of the power supply.

Some

discoloration of the board could be observed on close inspection.

The

technicians took the board to a module repair specialist who verified

that the hard wiring on the board was not damaged prior to replacing the

power supply.

The technicians demonstrated a questioning attitude and

attention to detail in -the performance of the task .

8

c. Conclusions

Replacement of a gamma-metrics excore power supply was performed

successfully.

The technicians demonstrated attention to detail and a

questioning attitude while following up on the cause of the power supply

failure.

Ml.3 Surveillance Observations

a.

Inspection Scope (61726)

The inspectors observed all or portions and/or reviewed documentation

for the surveillances discussed below.

b.

Observations and Findings

Charging Pump Operability and Performance Test

On January 7. 1998. the inspectors attended the pre-job briefing in the

Unit 1 control room for the monthly operability and performance test of

charging pump 1-CH-P-lA.

The briefing was thorough.

Procedure 1-0PT-

CH-001. "Charging Pump Operability and Performance Test For 1-CH-P-lA."

Revision 24. was walked-through by the test director. Responsibilities

were assigned. questions were answered and precautions. limits and

communications were discussed.

The inspectors accompanied operators to the field and observed the

positioning of various system valves. instrument valves and electrical

breakers per procedure 1-0PT-CH-001.

The procedure was present and

followed.

The steps were signed off as they were accomplished.

The

operators were familiar with the task.

Analog Rod Position Indication System Functional Test

On January 7. 1998. the inspectors observed the operability test on the

Unit 1 rod bottom bistables performed in accordance with procedure 1-IT-

FT-RI-001. "Analog Rod Position Indication System Functional Test."

Revision 1.

The test involved setting up instrumentation to input a

voltage signal to the rod bottom bistables and varying the signal to

determine at what voltage and rod position the bistables would trip.

The test also verified consistency between the relay racks and the

control room position indicators. Annunciator response was also

verified.

The procedure was detailed and was followed step-by-step. Signoffs and

setpoints were recorded as steps were performed and compared to the

acceptance range specified in the procedure.

One bistable was below the

acceptance range and was corrected on the spot. Three other bistable

setpoints were near the low end of the acceptance range and were

adjusted to the center of the tolerance range. Test instrument

calibrations were current. and personnel were knowledgeable of the

tasks.

9

Reactor Protection System Logic Test

On January 8. 1998. the inspectors observed portions of logic testing

conducted per 1-PT-8.1. "Periodic Test of the Reactor Trip Portion of

the Reactor Protection System." Simulated sensor signals were input to

the logic circuits from the test panel and operation of the logic relays

was confirmed by annunciators and indicator lights.

Pumps and valves

were not actually operated since the system was in a test configuration.

The inspectors observed the majority of test from the reactor trip

breaker cubicle.

Both maintenance. operations. and the shift supervisor

had responsibilities in performing the actual trip of the main reactor

trip breaker.

The reactor trip bypass breaker was tested and then put

into service.

Instrumentation was set up to measure the closure time of

the main reactor trip breaker.

The coordination of the station groups

was excellent.

Instrument calibration was current. the procedure was

present and carefully followed. and communications between relay room.

control room and the breaker cubicle were good.

Review of the procedure

showed that it was detailed and thorough.

In the course of this test.

192 logic functions were verified.

The operators and technicians were properly aware of the potential to

trip the reactor. The test personnel performed the procedure

methodically and demonstrated a knowledge of the systems and task.

c. Conclusions

Surveillance activities involving the analog rod position system.

charging pump operability and the reactor trip portion of the reactor

protection system were completed in a thorough and professional manner.

Personnel were knowledgeable of the assigned tasks.

Procedures were

detailed and actively used.

MB

Miscellaneous Maintenance Issues (92902, 62706)

M8.1

(Closed) EEI 50-280. 281/97001-09:

Inadequate corrective action for

self-assessment deficiencies. This item became an escalating and

mitigating factor in the enforcement package for EA 97-055. and as a

result was not issued as a part of the Notice of Violation.

Followup to

the licensee's corrective actions for Maintenance Rule self-assessments

during the North Anna Maintenance Rule baseline inspection determined

that corrective actions were acceptable with some minor weaknesses.

During this inspection. the inspectors reviewed the corrective actions

for the licensee's January 13. 1997. Maintenance Rule self-assessment

and the January 9. 1997. Sargent & Lundy assessment at Surry. and

determined that the status of each item was well known. corrective

actions were well documented. and corrective actions for identified

problems were adequate.

M8.2

(Closed) IFI 50-280. 281/97001-02:

Followup on licensee actions to

provide performance criteria for structures after industry resolution of

this issue. This item was issued to review the Maintenance Rule

10

structures performance criteria at Surry following development of an

industry standard in that area.

The industry guideline was approved by

the NRC in Regulatory Gui de 1.160. Revision 2. dated March 1997.

The

inspectors reviewed the licensee's instruction. Technical Report CE

0087. "Guidelines for Monitoring of Structures Surry Power Station."

Revision 2. and determined that the guidance for performance criteria

had been incorporated.

In addition. the inspectors reviewed the status

of the inspection of structures at Surry, and determined that all

accessible structures had been subjected to an initial baseline

inspection by the licensee.

MB.3

(Closed) VIO EA 97-055. 01013:

Inadequate goals and monitoring for the

Emergency Switchgear (ESG) Heating Ventilation and Air Conditioning

(HVAC) system. This violation identified that the licensee had not

established adequate goals and monitoring for the ESG HVAC system in

accordance with 10 CFR 50.65. the Maintenance Rul.e.

As a result of this violation and the other violations identified in the

Maintenance Rule baseline inspection and issued in EA 97-055, the

licensee established a Maintenance Rule recovery team to revise and

revalidate Virginia Power's entire Maintenance Rule program. This

recovery team took action to: rescope all SSCs under the Maintenance

Rule; risk-rank the SSCs; revise performance criteria to comply with the

guidance in NUMARC 93-01; re-perform the historical review of plant and

industry operating data; and reinforce the necessity for compliance with

10 CFR 50.65.

The inspectors reviewed the results of this effort. and

verified that the results were consistent with the NUMARC guidance for

implementation of the Maintenance Rule.

The inspectors reviewed the

revised scoping matrix. verified by sampling that performance criteria

were in accordance with NUMARC guidance. verified that the historical

review had been completed and that data had been loaded into the

licensee's Maintenance Rule database. and verified that current

monitoring of SSC performance was being accomplished.

In addition. the licensee placed the ESG HVAC system air handling units

and chillers in (a)(l) status under the Maintenance Rule and established

goals and monitoring for this equipment.

The inspectors reviewed the

goals and monitoring and determined they were adequate to meet

Maintenance Rule requirements.

No deficiencies were identified during

this review.

MB.4

(Open) via EA 97-055. 01023:

Failure to demonstrate performance of SSCs

had been adequately controlled through the performance of appropriate

preventive maintenance. This violation identified seven examples of

failure to demonstrate the adequacy of SSCs performance through

appropriate preventive maintenance.

These deficiencies were due to the

failure to establish adequate performance criteria for monitoring SSCs.'

failure to perform adequate historical review of operating data for

SSCs. and failure to adequately evaluate operating data and take

appropriate action under the Maintenance Rule when data indicated

unacceptable performance.

11

The corrective actions. which were accomplished by the licensee's

Maintenance Rule recovery team and verified by the inspector as

discussed under the closeout of EA 97-055. 01013 in Section M8.3 of this

report. apply to the closure of this violation.

In addition. the following specific corrective actions were taken by the

licensee and verified by the inspectors:

Example 1: This example identified that no historical review or

inadequate historical reviews had been done for direct current

power. ESG HVAC. service water. emergency lighting and condensate

polishing systems.

The inspectors verified that the historical

review had been done for each of these systems. the data had been

loaded into the licensee's Maintenance Rule database. and the data

had been evaluated against the new performance criteria for

appropriate actions under the Maintenance Rule.

This example is

closed.

Example 2:

This example identified that the performance criteria

for the radiation monitoring system was inappropriate and failures

of the system had not been adequately evaluated for appropriate

actions under the Maintenance Rule.

The inspectors verified that

new performance criteria had been established for the radiation

monitoring system. the historical review had been done and data

had been loaded into the Maintenance Rule database. *and the data

had been evaluated against the performance criteria for

appropriate actions under the Maintenance Rule.

This example is

closed.

Example 3: This example identi1ied that the performance criteria

for the reactor protection system and the safety injection

actuation system were not commensurate with safety, due to the

fact that they were not in accordance with the licensee's

Probabilistic Risk Assessment (PRA).

The inspector did not review

the specific corrective actions for this item due to the fact that

the Surry PRA has recently been identified to have s*imilar

problems to those identified in the North Anna Maintenance Rule

Baseline inspection conducted in October 1997 and documented in

NRC Inspection Report Nos. 50-338. 339/97-08. Additional review

of performance criteria as they relate to PRA will be conducted

concurrently with a review of the North Anna performance criteria

at a later date. This example remains open.

Example 4: This example identified that there were no performance

criteria established for the risk-significant component cooling

water pumps and the instrument air compressors.

The inspectors

verified that the licensee had established performance criteria

for monitoring these SSCs for reliability and unavailability in

accordance with NUMARC guidance. This example is closed .

Example 5: This example identified that no performance criteria

had been established to monitor setpoint drift of the reactor

12

coolant system code safety*valves. The inspectors verified that

new performance criteria had been established to monitor setpoint

drift of these SSCs.

This example is closed.

Example 6: .This example identified that the licensee had not

adequately evaluated service water system failures under the

Maintenance Rule prior to placing the system in (a)(2) status.

The inspectors verified that the licensee had properly evaluated

the failures. re-classified the system as (a)(l), and established

  • goals and monitoring as required by the Maintenance Rule.

This

example is closed.

Example 7:

This example identified that the licensee had not

established reliability performance criteria to monitor the

standby functions of the electro-hydraulic control system. bearing

cooling system. boric acid transfer pumps (emergency boration

mode). the auxiliary building HVAC, and the control room HVAC in

accordance with NUMARC guidance.

The inspectors verified that

reliability performance criteria were established for these SSCs.

This example is closed.

This violation remains open .. With the exception of example 3, all the

remaining examples of this violation were closed. Additional review is

required for example 3 prior to closure .

MS.5

(Closed) VIO EA 97-055. 01033:

Inadequate instructions concerning cause

determinations for maintenance preventable functional failures. This

item identified that the licensee's Maintenance Rule implementation

procedure provided inadequate instructions for the evaluation of

maintenance preventable function failures under the Maintenance Rule.

The corrective actions. whith were discussed under the closeout of EA 97-055, 01013 above. apply to the closure of this violation:

The inspectors verified that Virgin1a Power Administrative Procedure

VPAP-0815, "Maintenance Rule Program.* Revision 7. had been changed to

be consistent with the NUMARC guidance regarding evaluation of

maintenance preventable functional failures.

The re-evaluation of

historical data under the new requirements would compensate for any

failures evaluated under the old procedural requirements. This

violation is closed.

MS.6 (Closed) VIO EA 97-055. 01043:

Failure to follow procedure concerning

performance criteria for the reactor protection system. This violation

identified that the licensee had failed to obtain working group approval

for a change to the performance criteria for the reactor protection

system in accordance with VPAP-0815, "Maintenance Rule Program.*

Revision 3.

The licensee determined that this problem was caused by a

lack of emphasis on compliance with the Maintenance Rule program.

As a

result. the licensee trained personnel regarding their responsibilities

under the Maintenance Rule.

In addition. the Senior Vice-President.

Nuclear. issued a memorandum reinforcing managements expectations for

13

complete compliance with the Maintenance Rule program. This action was

verified by the inspectors.

M8.7

(Closed) VIO EA 97-055. 01053:

Failure to follow procedure concerning

approval of a risk-significant plant configuration. This violation

involved a failure to follow procedural requirements concerning

management approval of a risk-significant plant configuration. The

licensee has significantly changed the process for risk-evaluation of

on-line removal of equipment from service.

The process now involves

assessment by the licensee's PRA group for any plant configurations not

previously evaluated. This process is defined in VPAP-2001. "Station

Planning and Scheduling." Revision 5. and NAF-97-0086. "PSA (a)(3)

Maintenance Rule Risk - Significant Equipment - Surry Power Station

Units 1&2." Revision 0.

This process was reviewed during the North Anna

Maintenance Rule baseline inspection and found to be acceptable with the

exception of its PRA basis.

The same situation regarding problems with

the PRA exists at Surry, and as a result. additional inspection of this

process will be required after PRA revision. This followup will be

conducted under IFI 50-280. 281/97001-01: Followup licensee actions to

strengthen risk-assessment for on-line maintenance activities. which

remains open from the original baseline inspection at Surry.

Conclusions (Sections M8.1 through M8.7)

The licensee has made significant improvements since the otiginal

Maintenance Rule baseline inspection and now has a very comprehensive

Maintenance Rule program.

III. Engineering

El

Conduct of Engineering

El.l Temporary Modification Sl-98-02

a.

Inspection Scope (37551)

The 1nspectors reviewed Temporary Modification (TM) Sl-98-02 that

installed a temporary replacement Resistance Temperature Detector CRTD)

in the C main feedwater line.

b.

Observations and Findings

On January 15. 1998. the C main feedwater temperature detector 1-FW-RTD-

lllC failed.

Failure of the RTD resulted in the P-250 calorimetric

program being unreliable for determination of reactor power and required

that manual power calculations be performed to determine reactor power.

The licensee determined that the RTD failed due to water intrusion into

the RTD that resulted from a failed thermowell.

The licensee

implemented TM Sl-98-02 to install a temporary replacement RTD in the

thermowell associated with local temperature indicator TI-FW-154C .

Implementation of the TM would allow the P-250 computer calorimetric

14

program to be returned to service and cessation of manual calorimetrics.

The TM was implemented January 16. 1998.

The inspectors reviewed the TM and associated safety evaluation and held

discussions with reactor engineering personnel about implementation of

the TM.

The inspectors determined that the TM was adequately

implemented and that the associated safety evaluation adequately

justified implementation of the TM.

c.

Conclusions

Temporary Modification Sl-98-02 to install a temporary RTD in the C main

feedwater line was adequately implemented and the associated safety

evaluation justified implementation of the temporary modification.

IV. Plant Support

Rl

Radiological Protection and Chemistry Controls (71750)

Sl

On numerous occasions during the inspection period. the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit. survey results. and radiological area material

conditions.

No discrepancies were noted. and the inspectors determined

that RP practices were proper .

Conduct of Security and Safeguards Activities (71750)

On numerous occasions during the inspection period. the inspectors

performed walkdowns of the protected area perimeter to assess security

and general barrier conditions.

No deficiencies were noted and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained.

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on February 20 and on March 2.

1998.

The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary.

No proprietary information was

identified.

X2

Enforcement Meeting

On March 11. 1997. a Predecisional Enforcement Conference for EA Case 97-055.

covered in Inspection Report Nos. 50-280. 281/97-01. was held in the Regional

Office with the licensee in attendance.

The following EEis were discussed:

EEI 50-280.

EEI 50-280.

EEI 50-280.

EEI 50-280.

EEI 50-280.

EEI 50-280.

EEI 50-280.

281/97001-03

281/97001-04

281/97001-05

281/97001-06

281/97001-07

281/97001-08

281/97001-09

15

Following the conference. a Notice of Violation (NOV) was issued on August 29.

1997.

Based on the NOV issued. the above EEis are administratively closed.

with the exception of EEI 50-280. 281/97001-09 which is closed in Section MB.1

of this report.

The violations identified in the above Notice of Violation

will be tracked as:

EA 97-055 VIO 01013: Inadequate goals and monitoring for the emergency

switchgear heating ventilation and air conditioning system (Closed

Section MB. 3).

EA 97-055 VIO 01023: Failure to demonstrate performance of SSCs had been

adequately controlled through the performance of appropriate preventive

maintenance (Open Section MB.4).

EA 97-055 VIO 01033: Inadequate instructions concerning cause

determinations for maintenance preventable functional failures (Closed

Section MS.5).

EA 97-055 VIO 01043: Failure to follow procedure concerning performance

criteria for the reactor protection system (Closed Section MB.6).

EA 97-055 VIO 01053: Failure to follow procedure concerning approval of

a risk-significant plant configuration (Closed MS.7).

16

PARTIAL LIST OF PERSONS CONTACTED

M. Adams. Superintendent. Engineering

R. Allen. Superintendent. Maintenance

R. Blount. Assistant Station Manager. Nuclear Safety & Licensing

D. Christian. Station Manager

M. Crist. Superintendent. Operations

  • E. Collins. Director. Nuclear Oversight

B. Shriver. Assistant Station Manager. Operations & Maintenance

T. Sowers. Superintendent. Training

B. Stanley. Supervisor. Licensing

W. Thorton. Superintendent. Radiological Protection

IP 37551:

IP 40500:

IP 61726:

IP 62706:

IP 62707:

IP 71707:

IP 71714:

IP 71750:

IP 92902:

Opened

.INSPECTION PROCEDURES USED

Onsite Engineering.

Effectiveness of Licensee Controls in Identifying. Resolving. and

Preventing Problems

Surveillance Observation

Maintenance Rule

Maintenance Observation

Plant Operations

Cold Weather Preparations

Plant Support Activities

Followup - Maintenance

ITEMS OPENED, CLOSED, AND DISCUSSED

50-280. 281/98001-01

50-280, 281/98001-02

EA 97-055. 01013

IFI

Review EOG fuel oil requirements (Section 01. 4).

VIO

EOG aux oil pump failure (Section Ml.l).

VIO

Inadequate goals and monitoring for the

EA 97-055. 01023

EA 97-055. 01033

EA 97-055. 01043

emergency switchgear heating ventilation and air

conditioning system (Section X2).

VIO

Failure to demonstrate performance of SSCs had

been adequately controlled through the

performance of appropriate preventive

maintenance (Section X2).

VIO

Inadequate instructions concerning cause

determinations for maintenance preventable

functional failures (Section X2).

VIO

Failure to follow procedure concerning

performance criteria for the reactor protection

system (Section X2).

EA 97-055, 01053

Closed

50-280, 281/97001-02

50-280, 281/97001-03

50-280. 281/97001-04

50-280. 281/97001-05

50-280, 281/97001-06

50-280, 281/97001-07

50-280, 281/97001-08

50-286. 281/97001-09

EA 97-055. 01013

EA 97-055. 01033

EA 97-055. 01043

17

VIO

Failure to follow procedure concerning approval

of a risk-significant plant configuration

(Section X2).

IFI

Followup on licensee actions to provide

performance criteria for structures after

industry resolution of this issue (Section

M8.2).

EEI

Failure to establish adequate performance

criteria for monitoring systems resulting in

inadequate implementation of the maintenance

rule (Section X2).

EEI

Inadequate procedural requirements resulting in

inadequate implementation of the maintenance

rule (Section X2).

EEI

Failure to accomplish adequate historical

reviews resulting in inadequate implementation

of the maintenance rule (Section X2).

EEI

Goals and monitoring not established for ESW and

ESG HVAC systems resulting in inadequate

implementation of the maintenance rule

(Section X2).

EEI

Performance criteria changed without approval of

the WG (Section X2).

EEI

Management approval not obtained for high risk

plant configuratibn (Section X2).

EEI

Inadequate corrective action for self-assessment

deficiencies (Section M8.1).

VIO

Inadequate goals and monitoring for the

emergency switchgear heating ventilation and air

conditioning system (Section M8.3).

VIO

Inadequate instructions concerning cause

determinations for maintenance preventable

functional failures (Section M8.5).

VIO

Failure to follow procedure concerning

performance criteria for the reactor protection

system (Section M8.6).

EA 97-055. 01053

Discussed

EA 97-055. 01023

50-280, 281/97001-01

18

VIO

Failure to follow procedure concerning approval

of a risk-significant plant configuration

(Section M8.7).

VIO

Failure to demonstrate performance of SSCs had

been adequately controlled through the

performance of appropriate preventive

maintenance (Section M8.4).

IFI

Followup licensee actions to strengthen risk-

assessment for on-line maintenance activities

(Section M8.7).