ML18152A016

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Augmented Insp Team Repts 50-280/88-34 & 50-281/88-34 on 880901-03.Insp Findings Noted
ML18152A016
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/30/1988
From: Julian C, Shymlock M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A017 List:
References
50-280-88-34, 50-281-88-34, IEB-84-03, IEB-84-3, IEIN-84-93, NUDOCS 8810130050
Download: ML18152A016 (43)


See also: IR 05000280/1988034

Text

.

UNITED STATES

NU_CLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/88-34 and 50-281/88-34

Li~ensee:

Virginia Electric and Power Company

Richmond, Virginia 23261

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License No$.:

DPR-32 and DPR-37

Inspection Con

T earn Leader:

Team Members:

Approve~ by:

1-3, 1988

-ntrcJU

T. Collins, Radiation Specialist, Region II

M. DeGraff, Reactor Engineer, Region II

W. Holland, Senior Resident Inspector, Surry

W. LeFave, Senior Reactor Engineer, Plant

Systems Branch, NRR

L. Lawyer, Reactor Engineer, Reg*; on II

J. Mathis, Resident Inspector, Grand Gulf

C- 6-

~'Yl

t. A. Julian, Chie~

Operations Branch

Division-~f Reactor Safety

8810130050 880930

PDR

ADOCK 05000280

G

PNU.

c:/3 o / <1s

'Date Signed

'

t - (

TABLE OF CONTENTS

Page

I.

INTRODUCTION - FORMATION AND INITIATION OF AUGMENTED

INSPECTION TEAM (AIT) * . . * . . . . . * * * * . . * . . . . . . . . . * . . . . * . * . * . . . . * .

1

A.

Background . . . * . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . * . . . . . . . . . . . .

1

B.

Formation of AIT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

C.

AIT Charter - Initiation of Inspection...................

1

D.

Persons Contacted........................................

3

E.

Description of Operations Shift Staffing at the Time

of the Event ........................... * . . . . . . . . . . . . . . . . . .

3

F.

Design Description ****...***.**.*.*.......*******..*.***.

4

II.

DESCRIPTION OF EVENT..........................................

4

A.

Overview of Event fpr Surry Unit 1 ...*......*.**....*....

4

1.

Initial Conditions . ..... ... ......... .. .. .... .. . .. ...

4

2.

Event De~cription ..*.......***.......*....*....**...

4

3.

Licensee Actions Following the Event................

5

B.

Deta i 1 ed Sequence of Events- * . * * . . . . . . . . . . . . * * * . . . . . . . . . . .

5

III.

SUBSEQUENT LICENSEE ACTIONS ...**......................... ~~...

9

A.

Refill of the Reactor Cavity From the Spent Fuel Pool ...*

9

B.

  • Deviation and Human Performance Evaluation System

Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

10

C.

Incore Instrument Room Cleanup *.*.......... i ************* 12

D.

Lack of Engineering Review and Subsequent Fuel Reload .**. 12

E.

IOER Evaluation of the Event .................*.*......*.. 12

F.

IOER Evaluation Presented to Station Management and NRC .. 15

G.

Justification for Continued Operation .........**...*.*... 16

IV.

EQUIPMENT STATUS, FAILURES/MALFUNCTIONS, AND ANOMALIES ........ 17

A

IEB 84-03 Lic~nsee Response and Modification ........**. ~.

17

B.

Significan~e of Seal Failure ............... ~ ............. 20

i

C.

Maintenance Activities

20

1.

Local Leak Rate Testing ...............*.........*... 20

2.

Maintenance History . . . . . . . . . . . . . . * . . . . . . . . . . . . . . . . . .

21

D.

Refueling Cavity_ Floor Seal_ ...........*....*............. 22

1.

Refueling Cavi~y Floor Seal Design Application ...... 22

2.

Equipment Vendor Involvement .....*.................. 23

V.

RADIOLOGICAL CONSEQUENCES .................................*. ~.

24

VI.

FINDINGS OF THE AIT . . . . . . * . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

25

A.

Radiological Consequences .......................... :. . . . .

25

B.

Failure Investigation ............*........................ 26

C.

Modifications .**...*.....................*............... 26

D.

Installation and Test of Refueling Cavity Floor Seal .. ~ ..

26

E.

Local Leak Rate Test ..................................... 26

F.

Inadequate Instructions and Drawings . . . . . . . . . . . . . . . . . . . . .

27

G.

Training . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

27

"VII.

GENERIC IMPLICATION OF SEAL FAILURE***************************

28

VIII.

ROOT CAUSE DETERMINATION ...................................... 28

IX.

CONCLUSIONS ..****..***..*..* ; * . * * . . * * . . . . * . * * * * . . . * . * . . * * . * . . *

28

X.

EXIT INTERVIEW . .............................................. . 29

ii

APPENDICES

APPENDIX 1

PERSONS CONTACTED

APPENDIX 2 -

ACRONYMS AND ABBREVIATIONS

APPENDIX 3 -

DESIGN DESCRIPTIONS

A.

Refueling cavity floor seal

B.

Instrument air system

C.

Nitrogen back-up system

D.

Upper core internals storage

iii

..

' ** t

REPORT DETAILS

  • I.

INTRODUCTION -

FORMATION AND INITIATION OF AUGMENTED INSPECTION TEAM

(AIT)

A.

Background

Surry Units 1 and 2 are Westinghouse (W) pressurized water reac*tors

(PWR) with Stone & Webster designed sub-atmospheric containments.

The units are located five miles south of Williamsburg, Virginia,

on the James River in Surry County~ Virginia.

Unit 1 went critical

in July, 1972 and was declared commercial in December, 1972.

On Tuesday, August 30, 1988, the resident inspectors became aware

of a report by the Independent Offsite Evaluation Review (IOER)

group relating to an event involving borated water leakage through

  • the Unit 1 refueling cavity floor seal.

This event occurred on

May 17, 1988, during the Unit 1 refueling and maintenance outage.

This information was provided to regional management after prelim-

inary assessment by the residents.*

B.

Formation of AIT

  • On the morning of Wednesday, August 31, 1988, the acting Regional
  • Administrator, after further briefing by the regional and resident

staff and consultation with senior NRC management, directed the

dispatch of an AIT headed by the Section Chief of the Regfon II

Operational Programs Section.

The team included participation by

the Office of Nuclear Reactor Regulation *

. C.

AIT Charter - Initiation of Inspection

The Charter for the AIT was prepared on August 31, 1988, and

the AIT members arrived at the Surry site on September 1, 1988.

Security badging was completed for the team, and the special

inspection commenced with an entrance meeting and briefing by

licensee management at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on September 1, 1988.

The

Charter for the AIT speci!ied the following:

1.

Develop and validate the sequence ~f events associated with

approximately 15,000 gallons of borated water leakage from

the Unit 1 refueling cavity through the refueling -cavity

floor seal which occurred during the approximate time frame

of May 17, 1988, while Surry Unit 1 was in a refueling outage.

Our specific concerns which require evaluation include:

(1) the potential degradation of safety-related instrumen-

tation and equipment resultant from exposur~ to corrosive

borated water, (2) adequac~ of operator response during the

\\ .

l

-.

2

incident; (3) adequacy of the positive "J" seal design to

.prevent leakage of this type on Surry Unit 1 or Unit 2 and

potential generic implications, (4) extent and significance

of personnel radiation exposures during event, (5) adequacy of

low head safety injection to replace the leakage, (6) extent

of failure and safety significance of the failure of the

instrument air, backup nitrogen supply, and related seals and

equipment sufficient to support conclusions regarding the

safety of continued pl ant operations, (7) adequacy of manage-

ment evaluation of the event both with respect to s~ope and

timeliness, and (8) licensee reporting of the event.

Key

items the AIT should emphasize _incJude all equipment malfunc-

tions, major plant evolutions/status changes, operator errors,

licensee management/support organization response, and reports

made to the NRC.

2.

Evaluate the significance of the event with regard to

radi ol ogi cal consequences, safety system performance, and

plant proximity to-safety limits as defined in the Technical*

Specifications.

3.

Evaluate the accuracy, timeliness, and effectiveness with

which information on this event was reported to the NRC.

4.

For each seal or related equipment malfunction, to the extent

practical, determine:

a.

Root cause.

b.

If the equipment was known to be deficient prior to tne

event.

c.

If equipment history would indicate that the equipment

had been historically unreliable or if maintenance or

modifications had been recently performed.

d.

Any equipment vendor involvement prior to or after the

event.

e.

Pre-event status of surveillance, testing, (e.g., Section

XI), and/or preventative maintenance.

-

.

f.

The extent to which the equipment was covered by existing

corre*ctive action programs and the implication of the

failure with respect to program effectiveness.

5.

Evaluate the licensee's actions taken to verify equipment

operability.

6.

Identify any human factors/procedural deficiencies related to

this event.


----- ---~~~

\\ '

!

i

I

-

3

7.

Through operator and technician interviews, determine if any

of the following played a significant role in the event;* plant

material condition; the quality of maintenance; or the respon-

siveness of engineering to identified problems.

Unless these

concerns involve immediate safety issues, team actions. should

be limited to communicating the concerns to NRC management.

D. -

Persons Contacted

Those persons contacted by the AIT are identi-fied in Appendix 1.

E.

Description of principal Operations Shift Staffing at the Time of

  • the Event

Abbrevi ati ans for the pri nci pal Operations Staff are used for

convenience throughout the report. The following brief explanation

of each posjtion is provided:

SS

Shift Supervisor - A Senior Reactor Operator (SRO) responsible

for both Vnit 1 and Unit 2 operations.

While on shift he/she

is also the unit supervi-sor for one of the two units.

USS

Unit Shtft Supervisor - The junior of the two SROs on the

shift and responsible for the other unit.

STA Shift Technical Advisor - He/she is assigned to the shift to

advise the SS on matters pertaining to the engineering aspects

of assuring safe operations of the plant.

-

-

CRO

Control Room Operator - A licensed reactor operator respon-

sible for the operation of his/her assigned unit.

RS

Refueling Supervisor - An SRO responsible for all fuel move-

ment activities.

CS

Containment Supervisor - An SRO responsible for overall opera-

tions activities in containment other than fuel movement.

UTS -Unit Test Supervisor - An SRO responsible for Type C testing

of containment- penetrations and repair of their associated

components.

Severa 1 non-1 i censed operators work under the

direction of this individual in fulfilling his responsibili-

ties.

-

NLO

Non-Licensed Operator - A non-licensed operati~ns department

i_ndividual trained in the location, operation, and safety

significance of plant equipment in his work area.

Reports to

  • one of ;he CROs or supervisors des~ribed above.

These and other acronyms and abbreviations used in this report are

iaentified in Appendix 2.

' ' ,.

4

F.

Design Description

Design descriptions for the major equipment and systems discussed

in the report are provided in Appendix 3.

II. Description_ of Event

A.

Overview of Event for Surry Unit 1

1.

Initial Conditions

2.

On the morning of May 17,- 1988, Surry, Unit 1 was in the

mi9dle of a refueling and maintenance outage.

The reactor

- vessel was defueled (all fuel had been transferred to the

spent fue*l pool).

No fuel movement was in progress.

The

reactor cavity was flooded to approximately 27 feet and

the spent .fuel pool was isolated.

Contract personnel, W

were performing work from the refueling bridge on the upper

internals package thermocouple conduits.

An operations

department group was performing Local Leak Rate Tests (LLRT)

and maintenance on various containment penetrations.

Unit 2 had experienced an automatic reactor trip .from mo

  • percent power with a nianua l sa.fety injection early on the

morning of May 16, 1988.

Following the trip, the unit

experienced problems associated with auxiliary feedwater (AFW)

flow to the

11A

11 steam generator.

Evaluation and trouble-

shooting of the AFW flow problems were still receiving manage-

ment and operations staff attention on .May 17, 1988.

Event Description

On May 17, 1988, while preparing to repair instrument air

(IA) valve, l-IA-849, an NLO requested between 0800 and 0830

hours, via the control room, that IA to Unit 1 containment be

isolated (this was necessary to facilitate repair of the

valve).

Upon entering the

11C

11 loop room (located in contain-

ment) he observed water cascading down the wa 11 s through

the reactor loop piping penetrations.

His first response was

to inform the control room and have IA re-established to the

containment and his second was to determine if the nitrogen

bottles were supplying pressure to the refueling cavity floor

seal. He noted that one of the nitrogen bottles was empty and

the pressure regulator on the other bottle was misadjusted.

This prevented it from being able to pressurize the seal.

He

then adjusted the regulator to supply pressure to the seal and -

noted that the leak-decreased.

' '

5

This serie~ of events resulted in nearly 30,000 gallons (which

equates to approximately three feet of water in the refueling

cavity) of water being drained through the deflated refueling

cavity floor seal.

The reduction in cavity level resul°ted in

increased radiation level on the Unit 1 operating deck.

Work

on the upper i nterna 1 s package h*ad been suspended by the

health physics (HP) technician due to increased radiation

levels.

3.

Licensee Actions FQllowing the Event

The NLO, noting the water leak in the

11C

11 loop room informed

the control room.

The CRO and SS were informed of the

problem.

The CRO noted that the incore sump high level alarm

had alarmed.

Attempts to start the incore instrument room

sump pump failed.

An NLO was sent to check out the incore

instrument room sump pump breaker at the motor control center.

It was noted that the breaker had tripped on thermal overload

and it would not reset.

This may have indicated that the

motor was submerged.

Sometime between 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> and 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> the Operations

Coordinator entered the control room.

The SS informed him

that there had been

11 a foot or so drop

11 in cavity water levei,

and that HP had suspended* work on the operating deck due

to increased radiation levels.

The Operations Coordfoator

immediately went to inform the Assistant Station Manager.

Sometime later on May 17, 1988, the Superintendent of Opera-

tions and the Operations Coordinator insp~cted the

11C

11 loop

room.

No problems were identified.

The Station Manager was

also informed of ~he event that day.

The team was unable to determine whether any additional evalu-

ations or other actions pertinent to the event were taken

by the 1 i c*ensee unti 1 two days 1 ater when an STA prepared

deviation report Sl-88-422.

B.

Detailed Sequence of Events

SURRY UNIT 1 - REACTOR CAVITY SEAL FAILURE

MAY 15, 1988

Time

(EST

Hours)

0554

Data Source

CRO. Log-

Item

Periodic Test; PT-10 Reactor

Coolant Leakage walkdown. com-

pleted satisfactory. Containment

- sump in-leakage calculated to be

..

Time

(EST

Hours)

Data Source

MAY 16, 1988

0200

0223

1433

1504

1610

SS Log

CRO Log

SS Log

CRO Log

SS Log

CRO Log

Type C Test Log

6

Item

8.2 gpm.

Nitrogen bottle pres-

sures ( to the refueling cavity

floor seal) found to be 1800 psig

and 2200 psig.

Verified Instrument Air supply to

Unit 1 Containment instrument

air header being supplied through

valves 1-IA-446, and 447.

PT-10 Reactor Coolant Leakage

walkdown completed satisfactory.

Containment

sump

in-leakage

calculated to be 9.9 gpm.

Instrument air to Unit 1 contain-

ment isqlated to investigate a

problem associated with instru-

ment air valve, 1-IA-849.

The

nitrogen bottles were verified as

being aligned to the refue 1 i ng

cavity floor seal.

Instrument air re-established to

Unit 1 containment.

Instrument air was valved out

to Unit 1 containment (verified

that the refueling cavity floor

seal was being supplied by the

nitrogen

bottles).

Attempted

to seat valve 1-IA-849, the valve

still leaks.

Instrument air

returned to service.

The

NLO performing the valve

manipulations indicated that upon

exiting containment he requested

that his relief perform

11 indepen-

dent verification". associated

with instrument air and nitrogen

back-up supply valve line~ups.

r

' .

Time

(EST

Hours)

Data Source

MAY 17, 1988

0223

SS Log

0230

Chart recorder

0830

CRO Log

  • CRO Interview
  • USS Interview

7

Item

This

NLO indicated that the

verification requested from the

previous shift was completed

between 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> and 0200

hours.

The verification con-

sisted of insuring nitrogen and

instrument air supply valve line-

ups were correct as we 11 as *

verifying that, if required, the

nitrogen bottles would in fact

supply the seal.

PT-10 Reactor Coolant Leakage

walkdown completed satisfactory.

Containment

sump

in-leakage

calculated to be 13.4 gpm. The

nitrogen bottle pressures to the

refueling cavity floor seal were

verified to be 1500 psig and 1800

psig.

The ~hart recorder in the control

room which plots -input from

RMS-162,

manipulator

crane

radiation monitor, indicated the

measured radiation _levels to be

approximately 5mr/hr.

Isolated instrument air to con-

tainment for PT-16.4, Containment

Isolation Valve Leakage.

The operator recalled that during

the event, the incore room sump

high level alarm did annunciate.

The setpoint for this alann is

18 inches.

He recalled the incore instrument

rqom sump high level alarm being

i 11 umi nated.

Additfona lly, he

noted *attempts to start the

incore room sump pump failed.

' .

Time

(EST

Hours)

0852

0855

0857

0911

0921

Data Source

CRO Log

  • Chart Recorder

SS Log

SS Log

8

HP Supervisor Log

SS Log

Item

Valved instrument air back into

containment after noting contain-

ment sump level increasing and

discovered that one back-up

nitrogen bottle to the refueling

cavity floor seal was empty and

th*e other was at 1500 psi g but

did not appear to be* supplying

the refueling cavity floor seal.

The chart recorder in the control

room which plots input from

RMS~162, manipulator crane radia-

tion monitor,

indicated the

measured radiation levels increas-

ing to approximately 35mr/hr.

This increase occurred between

0830 and 0900.

Received a report of re*fue 1 i ng

cavity floor seal inflatable

seal leakage. Instrument air to

containment had been isolated to

support operations work.

Instrument air restored to

containment.

Water level in the reactor cavity

has dropped.

General area around

the cavity was up to lOOmr/hr.

Work on RWP No. 88-RWP-1507 was

stopped until water- level is

raised by operations.

NLO reports that one nitrogen

bottle to the refueling cavity

floor seal ring was completely

depressurized.

The second bottle

gage indicated 1500 psig, however

the regulator was mi sadjusted.

-The sea 1 was repressuri zed and

preparations are *in progress to

res tore 1 eve*1 in the ref ue 1 i ng

cavity using primary grade (PG)

water.

..

Time

(EST

Hours)

0958

1005

1105 *

1105

Data Source

SS Log

CRO Log

SS Log

Chart Recorder

SS Log

9

HP Supervisor Log

Item

Received a report from HP that

water is leaking around concrete

  • access plug_to the incore instru-

ment sump room 1 oca ted in the

containment basement.

Leak rate

is estimated at four gpm.

Con-

tainment sump pump is keeping up

  • with the leakage.

Incore sump

pump motor control breaker ther-

mal overlo.ads tripped.

Possible

cause, pump motor submerged.

The fuel transfer tube isolation

valve open approximately five

turns to raise refueling cavity

level.

Chart recorder for RMS-162, manip-

ulator crane radiation monitor,

recorded radiation levels begin

a decreasing trend.

Startin'g

at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> at approximately

35mr/hr and ending at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />

with approximately lOmr/hr.

( It

- should be noted that this decreas-

ing trend coincides with the

refi 11 of the refueling . cavity

from the spent fuel pool1

Secured filling the refueling

cavity through the fuel transfer

tube. Spent fuel pool was lowered

approximately eight inches.

Water 1 evel in the cavity has

returned to normal.

  • Indicates event is entered at the approximate time frame.

III.

SUBSEQUENT LICENSEE ACTIONS

A.

Refill of the ~eactor Cavity From the Spent Fuel ~ool

Following the event the licensee, in order to recover level in the

refueling cavity, opened the fuel transfer tube isolation valve

five turns.

This occu~red approximately two hours after the event

and the valve remained opened for approximately one hour.

This

resulted in an eight-inch drop in spent fuel pool water level.

The following day, May 18, the valve was opened again. This time,

the level in the spent fuel pool was reduced five inches. The AIT

was provided information which indicated that a one-inch decrease

in spent fuel pool water level was equal to approximately 1440

gallons.

U_sing the above information, the inspectors determined

that approximately 18,700 gallons of water was transferred from the

spent fuel pool to the refueling cavity to partially make up for

the water lost during the seal leak.

The AIT questioned the licensee*s* level recovery method and

requested a copy of the procedure which was used.

The licensee

indicated that there was no operating procedure which addressed

this evolution.-

During the time period between the two cavity

fills, the spent fuel pool was refilled with PG water.

After,

refilling, the spent fuel pool was sampled to verify boron

concentration to be greater than 2000 ppm.

The AIT expressed

concern that the above method of refilling the cavity was performed

without assurance that the seal could meet its intended design

function and without procedures.

The AIT also noted that additional water was added to the refueling

cavity from the refueling water storage tank just prior to refuel-

ing the vessel in order to establish proper refueling level.

B.

Deviation and Human Performance Evaluation System Reports

Two days after the event, May 19, 1988, an STA *prepared* Deviation

Report (DR) Sl-88-422.

Within the report possible causes leading

to the event were identified.

They ~ere human error, procedure/

drawing error and/or design.

The Corrective Action section of

the report dated June 13, 1988, indicated

11 no corrective action,

management informed - Surry Human Performance Evaluation System

(HPES) report 88-012, unresolved for human error.

Implementation

of design change similar to Unit 2, Engineering Work Request (EWR)85-200.

11

This DR was subsequent~y reviewed by the Site Nuclear

Safety Operation Committee (SNSOC) on July 7, 1988.

HPES report 88-012 was forwarded to the SNSOC cha*; rman* on June 13,

1988.

As in the case of the DR, the HPES report concerned itself

primarily with human error surrounding the event.

The conclusion

reached in this report was that during the time frame of 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />

to 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on May 17, 1988,

11an*unauthorized, non-recorded valve

isolation occurred on the norinal air supply to the cavity seal

ring r.esulting in partial loss of cavity level .

11

In addition, the

statement was made that

11the potential hazards that can be created

due to this activity cannot be understated.

11

Finally, the report

stated that

11 unfortunately no specific corrective actions can be

generated from this office

11 *

11

The cover letter indicated that "HPES evaluation could not deter-

mine specifi"c causal human factors that would have contributed

to the event and that the report was being submitted to SNSOC for

information and to assure that appropriate management personnel

were aware of the results."

The AIT reviewed the DR and HPES reports.

The DR dtsposition was

considered superficial in that it failed to recognize other

important factors such as:

possible design deficiencies in the seal;

the fa i1 ure of the "J" seal and operability concerns regarding

refueling activities;

the failure of the back-up nitrogen system to supply the

seal;

inadequate procedures to operate the air and-nitrogen systems;

inadequate drawings to indicate system configuration; and

the generic implications associated with the same seal

  • arrangement used on Unit 2.

The HPES report was considered to be inconclusive in that the only

"Human Performance" indicator identified was a "non-authorized,

non-recorded valve manipulation."

The AIT considers other "Human

Performance" indicators pertinent to the event which were not

discussed to be:

-

.0

no identification tags on IA or nitrogen system valves;

0

no drawings depicting IA or nitrogen system configuration.

The AIT also noted that repairs to valve 1-IA-849 were conducted

without procedural guidance.

On August 16, 1988 following the Independent Offsi te Evaluation

Review (IOER) group investigation of the event, a second DR,

Sl-88-0873, was written.

The deviation description identified that

the "J" seal portion of the refueling c;avity.floor seal would not

preclude leakage from t~e refueling cavity as stated in the Updated

Final Analysis Report (UFSAR) 9.12-3 and *in Surry's response to !EB

84-03, dated October 9, 1984.

The DR indicated that "the "J" seal

design is inadequate and would allow leakage greater than the

. available make-up source from on_e low head safety injection (LHSI)

pump* if the inflatable seal failed."

This second DR appeared to be

more complete in its identification and analysis of the deviation.

r

12

C.

Incore Instrument Room Cleanup

The failure of the refueling cavity floor seal resulted in borated

water being deposited in various locations in containment but

primarily in the incore instrument room located below the reactor

vessel.

The water that accumulated*was calculated to have achieved

a level of approximately five to six feet above the floor.

The borated water remained in the room for approximately 30 days.

The incore detector guide thimbles were retracted from the vessel

and- radiological conditions precluded entry.

Once refueling was

completed with the guide thimbles reinserted, radiation levels

were low enough to allow access.

The room was pumped out and the area washed down with purified

water.

There were no special tests performed or wall smears taken

to determine actual water levels.

Following the clean-up effort,

the room was inspected and the results determined to be satisfac-

tory.

The room was sealed and preparations were made to return to

power.

D.

Lack of Engineering Review and Subsequent Fuel Reload

Following the event, even though DR SI-88-422 indicated a probable

cause of the deficiency to be design related, no eng*ineering

evaluation of the *seal design or failure modes were performed.

This oversight was apparently caused by the station

I s be 1 i ef

that the leak was small and over a long period of time, and that

the event stemmed from human error.

As a result, the licensee

did not question the design or its ability to perform its intended

function.

Therefore, no corrective actions or compensatory

measures were implemented by the licensee prior to refueling the

reactor vessel.

The AIT and the licensee determined that the ability to make up for

a refueling cavity floor seal leak exceeded the capacity of one

LHSI pump.

Jt is uncertain how much of the "J" seal was actually

displaced, thus the anticipated leak rate could-be much higher.

The most significant concern is that refueling operations were

conducted (all the fuel was reloaded) without confirming that the

seal would perform its intended design function.

E.

IOER Evaluation of the Event

The IOER group received HPES report 88-012 on July 14, 1988.

Their

subsequent review deemed the report to be inconclusive and due to

the concerns raised, an investigation into the event was initiated.

13

On August 17, 1988; the IOER group forwarded to plant management

their findings regarding their investigation of the refueling

cavity floor seal failure at Surry Unit 1.

This investigation

report included a summary of events surrounding the failure of the

seal, the implications of the event, and finally, identification

of concerns and proposed actions in the areas of administrative

controls, technical issues, and ~perations response.

The report identified the most important*question as being "wh~ the

passive

11J

11 seal did not prevent catastrophic leakage and would the

resulting leakage exceed the capacity of the make-up capability

provided?"

Addi ti ona lly, it was stated that "this con*cern focuses

on the potential for uncovering a suspended fuel assembly and the

time necessary to relocate an assembly into a safe position." It

should qe noted*that both the licensee's UFSAR and response to IEB

84-03 state that the passive "J" seal will prevent this from

occurring.

In line with their investigation, the IOER group initiated a

detailed design review of the

11 J

11 seal.

They concluded that "the

lack of a positive backing plate on the seal can allow the upward

displacement of the bulbous portion of the seal due to forces

exerted underneath it. These forces result from the flow of water

past the seal due t"o s_urfa-ce imperfections or seal deterioration."

Additionally, it was stated that "the calculated buoyancy of the

seal in borated water with an air hole in the center is very near

the buoyancy point."

The report went on to further discuss the refueling cavity floor

seal installation procedure, MMP-C-RC-37.

MMP-C-RC-37 requires the

stand-off supports be set at 1 3/16 inches. Calculations performed

by the licensee show that for a 30% compression (which results from

the stand-offs being set at 1 3/ 16 inches) there wi 11 be about

3/8-inch of surface contact between the "J" seal and mating

surface.

Due to the lack of a backing plate, there is nothing

to guartl against a reduction in this surface contact.

In addi-

tion, it was stated that "if the seal were not r~gularly replaced,

res i 1 i ency is lost and the abi 1 ity of the sea 1 to accommodate

surface imperfections is lost."

As previously stated, the final portion of the investigation report_

i dent i fi ed several_ conce.rns and proposed actions in the areas of

administrative controls, technical issues and operations response.

-

.

In the area of administrative controls the following concerns were

identified:

"A station deviation report was not immediately submitted to

initiate a review of the event and to ascertain reportability.

11

"HPES report 88-012 was submitted without fully assess.i ng the

event or the ramifications of the event."

., .

14

-

11The UFSAR states that the "J" sea 1 wi 11 prevent 1 eakage in

the event of a failure of the inflatable seal.

This design

basis was reiterated in response to IEB Significant Operating

Experience Report, 84-03, 85-01 and internally to IEIN 84-93."

To resolve these concerns the proposed actions included:

"Submit a station deviation report to document evaluations and

determine reportabi 1 ity."

"Sta ti on personne 1 should be reminded of the requirements

for submitting deviation reports.

11

"HPES evaluators should be reinstructed on the necessity of

performing detailed evaluations, submitting deviation reports

for operational events beyond human factors and the need to

have a thorough review of reports prior to issuance.

11

In the area of technical issues the following concerns were noted:

"The potential flowrate past _the "J" seal in its current

design, may exceed the capacity of a single LHSI pump."

"Based on leakage experienced and discussion with the vendor

it appears the design of the**seal ring-is not an acceptable

app 1 i cation."

"Evaluate the residue of boric acid that accumulated on the

reactor vessel walls which was* not removed."

"The vendor recommends the inflatable seal should have

increased strength provided by fiber reinforcement.

In

addition, the sealing surface contact surface area should be

increased."

To resolve th~se concerns the proposed actions included:

"Determine the maximum fl owrate that can occur and compare

thi_s to _the make-up capability of a LHSI pump."

'!Investigate possible seal ring design improvements that can

be implemented."

"Evaluate the impact of boric acid residue on the carbon steel**

reactor vessel exterior walls."

"Review the design of the nitrogen *-back-up system and imple-

ment improvements as required."

"Review vendor recommendations for need."

In the area of operations the following concerns were noted:

11 How did IA to the inflatable seal become isolated.

It was

indicated that the local IA supply valve was found c*losed,

however logs indicate the problem occurred when IA was valved

out to support Type C LLRT on penetration 47.

11

110perators did not enter the appropriate procedure for a loss

of refueling cavity level.

11

11The fue 1 transfer gate va 1 ve was opened to restore l eve 1

in the refueling cavity.

G*iven the potential for further

leakage and a potential failure of the gate valve to close,

spent fuel pool level could have been significantly reduced.

This action was not based on procedural guidance, is an

unadvisable method and contradicts the requirements of

Technical Specification (TS) 5.4.D.

11

"AP-22

11Fuel Handling Abnormal Conditions

11 and AP-27

11Loss of

Decay Heat Removal Capability

11 provide inadequate guidance to

operations personnel on a rapid loss of refueling cavity water

level."

To resolve these concerns the foilowing action was identified:

"A review of current procedure controls for a loss of refueling

cavity level should be performed.

11

F.

IOER Evaluation Presented to Station Management and NRC

After identification of the above concerns by the IOER group, the

engineer who prepared the IOER report submitted a station DR in

accordance with procedure. That DR, Sl-88-0873, which is discussed

in section III B of this report, identified a design problem

associated with the "J

11 seal portion of the refueling cavity floor

sea 1.

After receiving the DR, the station safety committee

requested and received a presentation on the IOER concerns which

resulted in the DR.

This presentation was made at the Surry Power

Station on Thursday, August 25, 1988.

On that day, one of the NRC

residents walked into the meeting near the end of the presentation,

but was not aware of the problem at that point~

The safety committee concluded that some of the information pre-

- sented was incorrect and requested the IOER engineer to provide

additiona 1 information to justify some of the IOER concerns.

On

Friday, August 26, 1988, the Assistant Station Manager for Licens-

ing and Safety provided information on the IDER presentation to the

NRC residents; however, a copy of the IOER report was not provided .

~

I

.* . . .

16

-

This Manager indicated that design deficiencies identified in the

report were under review and would be addressed the following

week.

The resident inspectors became aware of the IDER report on

August 30, 1988.

The Station Manager provided the residents a copy

of the report on August 31, 1988.

The licensee made a 10 CFR 50.72

report of the rapid decrease in refue1ing cavity water level on

September 1, 1988.

G.

Justification for Continued Operation

On September 2, 1988, the licensee provided a Justification for

Continued Operation (JCO) of Unit 1 as requested by the NRG.

This JCO relied on and transmitted the licensee's engineering

evaluation, Technical Report PE-0005 dated September 1, 1988,

of the potential effects of borated water flooding of the incore

instrument room as related to the then *present and continued safe

operation of the facility.

The licensee's engineering.evaluation assumes that initial leakage

past the "J" seal would have been collected by the drip pan.

This

leakage would have then been carried away via drain piping to the

containment sump.

However, as 1 eak fl ow increased beyond the

capacity of the drip pan, the flow path would .have been primarily

down the exterior of -the reflective insulation~ over the neutron.

  • shield tank a"nd into the incore instrument room.

In addition, the

licensee indicated a small amount of leakage could have flowed onto

the reactor vessel nozzle reflective insulation and flowed and/or

splashed along the reactor coolant piping into the loop rooms.

The licensee's analysis states that all equipment in the loop

rooms is qualified for chemical spray.

Therefore, the subject

leakage/flooding would in no way prevent any equipment in the loop

rooms from performing their design functions.

Within the incore instrument room, 11 critical components were

identified.

Of these, three are constructed of austenitic* stain-

less steel which is not adversely affected by wetting with borated

water;

These three are the reflective i nsul ati on, the reactor

coolant piping, and the incore instrumentation guide tubes.

One component received spray but was probably not submerged.

Its

exposed surface is a 347 stainless steel sheath and other non-

stainless steel components are hermetically sea~ed in thi~ sheath.

Four of the components were coated with design bases accident

qualified paint which is not adversely affected by boric acid.

These were the supply and return lines for the neutron shield tank

coolers, the containment mat liner plate, the neutron shield tank

and the incore instrumentation guide tuQe supports.

'

17

One component, the Gamma Metrics Excore Neutron Detector is

composed of a signal cable and jun*ctfon box.

The junction box is

unprotected carbon steel with SS cabling attached.

This junction

box is sealed with a silicon 0-ring.

(It is not clear whether

this junction box is above or below the six foot water level.)

Even if the junction box was submerged, it should have only

suffered a loss of some 0.001 inch of its 3/8 inch thickn~ss.

The

cabling consists of a solid copper coaxial conductor insulated

with Kapton tape encased in a flexible stainless steel hose and

covered by woven glass fiber.

The remaining two components were briefly wetted, protected by

geometry, and would have suffered less than 0.001 inch material

1 ass.

These two were the reactor vesse 1 (primarily the flange)

and the reactor vessel sliding supports.

These latter supports

were also protected by a lubricant.

.

.

The licensee concluded in its JCO that

11As a result of these

investigations (described above), the flooding of the incore

instrument room with borated water wi 11 * have no adverse effect on

continued safe operation of the plant.

11

The AIT concluded, following an evaluation of. the JCO that the

1 i censee had adequately addressed the potenti a.1 degradation of

safety-re 1 ated instrumentation and equipment from exposure of

corrosive borated water.

IV.

EQUIPMENT STATUS, FAILURES/MALFUNCTIONS, AND ANOMALIES

A.

!EB 84-03 Licensee Response and Modification

The licensee's response to !EB 84-03 dated October 9, 1984, indi-

cated an evaluation of the potential for and the consequences of a

refueling cavity floor seal failure had been performed.

Their r~sponse contained a brief design description detailing the

operation of both the inflatable seal, and the passive

11J

11 seal.

In addition, the licensee indicated that procedures require a

pressure drop test on the inflatable seal as well as a visual

inspection of the

11J

11 seal prior to installation.

Although not

stated, it appears this information was provided to assure the NRC

that even if seal degradation were occurring, it would be

discovered prior to seal use.

They indicated that at least one makeup path was available at all

times during refueling.

Therefore should the pres.surized seal

fail, any of the available makeup paths could be used to maintain

water level, while the passive

11J-seal

11 would preclude leakage.

..

18 -

-

They further explained that although a catastrophic failure is not

credible because of the design, should such a failure-occur, the

elevation of the spent fuel transfer system would prevent a fuel

assembly from being uncovered.

Additionally*, a barrier in the

spent fuel storage pool precludes the draining of the pool's water

to less than 13 inches above the fuel racks.

The licensee concluded that a complete failure of the refueling

cavity floor seal was not a credible event.

In addition, based

on their evaluation and seal design differences between the two

facilities (Surry and Haddam Neck) they believed the seal assembly

employed at Surry to be adequate.

Finally, as a result of the

IEB review, the licensee revised AP-22, Fuel Transfer Equipment

Malfunction, to provide opera-tor actions to be taken in the event

of a rapid decrease in refueling cavity water level.

The procedure delineated immediate operator actions which consisted

of the following:

0

0-

0

Providing makeup by several means,

Placing the fuel assembly in the safest position possible. If

a fuel assemble was jn the maniptJlator the p*rocedure required

returning it to the core, and

Instruction to. close the fuel transfer tube gate valve,

isolating_the-spent fuel pool from the refueling cavity~

.Additional procedural actions provided were:

0

.

0

0

Isolation of the leak or rupture,

Monitoring residual heat removal

(RHR) pumps for proper

operation and signs of cavitation, and

Rectification of the problem and resumption of norma} activi-

ties as directed by the SS.

In April of 1987 as part of an intended procedure upgrade program,

many of the corrective actions were deleted from Abnormal Procedure

AP-22.

The AIT determined that AP-22, which was available to

operators on May 17, 1988, was inadequate to deal with a decrease

in refueling cavity level.

It was also noted that there were no d1rections in the procedure

for inspection of the IA and/or back-up nitrogen supply systems

- either prior to or after the procedure upgrade .

19

The AIT concl~ded that the licensee was not in compliance with the

!EB 84-03 response.

A catastrophic failure was probable, operating

procedures were not adequate to address the event, and an LHSI pump

(3250 gpm) will not be able to maintain cavity water level.

The

AIT also identified an inadequacy in the licensee's administrative

control process that assures that commitments to the NRC are

maintained.

Sys tern Modification .

Subsequent to the issuance of !EB 84-03, the licens~e

performed a review of the facility's refueling cavity floor

seal.

After the review the licensee concluded that it would

be desirable to incorporate a back-up air supply for the

refueling cavity floor seal.

This would provide redundancy

and thus maintain the inflatable seal inflated in case of IA

failure.

On April 4, 1985, EWR 85-200 was approved to. support the

design and installation of a nitrogen back-up supply system

on Unit 2.

During this inspection the AIT determined that

a similar nitrogen back.:.up supply system was installed on

Unit 1.

It appears that the system was installed under a

temporary modification during the 1984 Unit 1 refueling

outage.

However, the licensee could not produce any documen-

tation which supported the finalized installation similar to

EWR-85-200 used on Unit 2.

Since the AIT, the 1 icensee has

provided information which indicates that the temporary

modification was closed out following the outage with no

followup action.

EWR 85-200 discussed several conclusions and recommendations.

A review of the available documentation indicates several

problems with the Unit 1 and Unit 2 nitrogen back-up supply

systems.

These problems are enumerated below:

EWR 85-200 recommended that check valves to prevent air

backflow and relief valves to prevent overpressurization

be installed.

Discussions with the licensee indicated

that these components are installed on Unit 2 but not on

Unit 1.

In either case (Unit 1 or Unit 2) it is diffi-

cult to ascertain specific system configuration due to

the lack of as-built drawings.

EWR 85-200 recommended that procedure MMP-C-RC-037,

Installation, Inflatfon and* Removal of Reactor Cavity

Inn~r Seal Ring, be revised to include steps for set.ting

and testing the pressure regulators, ana relief valve,

and steps to install and remove the nitrogen bottl e*s.

A

review of MMP-C-RC-37, used during the May 1988 Unit 1

refueling outage, indicates that none of these recom-

mendations had been implemented.

This procedure is

applicable to Units 1 and 2;

B.

20

EWR 85-200 recommended that the nitrogen bottles have

their pressure regulators set at 20 psig.

In addition,

it recommended that the existing IA pressure regulators

be reset to 25 psig versus 20 psig.

A review of

MMP-C-RC-037 used during the May 1988 Unit 1 refueling

outage indicated that the IA pressure regulator was still

set at 20 psig, per step 5.5.2.

Significance of Seal Failure

During this inspection it was determined that approximately three

feet of water was drained from the refueling cavity over a rela-

tively short period of time.

The AIT was provided information .that

the refueling cavity contained approximately 240,000 gallons of

water when filled to a depth of 26 feet.

The AIT calculated that a

three foot drop in cavity level would result in a loss of approxi-

mately 27,800 gallons of water.

The licensee stated in the AIT

exit on September 3, 1988, that the majority of water was drained

in approximately* four minutes.

Using four minutes as the time in

which the water was drained and 27,800 gallons as the quantity of

water drained, the AIT determined that the leakage through the

refueling cavity seal was approximately 6,950 gallons per minute.

The c!esign flow rate of one*LHSI pump as specified in the UFSAR

is approximately 3250 gallons per minute at a design discharge

pressure of 225 feet of water.

Therefore, one LHSI pump would not

. keep up with the calculated leakage identified above.

It was noted

from operator logs during the event that the LHSI pumps were not

available.

C.

Maintenance Activities

1.

Local Leak Rate Testing

The licensee, on May 16,1988, was conducting LLRT on contain-

ment penetration No. 47.

The testing was being conducted

in accordance with PT-16. 4,

11Conta inment I sol ati on Valve

Leakage," dated April 8, 1988.

Penetration 47 supplies IA

to a two-inch IA pipe header inside containment. This header

distrioutes air to various components including the inflatable

refueling cavity floor seal.

The purpose of the test being

conducted was to measure back leakage through check valve

1-IA-939.

See IA description in Appendix 38 and Figure 2.

~foblems aisociated with se~t leakage on 1-IA-849 prevented

the test from being completed.

1-IA-849 is one of two valves

required to be closed in order to isolate the penetration. -

To expedite repairs, a contractor was brought in but, due to

time constraints and a lack of spare parts, repair efforts

were schedu.led to_ continue -the following day, May 17, 1988.

  • 21

On May 17, 1988, at about 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, repair activities

commenced on 1-IA-849.

Operations, to support this effort,

had isolated IA to containment.

The NLO assigned to this work

entered the

11 C

11 loop room to verify the nitrogen bottles were

supplying the seal (see Figure 2) at which time he discovered

water cascading down the walls.

2.

Maintenance* History

Maintenance had been performed on both the

11J

11 seals and the

inflatable seal.

In May.of 1986, the

11 J" seals, associated

fasteners and retainers were rep laced under work request 333552.

This work was accomplished due to natural end of

life.

MMP-C-RC-37, Installation, Inflation, and Removal of the

Reactor Cavity Inner Seal Ring, dated April 12, 1988,

requires:

(1) a pressure drop test on the inflatable seal;

(2) a visual inspection of the seals; and (3) a visual

inspection of the

11 J

11 seal seating surface.

All of the.

aforementioned tasks are to be completed prior to seal

assembly installation.

The pressure drop test requires that. the i nfl atabl e seal be

inflated to 20 psig.

Following inflation, the air source is .

removed.

The acceptance criteria specifies that 20 psig be

maintained for 10 minutes.

The test performed during the 1988 Unit 1 refueling outage

failed to meet this acceptance criteria.

Once the seal was

inflated, and the air source removed; the pressure dropped to

16 psig in the first 5 to 6 minutes.

It then held at this

pressure for the remaining portion of the test~

The visual

inspection noted evidence of surface nicking and scraping.

Each of these deficiencies resulted in a Quality Control (QC)

rejection.

The licensee performed an evaluation of the noted deficiencies

under EWR 88-116.

The EWR indicated the calculated leak rate

for the seal to be six to eight scfh.

This was determined to

be well within the capacity of the .nitrogen bottles which are

designed for a 25 scfh leak rate over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

It al so

concluded that the deficiencies noted during the visual

inspection were assumed to be caused by seal handling during

decontamination efforts.

Finally, the EWR concluded that even in the event of a com-

plete failure, deflation- of the inflatable seal, the. back-up

passive "J

11 seal will prevent excessive leakage.

22

The visual inspection performed on the

11J

11 seal seating

surface a 1 so resulted in a QC rejection.

This was based on

evidence of suspected boric acid and oii residue, fixed rust

  • and loose metallic flakes.

In addition, a six-inch long

scratch was also identified.

The 1 icensee performed an eva 1 uation of these deffci enci es

under EWR 88-148.

While generating the EWR, it was expanded

to include pitting, denting, hammer blows, and discoloration

as well as a sharp edge apparently caused by metallic contact.

The resolution of the identified deficiencies included the

following:

0

0

0

0

The defects did not encompass the entire width of the

seating surface at any location around the circumference

of the flange.

The defects were found to be less than 1/32 of an inch

indepth with no sharp edges or burrs.

The hammer blows were observed to have characteristics

similar to the defects.

The hammer blows were also identified as being located

outside the actual seating surface and having no affect

on the sealing.

Given the known deficiencies discussed above, contribution to

the event from these items cannot be overlooked.

No inspec-

tion of the seal assembly. was performed following the 1988

refueling activities.

This was due to the licensee's belief

that the event stemmed from personnel errors, and the leak

being small over a long period of time.

The AIT concluded that the licensee's evaluation of the

capability of the nitrogen bottles to maintain a six scfh seal

leak rate was incomplete.

The evaluation never addressed the

nitrogen bottles as a "finite supply."

The operators had no

direction to monitor, record, and trend the quantity of

nitrogen remaining in the bottles and therefore, the likeli- *

hood of nitrogen pressure failure leading to seal failure was

much higher than concluded by the licensee.

D .. Refueling Cavity Floor Seal

1.

Refueling Cavity Floor Seal Design Appli-cation

The refueling cavity fl oar seal design at Su~ry is seismic

category 1 and safety related.

The seal is part of the

refueling cavity pressure boun*dary.

Refer to App*endix 3A and

Figure 1 for a description of the refueling cavity floor seal

design.

. '

23

In an attempt to determine root cause failure, the AIT con-

ducted a review of the available refueling cavity floor seal

documentation.

There is no design documentation available

to describe the mechanics of how the overall seal assembly

operated and no documentation available that verifies the

design adequacy by testing.

In conversations with the vendor Presray it was determined

that the licensee's design was unique in that the seal does

not have a backing plate (located in the area identified as

dimension B in Figure 1 of Appendix 3A).

This backing plate

would a 11 ow better contact between the

11J

11 seal seating

surface and its mating surface.

Initially, the vendor informed the licensee that with the

current design configuration, the

11J

11 seal could be easily

displaced.

This displacement was predicted to be a result of

both buoyancy factors and the action of water flowing under-

neath the seal.

Since the AIT inspection, the licensee has

concluded that due to design tolerances not being controlled,

the

11 J

11 seal could have a 1/8 inch gap between the seating

surface and its mating surface.

With this maximum gap, the

11J

11 seal is flow limiting but to some value in excess of

6000 gpm.

In either case,. the AIT concludes th*at the current design

application is inadequate and that this condition has existed

since initial installation.

There are no design margins

identified relating to th~ vertical and horizontal relation-

ship betwe~n the vessel flange and the cavity floor.

Thus, *

without periodic testing, it cannot be assumed that the seal

would meet its design bases.

Based on this evaluation, the

AIT concludes that the licensee must reevaluate the present design

of the seal ring.

In addition, the seal must be tested to

ensure continued compliance with the design bases.

2.

Equipment Vendor Involvement

The IOER group contacted Presray on August 1, 1988, and the

following items were discussed:

0

0

11 Presray stated that, in the current design configura-

tion, the

11 J

11 seals- could easily be displaced from the

seating *surface due to the action of water flowing

underneath it.

11

11Pr~sray stated that the design of the licensee seal ribg

is unique and in their opinion, requires design improve-

ments to hold the

11J

11 seal in place with a backing plate.

In addition, the inflatable* seal should have a fiber

reinforcement to impr9ve strength and the surface contact

area (footprint) should.be increased."

...

V.

0

0

0

24

11The material used in the

11 J

11 seal should have improved

resiliency and should be subject to a frequent inspection

and replacement cycle.

11

11The original design intent was to use the "J" seal as

the primary seal with the inflatable seal as a backup and

f<;>r "housekeeping" concern*s."

"Presray stated that they manufactured and continue to

supply most of the refueling cavity seals used throughout

the industry. This is the only seal, to their knowledge,

that utilizes a "J" seal without a backing plate."

The AlT concluded that contact with the vendor was only

accomplished by the IOER group during their followup investi-

gation of the event.

This action was taken severa 1 months

after the event.

RADIOLOGICAL CONSEQUENCES

On May 17, 1988, a health physics (HP) technician providing co~tinuous

coverage for contract personnel noticed that the reactor cavity water-

1 evel had decreased and that the radiation levels had increased from

approximately 35mr/hr to IOOmr/hr.

The HP technician immediately

evacuated the Unit 1 containment operating deck (47 foot elevation) and

terminated the radiation work permit (RWP) under which the contract

per~onnel were working.

The purpose of RWP 88-RWP-1507 issued on May 12, 1988, was to allow work

on the upper internals package thermocouple lead conduit.

Appendix 30

indicates how the water level in the refueling cavity varied during the

event.

The AIT reviewed this RWP and concluded that the appropriate

precautions and requirements were adequately specified on the RW~ to

protect the health and safety of those personnel performing the work on

the Unit 1 containment operating deck.

Radiation exposures to personnel were reviewed as a result of this

event and noted that all exposures were well below NRC limits and the

licensee's administrative limits.

After the cavity water level was

restored, the RWP was reinstated for normal access.-

By reviewing the chart recorder for the Manipulator Crane Radiation

Monitor (Rl-RMS-162), the AIT determined that the remote read out in the

control room did not reach "the "Alert" setpoint of 35mr/hr during the

event.

The monitor was located above the reactor cavity. The setpoints

for the radiation monitor, Ri-RMS-162 had been changed to 35mr/hr for

the "Alert" setpoint and SOmr/hr for the "Alarm" setpoint*for refueling

operations.

The normal setpoints for routine operations are*12omr/hr on

11Alert

11-an 600mr/hr on

11Alarm

11

Rl-RMS-162 was calibrated on April 16,

1988, as required by TS prior to removing the Unit 1 reactor vessel

head.

25

The portable radiation survey instrument issuance log for May 17, 1988,

was reviewed.

During the time of the event it was noted that an

operator who entered the Unit 1 containment was issued a survey instru-

ment.

The survey meter was adequate (greater than lr/hr) to survey the

high radiation area.

The key issuance log for high radiation areas

access was reviewed.

The HP technician assigned to the Unit 1 contain-

ment to provide coverage for various tasks accompanied the operator who

entered several high radiation areas and provided positive access

control over each entry as required by TS 6.4.

Radiation, contamination and airborne radioactivity survey results for

the 47 foot elevation and the -27 foot elevation were reviewed.

The

airborne radioactivity concentrations were all less than 25% of Maximum

Permissible Concentration (MPC).

Contamination levels on the 47 foot

elevation of Unit 1 containment remained unchanged as a result of the

event, i.e., 2,000 - 5,000 disintegrations per minute per one hundred

square centimeters ( dpm/100cm 2 ).

However, in the 1 ower containment,

-27 foot elevation, the contamination levels increased from 2,000 -

15,000 dpm/100cm 2 to 4,000 - 20,000 dpm/100cm 2 *

This slight increase

did not create a health and safety concern.

The personnel contamination log was reviewed for the period of

May 16-17, 1988, and the event was discussed with licensee represent-

atives.

No personnel contaminations were at.tributed* to this event.

The AIT was informed that the radioactive liquid that drained from the*

reactor cavity was contained in the incore instrument room sump or in

the containment. sump.

The water was 1 a ter pumped to the High Leve 1

Liquid Waste Tanks and processed as normal radioactive waste.

VI.

FINDINGS OF THE AIT

A.

Radiological Consequences

0

0

0

0

The failure of the Reactor Cavity Seal did not result in

any radiulogical releases to the environment which exceeded

regulatory limits.

Radiation doses received by individuals involved in the event

were all below regulatory limits.

The one operator who was

wetted by the refueling cavity water was surveyed and the

water in the sump was sampled and.counted for radioactivity.

No intakes of radioactivity or personnel contamination

resulted from the event.

Under normal refueling conditions had _the seal failed the

potentia 1 existed for significant personne 1 exposure had a

fuel assembly been in the transfer position (i.e., suspended

from the ref~eling bridge).

The licensee

1s UFSAR Chapter 14, _

11Safety Analysis,

11 does not

address the accident or consequences due to loss of refueling

cavity or- spent fuel pool water level.

..

B.

26

Failure Investigation

The.licensee did not perform a failure evaluation or investigation

following the event.

An investigation was commenced in July by

the IDER group of the event.

C.

Modifications

0

0

0

0

No documentation exits to support the design and/or

installation of the nitrogen system on Unit 1.

Check valves to prevent backflow and overpressure protection

devices installed in Unit 2 nitrogen system are not installed

in the Unit 1 system.

Procedure revisions to include pressure regulators and relief

valve settings and testing were not implemented for either

unit.

EWR-85-200 dated April 1985 for Unit 2 recommended procedure*

revision to change IA pressure regulator settings to 25

psi g versus 20 psi g.

The current revision for procedure

MMP-C-RC-037 used for both units still. indicates 20 psig.

  • o.

Installation and Test of Refueling Cavity Floqr Seal

0

0

0

0

The inflatable seal failed t_o meet the acceptance criteria

established for the preinstallation pressure test during the

1988 Unit 1 refueling outage.

This test is required by

MMP-C-RC~37, Installation and Removal of reactor Cavity Seal

Ring.

Visual inspections performed for .seal degradation and of the

"J" seal seating surfaces, again a preinstallation requirement.

of MMP-C-RC-37 noted several deficiencies.

The licensee evaluated all of the aforementioned conpitions

as being acceptable under EWRs 116 and 148.

MMP-C-RC-37 provides .no guidance on:

Installation and/or removal of the nitrogen bot~1es; and

setting and testing of the relief valves and/or check

valves.

E.

Local Leak Rate Test

0

.*

Operation of system

(nitrogen and

IA)

valves and

regulato*rs outside the boundaries of PT 16.4 were performed

without procedures.

'*

0

0

27

Independent Veri fi cation was performed on nitrogen and IA

system valves and regulators without documenting actions.

No procedural method or documentation was implemented or

developed for the repair of valve 1-IA-849 performed on

May 16 and 17, 1988.

F.

Inadequate Instructions and Drawings

0

Current abnormal procedures for addressing a decrease in

refueling cavity level are inadequate.

The following concerns apply to the nitrogen and IA systems:

0

0

0

0

0.

0

0

limits and precautions to prevent overpressuri zati on and

rupture of the inflatable seal are not available to operators,

no provision to control valve positions (i.e., locks, tags),

no directions or setpoints for adjusting the pressure

regulators, pressure either high or low,

no method or procedure for establishing the preferred

regulator and nitrogen source, and

no lower setpoint limit of nitrogen bott1e pressure.

no logkeeping requirements when nitrogen bottle pressures

are monitored; and

no drawing to indicate system configuration for either system.

G.

Training

The following ar~ noted training findings:

0

0

0

the nitrogen back-up system was poorly understood in its

design, layout, operation, operational limits and precautions;

operational features of the refueling cavity floor seal design

were not understood by operations personnel; and

no training on emergency procedures to mitigate refueling

cavity floor seal failure had been implemented.*

. .

28

VII. GENERIC IMPLICATION OF SEAL FAILURE

Plants with designs similar to Surry have responded to Bulletin 84-03 as

Surry did, basically eliminating catastrophic seal failure as a credible

failure mode because of the passive

11J

11 seal function.

However, this

event indicates that a significant failure can occur even with the

passive seal.

The vendor has 'indicated that plants using the passive

seal design are not likely to have a similar failure because of a

backing plate which tends to maintain a more uniform seating surface

between the seal and its mating surface (as discussed in Section IV.D.

of this report).

The licensee could not locate documentation of any

acceptance tests (including initial preoperational tests) that verified

the passive

11J

11 seal assembly had ever been demonstrated or tested to

meet its design bases.

It is appropriate to require plants with similar

11J

11 seal designs to

verify through functional test that the original design intent of the

seal is maintained.

Tests after each installation need to be performed

to assure proper installation and integrity of the seals.

VIII. ROOT CAUSE DETERMINATION

The apparent root cause of the inflatable seal failure was due to

securing the IA supply to the seal for maintenance with a subsequent

lass of nitrogen pressure from the backup system. * The loss of nitrogen

pressure occurred because one bottle was somehow isolated in that the

regulator was misaojusted while the second bottJe (which was unisolated

with the regulator adjusted properly) bled down in some manner.

The

11J

11 seal root cause failure is much more difficult to de-termine

because there is no assurance that the

11 J

11 seal was ever completely

functional.

Therefore, a design application deficiency may have con-

tributed to the failure._ Also, dimension changes between the reactor

vessel flange (either vertical or horizontal) may. have contributed

to or caused the inability of the seal to perform its intended design

function.

Additionally, in May of 1986 the

11J

11 seal was replaced.

There are no specific procedures for replacing or repairing the seal.

Replacement and repairs were made using the associated design drawings.

This is another possible root cause of the seal failure if the replace-

ment was improperly performed and resulted in the

11J

II seals not being

installed in accordance with the original design.

IX. CONCLUSIONS

The overall conclusion of the AIT is that the root cause of the

seal assembly failure was a combination of inadequate administra-

tive controls, operator error, coupled with inadequate design

application, maintenance and testing of the

11 J

11 seal assembly.

The primary root cause of the.

11J

11 seal failure appears to be

design related.

Inadequate maintenance, testing, and installation

procedures may have contributed to the severity of the event.

Operator error was induced by inadequate operator aids an<f

training.

V

x.

29

Adequate functional testing of the

11J

11 seal would have discovered

the inadequacy of the initial design application and its ability to

perform its design function.

EX IT INTERVIEW

The findings and conclusion of this special inspection were discussed

on September 3, 1988, with those persons indicated in Appendix I.

No

dissenting comments were received .

,

1

I

.. .

APPENDIX 1 - PERSONS CONTACTED

Licensee Employees

  • J. Bailey, Superintendent of Operations
  • R. Bilyeu, Licensing Engineer
  • D. Benson, Station Manager

H. Blake, Superintendent of Site Services

R. Bracey, Control Room Operator (Unlicensed)

  • W. Cartwright, Vice President-Nuclear

B. Cox, Control Room Operator (Unlicensed)

  • S. Eisenhart, Staff Engineer, Independent Offsite

Evaluation Review .

  • E. Grecheck, Assistant Station Manager for Licensing and Safety

M. Hotchkiss, Shift Supervisor

R. Johnson, Ope_rati ans Supervisor*

T. Kendzie, Containment Coordinator

  • J. Logan, Supervisor, Safety Engineering Staff
  • G. Miller, Licensing Coordinator, Surry
  • H.*Miller,_ Assistant Station Manager for Operations and Maintenance
  • L. Morris, Supervisor, Health Physics and Radwaste

R. Mushenheim; Control Room Operator (licensed)

  • G. Pannell, Director, Safety Evaluation and Control

W. Patterson, Human Performance Evaluation System

Coordinator, Surry Power Station

  • -T. Shaub, Licensing Engineer*

J. Simpson, Shift Supervisor

K. Sloane, Shift Supervisor

  • J. Smith, Supervisor, Independent Offsite

Evaluation Review

NRC.Employees

L. Nicholson, NRC Resident Inspector

  • Attended exit interview*on September 3, 1988.

. .

./

AFW

AIT

AP

CRO

cs

DR

EST

EWR

HP

HPES

IA

IOER

JCO

LHSI

LLRT

MPC

NLO

PG

PT

PWR

QC

. RHR

RS

RWP

SD

SNSOC

ss

STA

TS

UFSAR

USS

UTS

w

APPENDIX 2 - ACRONYMS AND ABBREVIATIONS

Auxiliary Feedwater

Augmented Inspection Team

Abnormal Procedure

Control Room Operator

Containment Supervisor

Deviation Report

Eastern Standard Time

Engineering Work Request

Health Physics

Human Performance Evaluation System

Instrument Air

Independent Offsite Evaluation Review

Justification for Continued Operation

Low Head Safety Injection

Local Leak Rate Test.

Maximum Permissible Concentration

Non-Licensed Operator

Primary Grade

Periodic Test

Pressurized Water Reactor .

Quality Control

Residual Heat Removal

Refueling Supervisor

Radiation Work Permit

Station Deviation

Station Nuclear Safety Operations Committee

Shift Supervisor

Shift Technical Advisor

Technical Specification

Updated Final Safety Analysis Report

Unit Shift Supervisor

Unit Test Supervisor

_

Westinghouse Electric Corporation

C.

APPENDIX 3 - DESIGN DESCRIPTIONS

(, '

,I

APPENDIX 3A - REFUELING CAVITY FLOOR SEAL

GENERAL DESCRIPTION

The refueling cavity floor seal (Ftgure 1) is intended to seal the open.ing

between the reactor vessel flange and the refueling cavity floor.

This allows

the refueling cavity to be filled with borated water so that refueling opera-

tions can be accomplished under water.

The seal assembly consists of two separate sealing devices; an active or

inflatable seal and a passive or "J" seal.

The inflatable seals are manufactured from a nitride rubber material and are

designed to seal against a hydrostatic head of 27 feet of water.

A design

operating pressure of 25 psig is specified under ambient conditions of 60°F to

120°F.

The design pressure is 50 psig.

Figure 1 shows the inflatable seal in both the inflated and deflated conditions

(inner seal deflated, outer seal inflated).

Compressed air or nitrogen is

introduced into the inflatable seal via air connections on the bottom of the

seal ring.

The seal ring contains two air passages which direct the air to the

s*ea 1.

The "J" seals provide a passive sealing function and are intended to minimize

and/or preclude leakage ,n case of. inflatable seal failure.

The "J" seals are

fabricated from a high grade, thread-type natural rubber compound.

They are

7/8-inch in diameter with a 3/8-inch hollow inner core.

When the assembly is

lowered into place, the seal_ supports are required to be adjusted to achieve a

1 3/16-inch gap (dimension "A", Figure I).

Permanently attached to the vessel flange and refueling cavity floor are drip

pans which collect leakage past the seals.

This leakage is directed to the

reactor coolant loop rooms, through the telltale drains to the containment

sump.

The drlp pans and associated small drain lines (3/4-inch) are capable of

handling small leakage by the ~eais.

, .

APPENDIX 38 -

INSTRUMENT AIR SYSTEM

DESCRI PT! ON

The containment IA. system (Figure 2) consists of two water-sealed, rotary

compressors and associated refrigerant air driers installed on the 11

16

11

elevation of the main steam valve buildings for Units 1 and 2.

The compressors

take a suction from the containment via a 3

11 penetration.

Containment trip

valves are provided on both sides of* the penetration.

Each compressor has a

minimum capacity of 24-scfm at 90 psig.

A shell and tube heat exchanger is

provided on each compressor to cool the seal water.

Cooling water for these

heat exchangers comes from the containment cooling chilled water system.

The

alternate supply of cooling water is the component cooling system.

A connec-

tfon to component cooling water is also provided for seal-water make-up.

One

compressor is in continuous service and automatically loads or unloads to meet

system demand.

The other compressor is on standby and starts automatically if

system pressure decreases to 85 psig.

Each compressor discharges to its own moisture separator and filter.

Water

removed from the air by the separators and air driers is directed to a sump,

where a small sump pump transfers the water to the liquid waste system.

Each

air compressor discharges to its own refrigerant air drier.

The piping allows

the air compressors to be cross-connected with the air driers as well as

allowing them to *bypass the driers completely.

Air exiting the driers has

a dewpoint of 35°F.

The air enters the containment through a containment

trip valve using containment penetration 47 for Unit 1_ IA .

'

'

APPENDIX 3C - NITROGEN BACK-UP SYSTEM

The nitrogen back-up system, as shown in Figure 2 (configuration based on

personnel interviews), consists of two portable nitrogen cylinders each con-

taining 301 cubic feet of nitrogen at approximately 2200 psig when full. These

bottles supply nitrogen to 2200/20 psig variable pressure regulators. Flexible

tubing connects the downstream pressure of the regulator through an isolation

valve to a junction from

the containment IA system.

This nitrogen pressure

supply is then supplied to the refueling cavity floor seal if IA pressure is

not available.

The pressure regulators on the nitrogen bottles should be set

at 20 psig and the IA pressure regulator should be set at 25 psig.

L .

-1

~I

APPENDIX 30 - UPPER CORE INTERNALS STORAGE

As shown on the attached drawing, Figure 3, the upper internals package

(item 1) rests in the storage area on a stand (item 2) which holds the inter-

nals up some 6" off the* bottom of the reactor cavity.

The total height of the

upper internals .package, including the 611 offset provided by the stand, is 26

1

When the refueling cavity water level is "normal" (item 3) the top of the upper

internals package is about 1

16

11 below the surface of the water.

On March 17, 1988, W contractor personnel were working on upper internals

thermo coup 1 e 1 ead conduit.

This work was being performed from the refueling

bridge positioned directly over the upper internals package storage location.

The water level had been reduced about one foot below (item 4) the normal level

thus reducing* the remaining shielding to six inches.

Due to the loss of

refueling cavity water through the refueling cavity floor seal, this shielding

water was r_educed an additional three feet.

Following the event the water

level could have dropped to approximately twenty-four feet.

Thus allowing

about two* feet six inches of the upper interna 1 s package to be out of the

water .

a*-ct *

    • -1 .
    • -~* **-*~*
  • BEFORE COMPRESSION

Dimension

118

11

ltEI.ATML.£

SEAL

(Outer)

_...,..._.._.,~i-a-- Ori p Pans

Air Supply Line

SURRY REACTOR.CAVITY SEAL RING ASSEMBLY

Figure 1 *

REACTOR CAVITY LINER

EL 1e*-4*

~ <

r

!"',J

, .

'

I

1

1

  • -

To

' Cav1 ty

Ring

Seal

'C' Loop Room

'

I

I

I

l

Flex Tubing

I

I

CONFIGURATION

BASED UPON

OPERATOR*

  • I INTERVIEWS

r

INSIDE

CONTAINMENT

1-842

1-936

/

OUTSIDE

CONTAINMENT

UNIT 2 Air

Unit 1 Containment

Instrument Air

PS~ ~)PS

J

Unit 1 Containment

V1

Instrument Air System/Nitrogen Backup System

Figure 2

I

1-986

f'.

C r

\\', ..

~ -~ ;t .

-

Reactor Cavity

Water Seal

UPPER CORE INTERNALS STORAGE

Normal Water Level ~-

_

_

_

_

- -Reduced-Water-Level - ~

_ _

_

1:oii_ol_Iii1er~1~ - _-:-

-

Post Event

Water level


27' 6"

- 26' 6" -

,:-a6"' _ 0.,. _ --:. -=--

2~ .§_. -

Reactor Upper --4

(i)

Internals

)..._1-..~.,L_....L_~--L__.1..~__.___.~~~"l~

Pool Bottoa

Storage Stirfd R *

1~ter111ls Storage

\\1----------::J

Reactor

Figure 3