ML18142A178

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Insp Repts 50-280/84-30 & 50-281/84-30 on 841001-1102. Violation Noted:Inadequate Electrical Maint & Testing Procedures
ML18142A178
Person / Time
Site: Surry  
Issue date: 11/28/1984
From: Burke D, Marlone Davis, Elrod S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18142A174 List:
References
50-280-84-30, 50-281-84-30, IEB-84-03, IEB-84-3, NUDOCS 8502060333
Download: ML18142A178 (6)


See also: IR 05000280/1984030

Text

Report Nos.:

50-280/84-30 and 50-281/84-30

Licensee:

Virginia Electric and Power Company

Richmond, VA

23261

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry" 1 and 2

Inspectiondld

Conduct d:

October 1 - November 2, 1984

Inspectors: ~----+---------------------

0. ~,~J1r,~7, Senior Resident Inspector

Approved

dft1Jl#

M. J. Davis, Resident Inspector

lrod, Section Chief

Division of Reactor Projects

SUMMARY

igned

ti l~rlrr

Defte Signed

Scope:

This routine, unannounced inspection entailed 180 inspector-hours at the

site, in the areas of plant operations and operating records, refueling operations,

plant maintenance and surveillance, plant security, followup of events, licensee

event reports, and IE Bulletins.

Results:

In the areas inspected, one violation was identified in the plant

maintenance and surveillance area (inadequate electrical maintenance and testing

procedures - paragraph 5.b).

8502060333 850fi6

PDR ADOCK 05000280

G

PDR

REPORT DETAILS

1.

Licensee Employees Contacted

R. F. Saunders, Station Manager

D. L. Benson, Assistant Station Manager

H. L. Miller, Assistant Station Manager

D. A. Christian, Superintendent of Operations

M. R. Kansler, Superintendent of Technical Services

H. W. Kibler, Superintendent of Maintenance

D. Rickeard, Supervisor, Safety Engineering Staff

S. Sarver, Superintendent of Health Physics

R. Johnson, Operations Supervisor

R. Driscoll, Director, QA, Nuclear Operations

Other licensee employees contacted included control room operations, shift

technical advisors (STAs), shift supervisors, chemistry, health physics,

plant maintenance, security, engineering, administrative, records, and

contractor personnel and supervisors.

2.

Exit Interview

The inspection scope and findings were summarized on a biweekly basis with

certain individuals in paragraph I above.

The violation of paragraph 5.b

was discussed with licensee management.

3.

Licensee Action on Previous Enforcement Matters

This subject was not addressed in the inspection.

4.

Unresolved Items

Unresolved items were not identified during this inspection.

5.

Operations

a.

Units I and 2 operations were inspected and reviewed during the inspec-

tion period.

The inspectors routinely toured the control room and

other plant areas to verify that plant operations, testing, and main-

tenance were being conducted in accordance with the facility Technical

Specifications (TS) and procedures.

The inspectors verified that

monitoring equipment was recording as required, equipment was properly

tagged, and plant housekeeping efforts were adequate.

The inspectors

also determined that the appropriate radiation controls were properly

established, critical clean areas were being controlled in accordance

with procedures, excess material or equipment was stored properly, and

combustible material and debris were disposed of expeditiously.

During

tours, the inspector looked for the existence of unusual fluid leaks,

piping vibrations, piping hanger and seismic restraint settings,

various .valve and breaker positions, equipment caution and danger

2

tags, component positions, adequacy of fire fighting equipment, and

instrument calibration dates.

Some tours were conducted on backshifts.

Inspections included areas in the 1 and 2 cable vaults, swit_chgear

rooms, contra 1 rooms, and cab 1 e penetration areas to verify certain

breaker and equipment positions for safety re 1 ated components.

The

inspector routinely conducted partial walkdowns of ECCS systems.

During the inspection period, the inspectors conducted periodic inspec-

tions in the accessible areas of the Unit 2 Safeguards Building and

valve pit-checking ECCS trains, auxiliary feedwater systems, and

containment spray trains.

Unit 1 containment inspections verified

shutdown systems were operable and refueling cavity levels and boron

concentrations were within requirements.

The inspectors examined the Unit 1 refueling cavity seal ring to verify

that the design was different from the seal mentioned in IE Bulletin

84-03, and adequate.

The Surry design utilizes two independent seals.

The first consists of a J-type inner seal which seats atop the reactor

vessel flange ring and a similar outer seal which contacts the refueling

cavity floor to seal the space between the vessel and refueling cavity.

The second seal is a dual inflatable rubber seal which is mounted on a

vertical support in the seal ring and expands against the vertical edge

of the reactor vessel flange; a similar outside seal expands from the

support to the refueling cavity floor flange.

New inflatable seals

were installed on the seal ring and tested prior to ring installation

and use during this outage.

A pair of circumferential troughs are

permanently installed beneath the inner and outer ring seals to collect

any water which may leak by the seals. This is used to verify positive

sea 1 i ng when the refue 1 i ng cavity or can a 1 is being fi 11 ed from the

RWST.

The troughs drain through installed piping to the loop rooms in

containment, which are monitored periodically for leakage.

The inspec-

tors also verified that the seal testing and installation procedure,

MMP-C-RC-037,

specifies inflatable seal pressure (20 psig).

The

licensee performed evaluations with regard to refueling cavity water

sea 1 fa i 1 ures and revi sect Abnorma 1 Procedure AP-22 to address sea 1

assembly leakage or failure.

The inspectors had no further questions

at this time.

IE Bulletin 84-03 remains open pending further NRC

Region II review.

b.

Unit 1 began the reporting period shutdown for a refueling and main-

tenance outage.

Unit 2 began

the reporting period operating at full power.

On

October 29, 1984, during undervoltage testing on the

10 1 transfer bus,

the 2A main feedwater pump tripped due to automatic load shedding

initiated by the testing.

The test procedures failed to specify the

positioning of the load shed mode selector switch to manual position or

opening the defueled Unit 1 breaker 15Al.

The Reserve Station Service

(RSS) load shedding is actuated by simultaneous loading of both units

on a transfer bus, e.g., close bfeaker 15Al and 25Al.

One main feed-

water pump and one condensate pump are then automatically shed for

3

each unit.

The trip of the

1 2A 1 main feedwater pump resulted in a

12C 1

steam generator low water level and resultant reactor trip. During the

electrical transfer from station service to reserve station service or

off-site power following the trip, the

1A

1 reactor coolant pump stopped

since its RSS power source, the

10 1 transfer bus was isolated.

Rod

M-10 in control bank

18 1 appeared to hang up momentarily at 30 steps

when the unit tripped.

Subsequent rod exercises and rod drop testing

was satisfactory at intermediate shutdown conditions.

The rod was

dropped from the fully withdrawn position in 1.2 seconds, which is

normal.

Additional rod drop testing is scheduled to be performed at

normal operating conditions prior to Unit 2 restart.

Following restart

of the 1A1 reactor coolant pump, increased seal leakoff, vibration and

increasing temperature on the lower thrust bearing resulted in the

operators securing the pump.

The Unit ended the reporting period in

the cold shutdown condition with the 'A' loop drained for reactor

coolant pump seal and bearing repair on the

1A1 reactor coolant pump.

A low oil level in the RCP motor bearing reservoir apparently caused

the bearing failure; there was no annunciation or alarm of low oil

level due to the failure of the level switch itself.

The failure to provide adequate electrical testing and maintenance

operations procedures for the October 29 testing and maintenance

described above, which led to the RSS load shedding and reactor trip,

is a violation (280 & 281/84-30-01). Another example of this violation

occurred on October 20, 1984, during electrical switching of lighting

busses while defueling the Unit 1 core.

Inadequate electrical proce-

dures and switching orders resulted in the temporary loss of electrical

power to the lights in the Unit 1 containment and loss of the direct

communications between the contra 1 room and the refue 1 i ng cavity

manipulator crane in containment (TS 3.10.A.10) during irradiated fuel

movement in the cavity poo 1.

A 11 fue 1 movement stopped until the

communications and lighting were restored.

6.

Technical Specification Review

The inspectors reviewed the Surry Units 1 and 2 Technical Specifications

(TS) to determined if the systems required to be operable by Section 3 had

surveillance requirements in Section 4 which verified or demonstrated

operability.

The Surry non-standard TS, originally issued in 1972 but

amended regularly, does describe certain operability requirements or LCOs

in Section 3 which are not covered by surveillance requirements in Section 4.

However, the safety-re 1 a ted systems and equipment survei 11 ance to verify

operability are included in the Inservice- Inspection and Testing Programs,

which are reviewed and approved by the NRC.

Examples included the component

cooling water (CCW) pumps described in Section 3.13 of the TS.

The CCW pump

performance requirements are not specified in Section 4 of the TS, however,

the pumps are tested monthly by periodic test procedure PT 41.1,

11 CCW Pump

Operabi 1 ity and Performance Test,

11 under the IST program.

The inspectors

also identified certain TS Section 3 items, such as TS 3.14.A.2.a, which-

requires flow through one bearing cooling water heat exchanger, which did

not appear in Section 4 or the ISI program.

This inspection will continue

4

under inspector followup item (280/84-30-02).

The bearing cooling water

system cools the main generator, turbine, and other secondary equipment as

well as the instrument and service air compressors.

7.

Instrumentation Review

8.

Fo 11 owing the Unit 1 shutdown, Service Water ( SW) testing was performed

which included stroking the SW inlet isolation valves to the recirculation

spray heat exchangers and flowing the system.

When flow was established, 5

of the 6 SW flow instruments (FI-SW-105s and 106s) did not respond, and the

one instrument that did indicate flow remained upscale when the inlet valves

were closed.

The licensee is inspecting the Units 1 and 2 SW flow instruments

to identify the problem (!FI 280/84-30-03).

LER Review

The inspectors reviewed the License Event Reports (LERs) listed below to

ascertain that NRC reporting requirements were being met and to determine

the appropriateness of corrective action taken and planned.

Certain LERs

were reviewed in greater detail to verify correction action and determine

compliance with TS and other regulatory requirements.

The review included

examination of logbooks, internal correspondence and records review of SNSOC

meeting minutes, and discussions with various staff members.

Within the

areas inspected, no violations were identified.

(Closed)

LER 281/83-40 concerned ra i nwate*r grounding the 3A Auxi 1 i ary

Feedwater Pump Motor.

The motor windings were dried and the pump returned

to service.

Subsequent repairs to the safeguards building roof have been

completed.

(Closed) LER 280/83-37 concerned a possible dropped rod accident analysis

that may not represent the limiting case. A detailed evaluation documented

the NFE technical Report No. 334, determined that the current UFSAR rod drop

analysis is the most limiting for all core cycles.

(Closed) LER 280/83-44 concerned inoperable snubbers found during snubber

inspections. The inoperable snubbers were repaired. A 100 percent inspec-

tion of snubbers was subsequently performed.

(Closed) LER 281/83-37 concerned FCV-FW-2488, the

1B1 Main Feedwater Regu-

lating Valve failing to fully close on a SI signal.

The feedwater control

valves have been rebuilt and are currently performing satisfactorily.

(Closed) LER 281/83-52 concerned a containment spray pump breaker tripping

during attempts to start the pump.

The breaker overloads were checked and

the armature stop screw on the overload device was found to be loose. This

caused armature vibration and premature breaker tripping.

The stop screw

was tightened and the instantaneous trip settings were adjusted.

The pump

was tested satisfactorily.

5

9.

Plant Physical Protection

The inspector verified the following by observations:

a.

Gates and doors in protected and vital area barriers were closed and

locked when not attended.

b.

Isolation zones described in the physical security plans were not

compromised or obstructed.

c.

Personnel were properly identified, searched, authorized, badged and

escorted as necessary for plant access control.