ML18139B075

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LER 81-006/03L-0:on 810114,at Full Power,C Safety Injection Accumulator Found to Have Boron Concentration of 1943 Ppm, 7 Ppm Below Required Limit.Caused by Leakage Through Check Valve 1-SI-144.Valve Isolated
ML18139B075
Person / Time
Site: Surry Dominion icon.png
Issue date: 02/13/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B074 List:
References
LER-81-006-03L-02, LER-81-6-3L-2, NUDOCS 8102200529
Download: ML18139B075 (2)


Text

NRC"FORM 366 17-77) e LICENSEE EVENT REPORT U. -CLSAR REGULATORY COMMISSJCN CONTROL. BLOCK: j.

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-,!6 \.!.I (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION!

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A I s I pl s I 2101 0I OI -1 0I 01 01 01 01 -~ 0 I O 101 4 11 J 1 11 I 1101 I . I© LICENSEE CODE 14 15 LICENSE NUMBER . , . :ZS 26 LICENSE TYPE JO 57 CAT 58

~~~~ l1..J©lo Is lo lo !o !2 Is 11 6810169a Ii I1 !4 ! B ! l 741©1°75 12 11 13 IB 11 80I© 60 . 61 DOCKET NUMBER EVENT DATE REPORT CATE EVENT OESCr!IPT!ON AND PROBABLE CONSEQUENCES@ .
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(]ID I boron concentration of 1943 ppm, 7 ppm below. the required limit of* 1950 ppm. This

[]JI] I is contrary to T.S.-3.3.A.2 and is reportable per T.S .. -6.6.2.b(2). *since "C" I CI:I!] I accumulator boron concentration was increased above 1950 ppm ~hfn*t1re--zr- hr. 1

((El I Tech. Spec. limitation (-55 min.), the health and safety of the public were not IIIIJ I affected. I,.

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7 8 9 BD SYSTEM CAUSE CAUSE COMP. . VALVE cooe.

1v1A1L 1v 1E1x 1e w@ w@ -*

COOE SUBCODE COMPONENT CODE SUBCODE SUSCODE CITl]

7 8 1s 1F 1@ L.!J@

9 10 11 L!.J@

12 13 18 19 :ZD SEQUENTIAL OCCUR REN~ REPORT REVISION.

t:':;\ LE R/RO *cVENT VEAR REPORT NO. CODE TYPE NO.

~ REPORT NUMBER 1s 21 11 22I I23 I Io Io I 6126 24 1.....-1 27 Io I 3 I

ZS *. 29 LhJ

. 3D 1-1 31 l.LI 32 ACTION FUTURE EFFECT SHUTDOWN f.::\ ATTACHMENT . NPRD-4 PRIME C:OMP, ,. COMPONENT TAKEN ACTION ON Pl.ANT . . METHOD HOURS ~ . SUBMITTED *FORM liUB.

  • SU""LIER . MANUFACTURER ,

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  • L!.J LLI l O ! 0 I Of 35 36 37 Of 40 ILJ@.

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.CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS*@

_ o:I.]J JThe cause of the reduced concentration was leakage through check valve l-SI-144.

[IJJJ !The corrective action was .to isolate this valve with future plans to repair the

.o::u:J 1valve during an outage of sufficien~. duration.,. -I OJI]

o:El8 7 9 80 FACILITY '3o' METHOD OF

. STATUS *  % POWER . OTHER STATUS \;:::I DISCOVERY *DISCOVERY DESCR;PTION tilIJ L!J@ I 1 j OI 01@1 N/A I WI SamEling 7 8 9 10 12 13 t.::\

44 45 46 :80 .-

ACTIVITY RELEASED OF RELEASE CONTENT AMOUNT OF ACTIVITY ~ .. _LOCATION OF R.ELEASE .

!IE] ~ @ l..bl(§I

, a 9 10 11 N/A I I 45

!ilA J 80 FIERSONNEL EXPOSURES t.:::\

NUMBER A TYPE DESCRIPTION .

!III]

' 8 9

!0 ! 0 ! 0 11,~L!..Ji__ 12 1:1

___. : . ; . N : . . : / A = - - - - - - - - - - - - - - - - - - - - 80 Fl:RSONNEL INJURIES t,;";\

NUMBER . DESCRIPTION6 IITI] jo I o! o I@ N/A

, a g 11 12 * . 80 l..CSS OF OR OAMAGE TO FACILITY TYPE DESCRIPTION .

143'- ..

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[III] l..:J@ . N/A 7 8 9 10 1!0 PUBLICITY t::'\ NRC USE ONLY

  • ISSUEOt,;:;\ DESCRIPTION~ .*

'° II@ l!!Je, * . N/A ll III I I lSDI!;

7 9 68 69 .

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l:

e ATTACHMENT I SURRY *POWER STATION, UNIT 2 DOCKET NO: 50-281


* -- - - - REPORT-NO:-.----. 81-006/03L-O EVENT DATE: 01-14-81


~---

TITLE of EVENT: SI'ACCUMULATOR LOW BORON CONCENTRATION

1. EVENT DESCRIPTION:

With the unit* at full power, it was determined through sampling that,'.


***-the *bor6n-*concentratici1f of **".c" Safety Injection Accumulatc>'i~ was a:t T9tcr""ppm___ *-*- * - - *

' which .is below the 1950 ppm.required by Tech. Spec. *This.is contrary to

---**** * ** *-*Technical -Specif*icatio1f3-;3:-A.2 and is reportable per T.s*.-6~-6~2~b'(2r.*--* --- ------------ --

2. PROBABLE CONSEQUENCES:
    • --*---*-***-*-------------The *:rediiiidant**safe-t:y--Irijection accumulators~ 'A' & 'B', *were-veril{iif*-~-----* *--------*-

to be above the minimum concentration (2093 & 2098 respectively). * "C" *


... *------..--- --- ~SI-*ACCiim.Ula*t*,:;-r-was*-*ret*Urned~to an operable status; C gt"eiter -t:-itaii-i~f50--ppm-;- ----------**-

within the 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> Tech. Spec. limitation (55 minutes,. Therefore, the health


.. _ and safety of the public were not affected. -~ ----~- _

3. CAUSE:

There are several manual valves inside -containment which must be *open*in order to perform the month.1-y flushing of sensitized stainless steel pipe. In order that the number of containment entries could be kept to _:a minimum, thf!J~e manual valves had been *left-open. With manual valves 2-SI-249 and 2-SI_-256 left open, charging system pressure existed on the down~tr_eam side of check valve l-SI-144 which leaked througj:i, thereby diluting "C" accumulator.

4. IMMEDIATE CORRECTIVE ACTION:

__ .. ____ .. The illlmediate corrective action was to recirc. the accumulator"with- -the, -

RWST to bring the boron concentration within specification.

. -*- .. .:._ -----*------.---* ~----*---*- - ---* -*-

5. SUBSEQUENT CORRECTIVE: ~ACTION:

---*-***-- ---------- --*- *--*- ------*~. **--- --*--- _,,. _________ _

The subsequent corrective action was. to close the manuai valves ,in.

containment.

6. FUTURE CORRECTIVE ACTION:
        • --- - - - ---- *---- , *** Check-valve 1-SW-144---i;s- scheduled to be repaired during *the next-*outag-e---- - -**** -**-*
  • of sufficient duration.

-*---*---- '] .----GENERIC IMPLI-CATI6N:- ,_, --*--

None.