Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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PS~G*
- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit June 15, 1996 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 1 DOCKET NO: 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating report for the month of May is being sent to you.
(b;~
- David F: Garchow General Manager -
Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 475 Allendale Road*
King of Prussia, PA 19046
~----
' 9606200216 960531 PDR ADOCK 05000272 R PDR The power is in your hands.
95-2168 REV. 6/94
AVERA. DAILY UNIT POWER LEVEL e Docket No.: 50-272 Unit Name: Salem #1 Date: 06/10/96 Completed by: Robert Phillips Telephone: 339-2735 Month May 1996 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl
Completed by:
- OPERATING DATA REPORT Robert Phillips Docket No:
Date:
Telephone:
50-272 06/10/96 339-2735 Operating Status
- 1. Unit Name Salem No. 1 Notes
- 2. Reporting Period May 1996
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating (Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
- 9. Power Level to Which Restricted, if any (Net MWe) N/A
- 10. Reasons for Restrictions, if any NA This Month Year to Date cumulative
- 12. Hours in Reporting Period 744 3647 165864
- 12. No. of Hrs. Rx. was Critical 0 0 104380.5
- 13. Reactor Reserve Shutdown Hrs. 0 0 0
- 14. Hours Generator On-Line 0 0 100388.3
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 0 0 318062229.2
- 17. Gross Elec. Energy Generated (MWH) 0 0 105301000
- 18. Net Elec. Energy Gen. (MWH) -2458 -11191 100193722
- 19. Unit Service Factor 0 0 60.5
- 20. Unit Availability Factor 0 0 60.5
- 21. Unit Capacity Factor (using MDC Net) 0 0 54.6
- 22. Unit Capacity Factor (using DER Net) 0 0 54.2
- 23. Unit Forced Outage Rate 100
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
The outage type changed to Forced outage on the first day of this reporting period.
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
To be determined.
8-1-7.R2
- Jan-April was/, but due to no service hours; the approved equation of : Forced outage hrs (Forced outage hrs + Unit Service hrs) now equals 100%e
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH May 1996 DOCKET NO.: ~5~0_-=27~2..____ _~
UNIT NAME: Salem #1 DATE: 06/10/96
- COMPLETED BY: Robert Phillips TELEPHONE: 609-339-2735 METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE 4092 05-01-96 F 744 FC 4 ---------- HJ 2422 Nuclear Steam Generator Systems.
1 2 3* 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of (NUREG-0161)
E-Operator Training & License Examination Previous outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
10CFR50.59 EVALUATIONS
- DOCKET NO: 50-272 MONTH: MAY 1996 UNIT NAME: S.A...LEM 1 DATE: 06/10/96 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) lEC-3425, Pkg. 1 "Security System - CCTV Camera Installation "B" Building Roof' Rev. 0 - The DCP adds three new cameras to the roof of "B" Building to provide surveillance coverage at the circulating water intake structure. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 95-108)
- 2. Temporary Modifications (TMOD)
TMOD 96-14 "Temporary Ventilation For Support OfDCP lEC-3505 Implementation" Rev. 0 - This temporary modification package provides an alternate source of ventilation to the Unit 1 Control Room, Electrical Equipment Room, Data Logging Room, and Relay Room areas which are normally supplied from the Unit 1 Control Area Air Conditioning System (CAACDS). In order to support implementation ofDCP lEC-3505, the Unit 1 CAACS will be out of service intermittently, and therefore, will be unavailable to provide ventilation to the areas listed above.
The temporary modification assures temperatures are maintained below the technical specification value, safety margin is not reduced. (SORC 96-055)
TMOD 95-073 "Isolation of 12A CC Heat Exchanger" Rev. 1 - The purpose of this TMOD is to isolate the service water to the 12A half of the 12 Component Cooling Heat Exchanger. This will allow return of 12 Component Cooling Heat Exchanger back to service with on-going repairs to Service Water valves associated with the 12A half of the heat exchanger. The temporary modification will not affect the operability of the
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: MAY 1996 UNIT NAME: SALEM 1 DATE: 06/10/96 COMPLETED BY: R. HELLER TELEPHONE: 609-3 3 9-5162 component cooling system. Adequate margin exists in the design of the 12 Component Cooling Heat Exchanger that each half is capable of handling loads generated while the plant is defueled. Operability is not affected and therefore there is no reduction in the margin of safety as defined in the basis of any Technical Specification bases. (SORC 96-057)
- 3. UFSAR Change Notice (SCN)
SCN 96-038 "Accident Analysis Update" - This change implements new analyses and revises text in four Chapter 15 accidents in the Salem UFSAR. The accidents affected are: Excessive Heat Removal Due to Feedwater System Malfunctions; Major Reactor Coolant System Pipe Ruptures (Large Break Loss-Of-Coolant-Accident, only); Major Rupture of a Main Feedwater Line, and Mass and Energy Releases to Containment Following a Steamline Rupture. The results for the re-analyses of these accidents do not violate or change acceptance limits. Design failure points and system limitations remain unchanged. Hence, there has been no change to the margin of safety as defined in the basis of any technical specification. (SORC 96-057)
SCN 95-17 "Changes to the Salem Generating Station Organization Structure and Responsibilities" - The Nuclear Business Unit (NBU) has been re-organized to improve the direction, control, oversight, and accountability over nuclear plant operations and support functions. The NBU organization changes addressed by this proposal are any changes which hecame effective through April 18, 1996. The proposed changes reflect organization structure and responsibilities effective April 18, 1996, editorial enhancements, and clarifications. There is no reduction in the level of management control, responsibilities, training and qualifications, authority or commitments. The revised organization should improve alignment of responsibilities, and management focus on activities related to plant safety.
(SORC 96-057)
10CFR50.59 EVALUATIONS DOCKET NO:
- 50-272 MONTH: MAY 1996 UNIT NAME: SALEM 1 DATE: 06/10/96 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 SCN 96-44 "Loss ofCCW Flow to RCPs: FSAR Section 9.2.2.8.2 Revision" - This 50.59 evaluates the SER Supplement 3 of the NUREG-0517 and clarifies FSAR Section 9.2.2.8.2 by revising the UFSAR such that it meets the intent of the SER. It also serves as an additional safety evaluation document for the previously performed procedure changes of S !/S2. OP-AB.RCP-001 (Q) Rev. 3 and Sl/S2.0P-AB.CC-000l(Q) Rev. 2. The revised UFSAR will not reduce the margin of safety, as described in the bases for any Technical Specifications. (SORC 96-057)
SCN 96-16 "Response to PR 960209175 Making Clarifications to UFSAR"
- PR #960209175 identified items that need to be corrected in the Salem Generating Station UFSAR. The pages affected are 10.4-2 through 10.4-4. The proposal does not reduce the margin of safety as defined in the basis of any Technical Specifications. Sections 3/4.3 "Instrumentation," 3/4. 7 "Plant Systems" and 3/4.11 "Radioactive effluent" of the Salem Units 1 and 2 Tech Specs and their bases were reviewed in order to arrive at this determination. (SORC 96-068)
- 4. Procedures and Revisions Security Plan "Salem-Hope Creek Security Plan" - The Salem-Hope Creek Security Plan is revised to implement Technical Specification Amendment No. 181/162 (Salem) and Amendment No. 95 (Hope Creek), which involved the deletion of two security-related items, which are required to be relocated to the Security Plan. The first item is the requirements for SORC review of the Security Plan and its implementing procedures. The second is the requirements to audit the Security Program every twelve months. The SORC review requirement is added to the introduction to the Security Plan. The audit requirement already exists in the Plan in paragraph 13 .1 and that the audit is under the cognizance of the Off-Site Safety Review staff.
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: MAY 1996 UNIT NAME: SALEM I DATE: 06/10/96 COlVIPLETED BY: R.HELLER TELEPHONE: 609-339-5162 (Cont'd)
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 96-057)
- 5. Evaluations S96-0ll "Safety Evaluation for QA Organizational Changes" - This change to the UFSAR involves moving existing responsibilities between managers within the QA-NSR organization, specifically, the Quality Verification responsibilities previously assigned to the Manager - Quality Assessment are now assigned to the Manager - Corrective Action/Quality Services and the QA - Programs responsibilities previously assigned to the Manager - Corrective Action/Quality Services are now assigned to the Manager - Quality Assessment. This will allow the organization to more efficiently carry out theses functions. The proposed changes are administrative in nature and do not modify the margin of safety defined and maintained by Technical Specifications. (SORC 96-058)
S-C-CN-MEE-1073 "Condensate System Design Pressure Reconciliation" Rev. 0 -
The design basis engineering evaluation S-C-CN-MEE-1073 Rev. 0, provides the basis for taking exception to the system Code of record for the associated piping, vessels and valves.
This evaluation maintains the intent of the Code such that no safety concerns or adverse accidents may occur. Technical Specifications and their bases were reviewed in order to arrive at this determination. (SORC 96-058)
II .*
REfUELING INFORMATION DOCKET NO: 50-272 MONTH: MAY 1996 UNIT NAME: SALEM 1 DATE: 06/10/96 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH : MAY 1996 Refueling information has changed from last month: YES . X . NO ,,_._ ____,,
Scheduled date for next refueling: (to be determined)
Scheduled date for restart following refueling: (to be determined)
- a. Will Technical Specification changes or other license amendments be required?
YES . . NO ,,_._ ____,,
NOT DETERMINED TO DATE . X .
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES. . NO. X .
If no, when is it scheduled? (to be determined)
Scheduled date(s) for submitting proposed licensing action: . n/a Important licensing considerations associated with refueling:
Number of Fuel Assemblies:
- a. Incore 0
- b. In Spent Fuel Storage 989 Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632 Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: September 2008 8-l-7.R4
SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 1 MAY 1996 SALEM UNIT NO. 1 The Unit is in a refueling outage and remained shutdown for the entire period. Evaluation and assessment of the Steam Generator tube indications continues. According to commitments from PSE&G and a subsequent confirmatory action letter from the NRC, the Unit will remain shutdown pending completion of the following actions:
- Appropriately address long standing equipment reliability and operability issues
- After the work is completed, conduct a restart readiness review to determine for ourselves the ability of each Unit to operate in a safe, event free manner
- After the restart review, meet with the NRC and communicate the results of that review