ML18101A628

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Forwards Insp Repts 50-272/95-02 & 50-311/95-02 on 950129- 0322.Violations Noted But Not Cited
ML18101A628
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/07/1995
From: Cooper R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Eliason L
Public Service Enterprise Group
Shared Package
ML18101A629 List:
References
NUDOCS 9504170012
Download: ML18101A628 (6)


See also: IR 05000272/1995002

Text

EA# 95-62

Mr. Leon R. Eliason

Chief Nuclear Officer & President

Nuclear Business Unit

April 7, 1995

. Public Service Electric and Gas Company

  • P .0. Box 236

Hancocks Bridge, NJ

08038

SUBJECT:

NRC INSPECTION NOS. 50-272/95-02; 50-311/95-02

Dear Mr. Eliason:

The enclosed report documents an inspection for public health and safety,

conducted by Mr. C. Marschall, Senior Resident Inspector and other members of

the NRC resident and regional staff at the Salem Nuclear Generating Station

for the period between January 29, 1995 and March 22, 1995.

The inspectors

discussed the findings of this inspection with Mr. J. Summers, General

Manager-Salem Operations, and other members of your staff. '

Within the scope of this inspection, relative to Salem Unit 2, the inspectors

identified several examples of continued weaknesses relative to corrective

action determination and effectiveness, and an example of inadequate measures

to assure proper configuration control for a safety-related system following

modification of pressurizer safety valve loop seals.

As a result, the Unit

was operated outside the design basis for an entire operating cycle. These

apparent violations, as described in Enclosure 1, are being considered for

escalated enforcement action in accordance with the "General Statement of

Policy and Procedure for NRC Enforcement Actions" (Enforcement Policy), 10 CFR

Part 2, Appendix C.

Accordingly, a Notice of Violation is not being issued

for these inspection findings at this time.

The number and characterization

of the apparent violations may change as a result of further NRC review.

Accordingly, no response to these matters is required at this time.

Additionally, we consider a violation concerning failure to collect grab

samples of the waste gas decay tank a non-cited issue since the item conforms

with our enforcement policy as described in 10 CFR Part 2, Appendix C, Section

VII.

The details of all of these matters are described in the enclosed

inspection report .

. These apparent violations (as described in the enclosure) were discussed

between Mr. John Summers, General Manager, Salem Operations and Mr. John White

of our office on April 7, 1995.

An Enforcement Conference will be scheduled

with your organization in the near future. This conference will be closed to

public observation .

~ ""~ r. r, ' "

  • til,:ull

9504170012 950407

PDR

ADOCK 05000272

Q

PDR

-**

Mr .. Leon R. Eli as on

2

The decision to hold an Enforcement Conference does not mean that violati~ns

have occurred, or that enforcement action will be taken.

The purposes of this

conference are: (1) to discuss the apparent violations, including cause and

safety significance; (2) to provide you with an opportunity to point out

errors in our inspection report, and identify corrective actions, taken or

planned; and (3) to discuss any other information that will help us determine

the appropriate action in accordance with the Enforcement Policy.

The

conference is also an opportunity for you to provide any information

concerning your perspectives on the severity of the apparent violations, and

the application of the factors that the NRC considers when it determines the

amount of a civil penalty that may be assessed in accordance with Section

VI.B.2 of the Enforcement Policy.

Your cooperation with us is appreciated.

Sincerely,

ORIGINAL SIGNED BY:

Wayne Lanning for

R1cnard W. Cooper, Director

Division of Reactor Projects

Docket Nos.

50-272; 50-311

Enclosures:

1. Apparent Violations

2.

NRC Inspection Report Nos. 50-272/95-02; 50-311/95-02

cc w/encl:

J. J. Hagan, Vice President-Operations

S. LaBruna, Vice President - Engineering and Plant Betterment

C. Schaefer, External Operations - Nuclear, Delmarva Power & Light Co.

P. J. Curham, Manager, Joint Generation Department,

Atlantic Electric Company

R. Burricelli, General Manager - Information Systems & External Affairs

J. Summers, General Manager-Salem Operations

J. Benjamin, Director of Quality Assurance and Safety Review

F. Thomson, Manager - Licensing and Regulation

R. Kankus, Joint Owner Affairs

A. C. Tapert, Program Administrator

R. Fryling, Jr., Esquire

M. J. Wetterhahn, Esquire

Consumer Advocate, Office of Consumer Advocate

William Conklin, Public Safety Consultant, Lower Alloways Creek Township

Public Service Commission of Maryland

D. Screnci, PAO (2)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of New Jersey

State of Delaware

.

.

Mr .. Leon R. Eliason

3

Distribution w/encl:

Region I Docket Koom (with concurrences)

K. Gal 1 agher

E. Kelly, DRS (section 4.6 and 4.8)

PUBLIC

Distribution w/encl: (Via E-Mail)

L. Olshan, NRR

W. Dean, OEDO

J. Stolz, PDl-2, NRR

M. Callahan, OCA

Inspection Program Branch, NRR (IPAS)

J. Lieberman, OE

D. Holody, EO,RI

py without attachmentf enclosure 'E" = Copy with

I

ENCLOSURE 1

~PPARENT VIOLATIONS

A.

10 CFR 50 Appendix B Criterion V, "Instructions, Procedures, and

Drawings", requires that measures to ensure activities affecting safety

are satisfactorily accomplished.

The following example of a failure to

meet this requirement occurred in May 1993:

B.

During a modification to install a drain system for the Salem Unit 2

pressurizer code safety loop seals, the licensee did not adequately

ensure that the drain valves were properly positioned prior to plant

startup after the modification. Specifically, valve 2PR66, a valve in a

common drain line for the 2PR3, 2PR4, and 2PR5, pressurizer safety

valves, was left closed throughout the operating cycle between May 1993

and October 1994.

As a result, the licensee operated Salem Unit 2 in

that period with the loop seals filled with water.

No analysis was

performed to assess the effect of filled loop seals on the discharge

piping or on system operability. Subsequently, in an effort to

demonstrate that thrust loading from the water in the loop seals would

not damage safety valve discharge piping sufficiently to prevent the

pressurizer code safety valves from limiting Reactor Coolant System

pressure, the licensee initiated a detailed engineering calculation,

scheduled for completion in April 1995.

10 CFR 50, Appendix B, Criterion XVI "Corrective Action", requires in

part, that licensees identify significant conditions adverse to quality,

determine their causes, and take corrective action to preclude

recurrence. Three examples of failure to meet this requirement

occurred:

1)

On June 7, 1994, the licensee identified that material management

documentation for limit switches related to the reactor head vent

valves, improperly classified the components as non-safety

related. A nuclear design discrepancy evaluation form (DEF)

identified that a switch short circuit could render two head vent

valves inoperable since the components were powered from the same

common circuit. Notwithstanding, the DEF did not identify any

concern relative to operability or safety. The reviewers

determined that switches obtained as safety-related or non-safety

related were essentially the same part, with the exception that

the qualified part is certified by testing.

2)

It was not until February 1995, that the licensee determined that

non-safety related limit switches were installed in reactor head

vent valves 1RC41 and 1RC43 at Salem Unit 1. Subsequently, the

licensee failed to perform and document an engineering evaluation

to demonstrate the acceptability of continued Salem Unit 1

operation with non-safety-related parts installed in a safety-

related application.

On February 24, 1995, at 8:58 p.m. Unit No. 1 operators placed

control of a Power Operated Relief Valve (PORV) in the manual

mode, rendering it inoperable, and failed to adhere to the

3)

2

Technical Specification 3.4.3 action statement which required

operators to close the block valve within one hour. A shift

supervisor discovered the error and corrected it on February 25;

1995 at 7:10 p.m. (about 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br /> later). This performance error

is similar to a violation of the same technical specification

requirement involving on Salem Unit No. 2 on March 24, 1994.

The

licensee's corrective actions for the previous occurrence appear

to have been ineffective in preventing recurrence of this type of

performance deficiency.

On July 6, 1994, safety-related reactor head vent valve 2RC40

failed to operate (stroke open) during testing while Unit No. 2

was in cold shutdown. Subsequently, the licensee speculated that

the low reactor coolant system temperature which may have promoted

boric acid crystallization that adversely affected valve

operation, and later confirmed function of the valve when RCS

temperature was increased. Subsequently, the valve was returned

to normal service on July 10, 1994, without any review or

assessment in accordance with established procedures.

In this

case, the licensee failed to process this occurrence in accordance

with the applicable "Work Control Process" procedure.

Consequently, this failure of a safety-related component was never

documented and formally assessed relative to preventive

maintenance, operability, actions to prevent recurrence, or

generic implications .

3)

2

Technical Spec}fication 3.4.3 action statement which required

operators to close the block valve within one hour. A shift

supervisor discovered the error and corrected it on February 25,

1995 at 7:10 p.m. (about 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br /> later). This performance error

is similar to a violation of the same technical specification

requirement involving on Salem Unit No. 2 on March 24, 1994. * The

licensee's corrective actions for the previous occurrence appear

to have been ineffective in preventing recurrence of this type of

performance deficiency.

On .July 6, 1994, safety-related reactor head vent valve 2RC40

failed to operate (stroke open) during testing while Unit No. 2

was in cold shutdown.

Subsequently, the licensee speculated that

the low reactor coolant system temperature which may have promoted

boric acid crystallization that adversely affected valve

operation, and later confirmed function of the valve when RCS

temperature was increased. Subsequently, the valve was returned

to normal service on July 10, 1994, without any review or

assessment in accordance with established procedures.

In tr.~s

case, the licensee failed to process this occurrence in accordance

with the applicable "Work Control Process" procedure.

Consequently, this failure of a safety-related component was never

documented and formally assessed relative to preventive

maintenance, operability, actions to prevent recurrence, or

generic implications .