ML18101A219

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Insp Repts 50-272/94-18,50-311/94-18 & 50-354/94-18 on 940808-12 & 940818-22.Violations Noted.Major Areas Inspected:Licensee Corrective Actions of Previously Identified Edsfi Findings & Rod Control Process Methods
ML18101A219
Person / Time
Site: Salem, Hope Creek  
Issue date: 09/07/1994
From: Ruland W, Richard Skokowski
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18101A217 List:
References
50-272-94-18, 50-311-94-18, 50-354-94-18, NUDOCS 9409130298
Download: ML18101A219 (16)


See also: IR 05000272/1994018

Text

DOCKET/REPORT NOS:

LICENSEE:

FACILITY:

INSPECTION AT:

DATES:

SUBMITTED BY:

APPROVED BY:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/94-18

50-311/94-18

50-354/94-18

Public Service Electric and Gas Company

Salem 1 & 2 and Hope Creek Generating Stations

Hancocks Bridge, New Jersey 08038

Hancocks Bridge, New Jersey

August 8 - 12 and 18 - 22, 1994

RiCarA.so owskl;ReictorEngi neer

Electrical Section

Division of Reactor Safety

'f Se:or 94

Date

c;-7-9j

Date

Area Inspected: This was an announced inspection to review the licensee's

corrective actions of previously identified electrical .distribution system

functional inspection (EDSFI) findings.

Additionally, evaluations of the troubleshooting of the rod control process

signal noise at both Salem Units and the load fluctuations on the Salem IA

emergency diesel generator (EOG) identified during surveillance testing on

August 16, 1994, were performed~

Results: During this inspection, two previously identified deviations and one

unresolved item at Hope Creek and three unresolved items at both the Salem

Units were review and closed. The inspector considered the engineering

evaluation, associated with the potential failure of the Salem rod control

motor generator set flywheels, to be technically sound.

The acceptance criterion for the Hope Creek 125V battery service test was

found to be inadequate.

The same issue was identified by the inspector for

the 125V battery service tests at both Salem Units. These examples of

inadequate test acceptance criteria were considered a violation of 10 CFR 50

Appendix B, Criterion XI, "Test Control." The violation is of concern because

the acceptance criteria for the 125V battery service test at Hope Creek and

Salem Units 1 and 2 were inadequate to assure the functionality of safety-

related equipment. Specifically, the acceptance criteria provided in the test

procedures were not consistent with design documents and were not

9409130298 940907

PDR

ADOCK 05000272

G

PDR

conservative. The inadequate acceptance criterion was identified as an

unresolved item at Hope Creek by the EDSFI in early 1992.

However, the

engineering staff failed to adequately address a similar problem with the

Salem test procedures.

The inspector concluded that when the PSE&G maintenance staff started around-

the-clock troubleshooting of the rod control process signal noise, the

troubleshooting was methodical and thorough. Additionally, the

troubleshooting associated with the EOG load fluctuations was found to be

adequate. The root cause analysis for the identified EDG component failures

was not completed at the conclusion of this inspection and was identified as

an unresolved item.

The inspector considered the independent review of the design change packages

for the upcoming refueling outage at Salem Unit 2, to be noteworthy, in that

it provided the licensee a chance to re-review packages that were prepared in

advance.

The inspector considered the changes to the

11 Engineering Assurance Self-

Assessment Process

11 procedure, and the use of team leader training for

collegial self-assessment team leaders to be good.

ii

DETAILS

1.0

PURPOSE

This inspection reviewed actions taken to address previously identified

electrical distribution system functional inspection (EDSFI) unresolved items.

In addition, this inspection evaluated the effectiveness of the root cause

investigations initiated in response to apparent malfunctions of the Salem

automatic rod control systems and the Salem IA emergency diesel generator

(EDG).

2.0

FOLLOWUP OF PREVIOUS IDENTIFIED FINDINGS (2515/111)

2.1

Salem Units 1 and 2

Three previously identified unresolved items were reviewed for both Salem

Units.

2.1.1 (Closed) Unresolved Item (50-272;311/93-82-03) EOG Output Voltage Below

Allowable Degraded Voltage

The EDSFI team identified that the EDG surveillance test procedures for both

Salem Units and the Unit 2 Technical Specification {TS) allowed the EDG to be

operated at a steady-state voltage lower than the degraded voltage setpoint.

The degraded voltage setpoint was established to ensure that adequate voltage

would be available to required electrical equipment.

Additionally, the EDSFI

team noted that there was no specified limit on EDG running voltage in the

Unit 1 TS.

The inspector verified that Public Service Electric and Gas Company (PSE&G)

completed the corrective actions described in their response letter to the

NRC, NLR-N94013, dated February 7, 1994, regarding the EDSFI findings.

The

corrective actions included:

changing the Unit 2 minimum steady state EDG voltage Technical

Specification surveillance requirement to greater than or equal to

3950V;

adding a Technical Specification requiring Unit 1 minimum steady state

EDG voltage to be greater than or equal to 3950V; and

revising the appropriate surveillance procedures to reflect this minimum

required value for steady state EDG voltage.

The inspector found the licensee's actions appropriate and considered this

item closed .

2

2.1.2 (Closed) Unresolved Item (50-272;311/93-82-11) Potential Damage of Vital

Buses from a Failure of a Rod Control Motor-Generator Set Flywheel

The EDSFI team identified a concern regarding the potential damage to safety-

rel ated vital buses from a failure of the rod control motor-generator {MG) set

flywheels.

These MG sets are classified as nonsafety-related.

The concern

was that the disintegration of the flywheel could damage 4kV vital buses.

PSE&G developed Engineering Evaluation S-C-RCS-SEE-0866,

11 Rod Control System

MG Set Flywheel Failure,

11 January I2, I994, to determine the potential of a

failure of the Rod Control MG Set flywheel. This evaluation concluded that a

failure of the flywheel could damage both vital buses A and B.

However, the

evaluation determined that the flywheel disintegration was not credible. This

determination was based on information provided by Westinghouse, that the

flywheels, which were design-procured and fabricated under closely controlled

quality standards, have such a high degree of structural integrity that a

postulated failure was not credible.

The inspector reviewed the associated engineering evaluation and determined

that it was technically sound.

The evaluation used a methodology similar to

that used in Regulatory Guide 1.14, "Reactor Coolant Pump Flywheel Integrity,

11

to determine the integrity of the rod control MG set flywheels.

Additionally,

the evaluation stated that there has never been a reported Westinghouse

nuclear unit MG set flywheel structure failure.

The engineering evaluation

also stated that the flywheels are enclosed by steel casings and that there

are marinite board barriers between the MG sets and the vital buses.

These

barriers would deflect any missiles generated by the postulated flywheel

failure.

The inspector performed a walkdown on the MG sets and surrounding

area and verified the installation of these barriers.

The inspector determined this engineering evaluation to be technically sound.

Unresolved Item 50-272;3Il/93-82-1I is considered closed.

2.1.3 (Update) Unresolved Item (50-272;311/93-82-15) Potential High

Temperature Aging of Vital Batteries lC and 2C

The EDSFI team identified that the IC and 2C batteries may have experienced

accelerated aging due to high ambient battery room temperatures.

The EDSFI

noted that surveillance test data indicated that the IC and 2C batteries had

operated with ambient room temperatures ranging from 70°F to 96°F.

The other

station vital batteries normally were within a three or four degrees band of

the nominal operating temperature of 77°F.

The team also noted other

indications of potential accelerated aging of the IC battery, such as an

abnormal operating characteristic, the failure of Cell No. 47 and the build up

of sediment in the jar bottoms of several IC battery cells.

To address this issue, PSE&G replaced the IC battery in April I994.

The

battery vendor perform a root cause analysis of the failed cell.

In addition,

PSE&G performed a review of the battery surveillance test temperatures and

evaluated the impact of these temperatures on the aging of batteries IC and

3

2C.

The results of this evaluation were provided to the NRC in a May 7, 1994,

letter from PSE&G regarding the EDSFI findings, and concluded that the 2C

battery did not need to be replaced at this time.

This evaluation stated that according to the vendor, that the operation of the

batteries in an increased temperature will decrease the life expectancy of the

battery cells. The vendor stated that for every l8°F above 77°F will decrease

the battery life by 50%.

However, the increased temperature does not increase

the potential for a sudden catastrophic battery failure.

PSE&G also stated

that the existing surveillance program adequately monitors the battery status.

Therefore, any degradation of the battery life due to varying temperatures

will be detected before it leads to battery failure.

The inspector performed a walkdown of the battery rooms and reviewed the

vendor's information and determined that it was consistent with PSE&G's

evaluation.

The inspector also reviewed the battery performance test and

service test procedures. These tests were found to be performed in accordance

with the guidance provided in the Institute of Electrical and Electronics

Engineers (IEEE) Standard 450-1987, "IEEE Recommended Practice for

Maintenance, Testing and Replacement of Large Lead Storage Batteries for

Generating Stations and Substations." However, the acceptance criterion for

the service test was found to be inadequate.

Prior to the completion of this

inspection, PSE&G took actions to ensure the proper acceptance criterion was

reflected in the procedures. This issue is described in Section 2.1.4 of this

report.

The written root cause analysis for the failed lC Battery Cell No. 47 had not

been provided to PSE&G at the conclusion of this inspection.

However, the

battery vendor had verbally informed PSE&G of the analysis results.

PSE&G

stated that the root cause was determined to be a random failure that allowed

for an internal plate-to-plate short-circuit. This failure caused the cell to

become degraded, but testing performed by both the licens.ee and the vendor

indicated that it was not a complete failure of the cell.

Based on the conclusion of PSE&G's evaluation that the high ambient

temperatures do not increase the potential for a sudden catastrophic battery

failure, and PSE&G's actions to correct the 125V battery service test

acceptance criteria to ensure the detection of degradation of battery life,

the inspector considered Unresolved Item 50-272;311/93-82-15 closed.

2.1.4 Inadequate Acceptance Criteria for the Battery Service Test

The inspector identified that the acceptance criterion established in

Procedure SC.MD-ST.125-0004(Q), "125 Volt Station Batteries 18 Month Service

Test and Associated Surveillance Testing using BCT-2000," Revision 3, was

inadequate.

The acceptance criterion of 105V did not appropriately include

the voltage drop between the battery terminals and the attached safety-related

equipment.

Based on the PSE&G Calculation ES-4.003Q, "125V VDC System Study,"

the acceptance criteria should have been 113.4V for the "A" batteries and

112.8V for the "B" and "C" batteries. Service test results less than the

voltages determined by the calculation indicate that the battery would not be

capable of supplying the necessary voltage to assure safety-related equipment

4

functionality required for accident mitigation. The inspector verified that

the results of the last service test for each battery indicated a voltage

level greater than the newly determined acceptance criteria.

PSE&G developed

a procedure change request to address this issue, requiring that the

procedures be changed prior to the next use.

Battery testing was not reviewed

during the Salem EDSFI.

However, this issue was identified as an unresolved

item during the Hope Creek Station EDSFI in I992.

The Hope Creek issue is

described in Section 2.2.1 of this report.

The inadequate acceptance criteria for the I25V service testing is considered

a violation of IO CFR 50 Appendix B, Criterion XI, "Test Control," (50-

272;3Il/94-I8-0I). This violation will be combined with the same issue

identified at Hope Creek Generating Station (HCGS) as described in Section

2.2.I of this report.

The technical issues associated with this violation are

complete; however, there still is a concern in that the item was identified at

Hope Creek during the EDSFI in early 1992, but was not addressed in the Salem

Station procedures.

2.2

Hope Creek

Two previously identified deviations and one previously identified unresolved

item for Hope Creek Generating Station.were reviewed.

2.2.1 (Closed) Unresolved Item (50-354/92-80-04) Inadequate Battery Service

Testing Acceptance Criteria.

The EDSFI team identified a concern regarding the adequacy of the 125V and

250V de battery service test acceptance criteria as stated in both the TS and

surveillance procedures.

The acceptance criteria failed to include the cable

voltage drop.

PSE&G revised the associated voltage drop calculations to include the cable

voltage drop, and to determine the appropriate service test acceptance

criteria.

PSE&G determined that the previously identified acceptance

criterion of 2IOV was acceptable for the 250V batteries. However, PSE&G

determined that the previously identified acceptance criterion of lOSV for the

I25V batteries was inadequate to assure the functionality of safety-related

equipment.

PSE&G determined the appropriate acceptance criterion to be 108V.

On March 3, I994, this new acceptance criterion was incorporated in the

appropriate surveillance test, HC.IC-ST.PK-0002(Q), "I8 month surveillance &

service test of the I25 Volt Batteries Using BCT-2000."

PSE&G was also

preparing a license amendment request to change the associated TS surveillance

test acceptance criterion.

Through discussions with PSE&G staff members and a sample review of

Calculations E-4.2(Q), Revision 3, "Hope Creek Generating Station IE DC

Equipment & Component Voltage Study," and E-4.2(Q), Revision 3, "Hope Creek

Generating Station I25V & 250V CL IE DC System:

Short Circuit & Voltage Drop

Studies," the inspector verified the acceptance criteria for both the I25V and

250V batteries .

5

The inspector also reviewed Procedure HC.IC-ST.PK-0002(Q), Revision 1,

11 18

month surveillance & service test of the 125 Volt Batteries Using BCT-2000,"

approved March 18, 1994. This procedure included the acceptance criterion of

108V.

Based on the inspectors review, and PSE&G's commitment to complete the

associated license amendment request, Unresolved Item 50-354/92-80-04 is

considered closed. However, the inadequate acceptance criterion for the 125V

service testing is considered a violation of 10 CFR 50 Appendix B, Criterion

XI, "Test Control," (50-354/94-18-01).

This violation will be combined with

the same issue identifi.ed at Salem Generating Station as described in Section

2.1.4 of this report.

The technical issues associated with this violation are

complete; however, there still is a concern in that the item was identified at

Hope Creek during the EDSFI in early 1992, but a similar deficiency was not

addressed in the Salem Station procedures.

2.2.2 (Closed) Deviation (50-354/92-80-05) EDG Fuel Oil Storage was Not

Consistent With Seven Day Updated Final Safety Analysis Report (UFSAR)

Cammi tment

The EDSFI team identified that each dedicated EDG fuel reserve could not

independently sustain seven days of worst-case EDG operation, as described in

Section 9.5.4 of the UFSAR.

Section 9.5.4 of the UFSAR stated that "each set

of storage tanks can store a quantity of diesel fuel oil that is sufficient

for 7 days of continuous operation of one EDG unit under rated operating loads

as described in EDG loading Tables 8.3-2 through 8.3-6.

11

The EDSFI team's

review of applicable calculations indicated a shortage of 5579 gallons to meet

the seven-day commitment of 151,979 gallons when three EDGs were operating

(assuming one EDG inoperable).

-

The inspector reviewed the licensee's responses to this deviation as provided

in letters to the NRC dated July 10, 1992 and November 19, 1992.

In their

initial response, PSE&G indicated that they would review and revise their

UFSAR loads tables to demonstrate that there was sufficient fuel oil to power

the required loads for seven days following the worst case conditions.

In

their second response to this deviation, PSE&G indicated that revising the

UFSAR load tables would limit the operators' ability to load nonsafety-related

loads on the EDGs in accordance with the current emergency operating

procedures (EOPs).

PSE&G determined that there were more safety benefits for

leaving the operators with the ability to load nonsafety-related loads on the

EDGs.

Therefore, PSE&G requested that*the NRC provide relief from their HCGS

UFSAR commitment to the Standard Review Plan, Section 9.5.4.

The relief from this UFSAR commitment was made in the form of a license

amendment request, dated December 23, 1993.

A license amendment was required

because the change involved an unreviewed safety questions as identified by

the licensee. This license amendment request was reviewed by the Office of

Nuclear Reactor Regulation (NRR) staff and found acceptable as documented in

the Safety Evaluation related to Amendment Number 59 to facility Operating

License Number NPF-57.

6

The bases for PSE&G's license amendment was that since the quantity of fuel

oil was only a concern in the case where one EDG is not available, the fuel

oil from the two storage tanks associated with the inoperable EDG could be

used to ensure an adequate fuel oil supply. Since the fuel oil cross-tie

lines are designed as non-seismic Category I, Quality Group D, the licensee

proposed to pre-stage equipment necessary to maintain fuel oil transfer

capability should the fuel oil cross-tie lines not be available following an

accident. Additionally, procedures were to be in place for the transferring

fuel between fuel oil storage tanks when the cross-tie lines are intact ..

The inspector verified a selected sample of items addressed in the Safety

Evaluation. This included a walkdown of the pre-staged fuel transfer

equipment and storage tanks, a review of the related procedures and

discussions with members of the HCGS operating staff. These items were found

to meet the intent of the Safety Evaluation.

During the_walkdown of the pre-staged fuel transfer equipment and subsequent

discussions with the Hope Creek Operation Management, the inspector noted that

the ends of the pre-staged hoses were not sealed to prevent the introduction

of dirt.

HCGS Operation Management stated that they will address this issue.

Also noted was that the pre-staged fuel oil transfer pump was used by the

operating staff to transfer other fuel oil. This operation, while not

considered scheduled testing, did provide some periodic assurance of the

ability of the pump to work.

The PSE&G licensing staff stated that the proposed UFSAR changes associated

with this deviation were currently scheduled to be included in the Spring 1996

UFSAR revision.

The corrective actions taken were appropriate and Item 50-

354/92-80-05 is closed.

2.2.3 (Closed) Deviation (50-354/92-80-06) EOG Day Tank Does not meet UFSAR

Conunitment

'

The EDSFI team identified that the EDG tank fuel oil capacity was not

consistent with the Hope Creek UFSAR.

Paragraphs 9.5.4.2 and 1.8.1.137

described that the EDG fuel oil storage system was sized in accordance with

the requirements of Regulatory Guide 1.137, "Fuel-Oil Systems for Standby

Diesel Generators," Revision 1, which in turns refers to American National

Standards Institute (ANSI} Standard Nl95-1976.

This standard requires the day

tank for each EOG to be sufficient to maintain at least 60 minutes of EOG

operation at the level where fuel oil is automatically added.

This capacity

is based on the fuel consumption at a load of 100% of continuous rating of the

diesel plus a minimum margin of 10%.

At the time of the EDSFI, the licensee

estimated the day tank capacities to be about 47 minutes.

The inspector reviewed the licensee's responses to this deviation as provided

in letters to the NRC dated July 10, 1992 and November 19, 1992.

In their

initial response, PSE&G indicated that.they would be to revise the start

setpoint of the EDG fuel oil transfer pump to meet the requirements of ANSI

Standard Nl95-1976, and.submit a change to the TS to revise the minimum fuel

oil day tank level to correspond to the revised setpoint.

In their second

response to this deviation, PSE&G indicated that revising the start setpoint

7

of the EDG fuel oil transfer pump to meet the requirements of the ANSI

Standard would increase the cycling of the transfer pump seven times and

increase the probability of pump motor failure. Therefore, PSE&G requested

that the NRC provide relief from their commitment to Regulatory Guide 1.137 as

stated in HCGS UFSAR Section 1.8.1.137. The revised HCGS UFSAR would take

exception to Regulatory Guide 1.137 and provide administrative controls to

ensure that the EDG day tanks were adequately filled following the operation

of an EDG.

Additionally, the fuel oil transfer pump start setpoint was

increase to a level that provides approximately 55 to 60 minutes of EDG

operation at full load.

The relief from this UFSAR commitment was made in the form of a license

amendment request, dated December 23, 1993. A license amendment was required

because the lic~nsee determined that the change involved an unreviewed safety

questions. This license amendment request was accepted by the NRR staff as

documented in Amendment Number 59 Safety Evaluation.

The inspector verified a selected sample of items addressed in the Safety

Evaluation.

This included a walkdown of the EDGs and the associated day

tanks, a review of fuel consumption calculations, a review of the fuel oil

transfer pump starting relay calibration and a review of the EDG day tanks

levels from July 1, 1994 to August 10, 1994.

The information reviewed was

determined to be consistent with the Safety Evaluation.

Discussions with the PSE&G licensing staff indicated that the proposed UFSAR

changes associated with this deviation were scheduled to be incorporated in

the Spring 1996 UFSAR revision. Additionally, the TS change associated with

the EOG fuel oil transfer pump start setpoint was submitted to NRR on

April 25, 1994.

The inspector concluded that the licensee actions to address

the deviation were acceptable and Item 50-354/92-80-06 is closed.

3.0

TROUBLESHOOTING - SALEM GENERATING STATION (92903)

3.1

Rod Cont~ol Process Signal Noise - Salem Units 1 and 2

The inspector assessed various aspects of PSE&G's troubleshooting of the rod

control process signal noise.

Background

On May 30, 1994, PSE&G started troubleshooting a problem at Unit 2 with the

automatic rod control system.

The problem was that the control rods would

step in half steps without appropriate process demand signals. The trouble

shooting continued off and on, due to various plant shutdowns and work

priorities, until August 1, 1994.

On August 1, 1994, around-the-clock

monitoring and troubleshooting began.

This troubleshooting identified noised

on the average temperature (Tav.} and nuclear instrument (NI} signals to rod

control.

On August 8, 1994, by Plant Manager request, a Task Force was

developed to address the concerns with rod control process signal noise.

The

goal of this task force was to understand if the noise from Tave and Nis was

expected, and what should be done to address it.

8

Task Force

Until the development of the task force, the maintenance department was the

only organization involved with the troubleshooting.

The PSE&G staff

justified this by stating that the maintenance department needed to gain an

understanding of the problem, and an opportunity to correct the problem before

getting outside assistance. With the development of the task force,

engineering and vendor support was provided.

The inspector attended* the task force daily meeting on August 14, 1994, and

held discussions with members of PSE&G regarding the troubleshooting. Through

these discussions, the inspector ascertained the following information:

Even though the troubleshooting started May 30, 1994, the maintenance

department determined, through discussions with the operation staff,

that rods have been half stepping for approximately nine years in both

units.

Both units went to low leakage cores approximately nine years ago.

The

low leakage core caused the NI signal to be cut in half, while the noise

level stayed the same.

Therefore, twice as much noise for the same

signal was being transferred to rod control.

The licensee stated that

this noise could be enough to cause rod movement.

Westinghouse provided PSE&G with information about other utilities

experiencing similar noise problems and the possible solutions to these

noise problems.

Troubleshooting

During the troubleshooting, both units were instrumented to gain information.

This troubleshooting and monitoring provided PSE&G with information

specifically for the rod control process signal concern, and also allowed for

the identification of several hardware deficiencies.

With respect to the rod control process signal concern, PSE&G determined the

following:

Since the plants operate with the control bank control rods fully

withdrawn, all rod motion observed was in the "IN" direction. However,

the information gained through monitoring, revealed that there was

enough noise to exceed the designed threshold to cause outward rod

motion on both units.

Noise was observed on both the Tave and NI signals to the rod control

compensated temperature error summator.

The combination of noise on

these signals .created spikes that exceeded the threshold required for

rod movement.

  • ,

9

The Tave/Terr (temperature error) calibration tolerances prevented inward

rod motion at Unit 1, but noise did exist, and if not for these

calibration tolerances, inward rod motion would have occurred at Unit 1.

The root cause analysis associated with the Tave and NI noise will be addressed

by PSE&G in a root cause analysis report. This report was not completed by

the conclusion of this inspection.

In addition, during troubleshooting activities, PSE&G identified the following

hardware problems:

double grounds on shielded cables;

Unit 1, recorder switch and Tave defeat switch relay operation resulting

in signal spiking;

Unit 1, nuclear instrument N41 signal spiking; and

Unit 1, loose pin

11M

11 on summator module QM412J.

The licensee stated that these hardware problems would be addressed by

individual work orders. The inspector was concerned with the proposed cause

of the rod movement on Unit 1, August 16, 1994, which was determined to be the

loose pin on summator module QM412J.

PSE&G was able to recreate the event by

manipulating a wire in series with the pin.

Conclusion

The inspector concluded that when the PSE&G maintenance staff started around-

the-clock troubleshooting of the rod control process signal noise, the

troubleshooting was methodical and thorough.

3.2

Load Fluctuations on

EOG lA - Salem Unit 1

On August 16, 1994, during the monthly surveillance run of the Salem IA EDG

the operator noticed approximately lOOkW load fluctuations from the target

value of 2600kW.

The review of this event was described in NRC Inspection

Report 50-272/94-19.

The subsequent troubleshooting performed by PSE&G was

evaluated during this inspectidn.

Troubleshooting performed by the Salem Technical Department on

August 16, 1994, indicated a malfunction in the load control feature for the

electrical portion of the governor controller (EGA).

The load control feature

of the EGA is only used during parallel operations of the EOG.

When the EDG

is in stand alone operation, as it would be during a loss of offsite power,

the speed control feature is utilized. During the troubleshooting on

August 16, 1994, the Technical Department verified that the speed control

feature operated properly. Therefore, the EDG was considered operable.

However, the malfunction in the load control feature still needed to be

corrected.

After discussing the indications with the governor vendor, PSE&G decided to

IO

perform a realignment of both the electrical (EGA) and mechanical (EGB)

portions of the governor controller.

On August 2I, I994, during this governor

realignment, PSE&G determined that the EGA amplifier was the cause of the

malfunction.

PSE&G replaced the EGA and completed an alignment of both the

EGA and EGB.

Later the same day, during testing of the newly installed EGA, PSE&G

experienced unexpected responses to load changes on the IA EOG.

Subsequent

troubleshooting identified some individual fuel injection pump racks sticking

and potential damage to the EGB.

The root cause analysis for the identified

problems was not complete at the conclusion of this inspection.

The inspector noted that the EGA amplifier is shared by both the load control

and speed control features.

The system engineer stated that the amplifier

malfunction did not appear to have an adverse effect on the speed control

function of the EGA, but the impact of the amplifier malfunction on the speed

control feature and the initial operability decision was being reviewed.

Following the conclusion of this inspection, PSE&G completed the repairs to

the IA EOG including the replacement of the EGB and required alignment, and a

lubrication of the fuel rack.

Post maintenance testing was performed

satisfactorily and the EDG IA was declared operable on August 23, I994.

Additionally, PSE&G had initiated actions to address the sticking fuel racks

including:

enhancing the procedures to include instructions to manipulate the

individual fuel racks to inspect for binding;

evaluating the lubricating oil used to lube the fuel racks;

planning an inspection of the individual fuel pump eccentric adjustment

lever pin connections for excess tightness that could have contributed

to the severity of the lack-of-lube binding; and

evaluating the remaining five EOGs for previous fuel injection rack

binding occurrences.

Through discussions with the system engineers, and a review of the

troubleshooting results, the inspector considered the troubleshooting

methodology adequate. This item will remain unresolved until the completion

of the licensee's root cause analysis for the identified failures and

subsequent NRC review (50-272/94-IS-02).

4.0

MANAGEMENT OVERSIGHT AND SELF-ASSESSMENT

The inspector assessed two areas associated with the management oversight and

self-assessment of the engineering organization.

The areas reviewed were:

the licensee's independent review of Salem Unit 2, Refueling Outage No. 8,

design changes; and the recent changes to the engineering assurance and self-

assessment process.

11

4.1

Independent Review of Salem Unit 2, Refueling Outage No. 8, Design

Changes

The inspector assessed PSE&G's initiative to perform independent reviews of

the issued design change packages (DCPs) for the upcoming 2R8 refueling outage

at Salem Unit 2.

The goal of these independent reviews, as stated in the

July 11, 1994, PSE&G internal memorandum from the Manager of Nuclear Engineer

Design (NED), was to ensure that the DCPs to be implemented during the

upcoming refueling outage meet the expectation of error-free designs.

These reviews began on July 25, 1994.

The review teams consisted of four to

six members of various disciplines and backgrounds. Action items identified

for each review are documented and maintained by the NED Manager.

Action item

responses are returned to the NED manager for tracking and closeout. The

PSE&G engineering staff stated that considerations were being made regarding

the need to compile and evaluate the findings of these reviews for future use.

The inspector attended a meeting to review DCP 2EC-3279, regarding the feed

pump pressure switch replacement.

The inspector found both the reviewers and

the presenters well prepared, allowing for a thorough review of the DCP.

The

emphasis of the review was placed on the installation and testing of the DCP.

In addition, several other areas were also addressed during this review,

including:

lessons learned from both industry and past PSE&G experience;

verification that no changes to the plant, since the issuance of the

DCP, adversely impact the DCP as designed;

operational impacts considered during the design; and

the first time application of any materials or technology.

The inspector determined that this was a strong engineering management

initiative to improve the quality of DCPs.

4.2

Engineering Assurance Self-Assessment Process

The inspector reviewed the revisions to the recently developed Procedure

ND.DE-PS.ZZ-0022(Z), "Engineering Assurance Self-Assessment Process" Revision

2, approved August 4, 1994.

The earlier revision of this procedure was

reviewed by the NRC in Combined Inspection Report 50-272/94-07; 50-311/94-07,

50-354/94-05. Since that inspection, PSE&G had completed their first two

collegial self-assessments.

Based on the lessons learned from those two

collegial assessments, PSE&G revised their procedure.

The inspector discussed the procedure revisions with the responsible PSE&G

staff member.

This discussion indicated that many of the procedure changes

~ere based on insight gained through a recently attended Team Leader Course.

The majority of the procedure changes focused on defining the responsibilities

of the Executive Sponsor, Team Leader, and Facilitator. Previously, the

12

functions of the Team Leader and the Facilitator were performed by the same

individual, this was determined to be less than ideal, and, therefore, was

changed.

These di.scussions also revealed that the scheduled team leaders for remainder

of the 1994 self-assessments have been to team leader training and that PSE&G

intends to have future team leaders trained.

The inspector considered the changes to the procedure positive enhancements

and the use of team leader training to be good.

5.0

UNRESOLVED ITEMS

Unresolved items are matters about which additional information is necessary

to determine whether they are acceptable, a deviation, or a violation.

Several unresolved items are discussed in detail under Sections 2.0, and 3.2.

6.0

EXIT MEETING

The inspector met with the licensee's personnel denoted in Attachment 1 of

this report at the conclusion of the first week of this inspection on

August 12, 1994, and then again at the conclusion of the inspection on

August 22, 1994.

The scope of the inspection and inspection results were

summarized during these meetings.

During these meetings, the licensee

acknowledged the inspection findings as detailed in this report. The.

commitment described in Section 2.2.1 of this report was confirmed during a

telephone call with Mr. F. Thomson, PSE&G's Licensing and Regulation Manager,

on August 23, 1994.

The technical contact for this report is Mr. Dave Smith.

The inspectors received no proprietary material during this inspection.

Attachment:

Persons Contacted

..

ATTACHMENT 1

PERSONS CONTACTED

Public Service Electric and Gas Companv

C. Atkinson

J. Bailey

+*D. Beckwith

A. Bel 1

P. Benini

A. Blum

  • M. Burnstein

+*R. Chranowski

A. Cul 1 iton

G. Daves

S. Davies

D. Demarest

L. Dewolff

  • G. Englert

L. Hajos

B. Hamilton

F. Hughes

S. Johnson

K. Kimmel

D. Kolasinski

  • C. Lambert
  • E. Lawrence
  • C. Manges

L. Miceli

W. Mokoid

+ M. Morroni

+ G. Nagy

I. Owens

+ K. Petroff

J. Reistle

+*J. Rucki

  • M. Quadin

R. Sandy

J. Shank

  • D. Smith

D. Smith

K. Soumi

F. Thomson

H. Trenka

Instrumentation & Controls Supervisor, Hope Creek

Nuclear Engineering Science Manager

Station Licensing Engineer

Nuclear Electrical Engineer, E&PB

Principal Engineer, QA Audits

Principal Engineer, PAG

Manager, Nuclear Electrical Engineering

Electrical Technical Engineer, Salem

Standard and Assurance Supervisor

Acting Operation Manager, Hope Creek

System Engineer, Salem

Instrumentation & Controls Maintenance, Salem

Equipment Operator, Hope Creek

Nuclear Engineering Standards Manager

Acting Electrical Engineering Supervisor

Operations Engineer, Salem

Senior Shift Supervisor, Hope Creek

Technical Engineer, Salem

Senior Staff Engineer, Nuclear Engineering Standards

System Engineer, Salem

Manager, Nuclear Engineering Design

Senior Staff Engineer, QA

Licensing Engineer, Hope Creek

System Engineer, Salem

Maintenance Engineer, Controls, Salem Unit I

Maintenance Controls Manager, Salem

Maintenance Engineer, Controls, Salem Unit 2

Principal Engineer, Salem

System Engineer, Hope Creek

Instrumentation & Controls Maintenance, Salem

Technical Engineer, Hope Creek

Senior Project Engineer

Senior Project Engineer

.

Nuclear Electrical Engineer, E&PB

Principal Engineer, Nuclear Licensing

Engineer, Installation and Test

Senior Nuclear Maintenance Supervisor, Hope Creek

Manager, Li~ensing and Regulation

Senior Project Engineer

Attachment 1

2

U.S. Nuclear Regulatory Commission

S. Barber

Project Engineer, Section 2A, Region I

+ T. Fish

Resident Inspector, Salem

J. Laughlin

Acting Resident Inspector, Salem

c. Marschall

Senior Resident Inspector, Salem

+ S. Morris

Resident Inspector, Hope Creek

w. Ruland

Section Chief, Electrical Section, Region I

J. Schoppy

Resident Inspector, Salem

+ R. Summers

Senior Resident Inspector, Hope Creek

J. Trapp

Acting Section Chief, Electrical Section, Region

  • Denotes those present at the meeting on August 12, 1994.

+Denotes those present at the exit meeting on August 22, 1994.

I