ML18093B218

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Confirms 881014 Telephone Authorization to Revise Tech Spec Page 3/4 15a Re Alternate Insp Sampling Plan for Fourth Refueling Outage
ML18093B218
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/14/1988
From: Boger B
Office of Nuclear Reactor Regulation
To: Miltenberger S
Public Service Enterprise Group
References
NUDOCS 8810180369
Download: ML18093B218 (5)


Text

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October 14, 1988 Docket No. 50-311 Mr. Steven E. Miltenberger Vice President and Chief Nuclear Officer Public Service Electric & Gas Company Post Office Box 236 Hancocks Bridge, New Jersey 08038

Dear Mr. Miltenberger:

SUBJECT:

CONFIRMATION OF CHANGE TO TECHNICAL SPECIFICATIONS Re:

SALEM GENERATING STATION, UNIT 2 This confirms our telephone authorization given on October 14, 1988, for the change to the Technical Specifications for Salem Generating Station, Unit 2 as requested on an emergency basis in your letter dated October 10, 1988.

Facility Operating License DPR-75 is amended on October 14, 1988.

The revised Technical Specifications page 3/4 15a is enclosed.

The formal license amendment, our completed safety evaluation, and the Federal RegistJ;,?: Notice of this change to the Technical Specifications for Salem Generating Station, Unit 2 are being processed and copies of these documents will be sent to you in the near future.

Enclosures:

Technical Specification Page cc w/enclosures:

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UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 Docket No. 50-311 Mr. Steven E. Miltenberger Vice President and Chief Nuclear Officer Public Service Electric & Gas Company Post Office Box 236 Hancocks Bridge, New Jersey 08038

Dear Mr. Miltenberger:

October 14, 1988

SUBJECT:

CONFIRMATION OF CHANGE TO TECHNICAL SPECIFICATIONS Re:

SALEM GENERATING STATION, UNIT 2 This confirms our telephone authorization given on October 14, 1988, for the change to the Technical Specifications for Salem Generating Station, Unit 2 as requested on an emergency basis in your letter dated October 10, 1988.

Facility Operating License DPR-75 is amended on October 14, 1988.

The revised Technical Specifications page 3/4 15a is enclosed.

The formal license amendment, our completed safety evaluation, and the Federal Register Notice of this change to the Technical Specifications for Salem Generating Station, Unit 2 are being processed and copies of these documents will be sent to you in the near future.

Enclosures:

Technical Specification Page cc w/enclosures:

See next page Sincerely, Bruce A. Boger, Assistant Director for Region I Reactors Division of Reactor Projects I/II

~"1 J' Mr. Steven E. Miltenberger Public Service Electric & Gas Company cc:

Mark J. Wetterhahn, Esquire Conner and Wetterhahn Suite 1050 1747 Pennsylvania Avenue, NW Washington, QC 20006 Richard Fryling, Jr., Esquire Law Department - Tower 5E 80 Park Place Newark, NJ 07101 Mr. L. K. Miller General Manager - Salem Operations Salem Generating Station P.O. Box 236 Hancocks Bridge, NJ 08038 Mr. S. LaBruna Vice President - Nuclear Operations Nuclear Department P.O. Box 236 Hancocks Bridge, New Jersey 08038 Robert Traee, Mayor Lower Alloways Creek Township ft1unicipal Hall Hancocks Bridge, NJ OA038 Richard W. Borchardt, Resident Inspector Salem Nuclear Generating Station U.S. Nuclear Regulatory Commission Drawer I Hancocks Bridge, NJ 0~038 Richard F. Engel Deputy Attorney General Department of Law and Public Safety CN-112 State House Annex -

Trenton, NJ 08625 Mr. David M. Scott, Chief Bureau of Nuclear Engineering Department of Environmental Protection State of New Jersey CN 411 Trenton, NJ 08625 Salem Nuclear Generating Statio" Richard R. McGlynn, Commission Department of Public Utilities State of New Jersev 101 Commerce Street Newark, NJ 07102 Regional Administrator, Region I U. S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Lower Alloways Creek Township c/o Mary 0. Henderson, Clerk Municipal Building, P.O. Box 157 Hancocks Bridge, NJ 08038 Mr. Bruce A. Preston, Manager Licensing and Regulation Nuclear Department P.O. Box 236 Hancocks Bridge, NJ 08038 Mr. David Wersan Assistant Consumer Advocate Office of Consumer Advocate 1425 Strawberry Square Harrisburg, PA 17120 Morgan J. Morris, III General Manager - Operating License Atlantic Electric P.O. Box 1500 1199 Black Horse Pike Pleasantville, NJ 08232 Delmarva Power & Light Company_

c/o Jack Urban General Manager, Fuel Supply 800 King Street P.O. Box 231 Wilmington, DE 19899

REVISED PAGES -

UNIT NO. 2 TECHNICAL SPECIFICATIONS

ALTERNATE INSPECTION SAMPLING PLAN FOR SALEM UNIT 2 FOURTH REFUELING OUTAGE Durinq the Salem Unit 2 Fourth Refueling Outaqe, indications associated with wall degradation were detected on the tubing of the No. 22 and No. 24 Steam Generators.

The condition was established as occurring on the inside diameter of the Row 1 tubes in the tangential region of the u-bend.

The following alternate action may be taken in place of that required by Technical Specification Table 4.4-2 when the results of the initial sample requires that an additional sample or samples must be inspected and the condition for which the added inspection is required is limited to the Row 1 tubes.

When examination results fall into a C-2 or C-3 Supplemental Sample category, pursuant to Technical Specification Table 4.4-2 as a result of Row 1 and/or Row 2 u-bend defective or degraded tubes, additional samples may be limited to Rows 1 and 2.

The results of the examination of the Row 1 and Row 2 tubes will be exempt from the additional sampling requirements of Technical Specification Table 4.4-2.

This change applies to only those steam generator eddy current inspections performed during the Salem Unit 2 Fourth Refueling Outage.

SALEM - UNIT 2 3/4-lSa