05000311/LER-1980-030-03, /03L-0:on 800907,during Cold Shutdown,Both Safety Injection Pumps Were Made Operable at Same Time.Caused by Supervisor Error.Supervisor Counseled

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/03L-0:on 800907,during Cold Shutdown,Both Safety Injection Pumps Were Made Operable at Same Time.Caused by Supervisor Error.Supervisor Counseled
ML18082B329
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/06/1980
From: Randolph J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082B328 List:
References
LER-80-030-03L-01, LER-80-30-3L-1, NUDOCS 8010100348
Download: ML18082B329 (1)


LER-1980-030, /03L-0:on 800907,during Cold Shutdown,Both Safety Injection Pumps Were Made Operable at Same Time.Caused by Supervisor Error.Supervisor Counseled
Event date:
Report date:
3111980030R03 - NRC Website

text

NRC FORM 366 (7.,f-7-f CONTROL BLOCK: I 1

U.S. NUCLEAR REGULATORY COMMISSION e LICENSEE EVENT REPORT I IG) 6 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

C£:E] IN I J I s I G Is 12 l@I 0 I 0 I - I 0 I 0 I 0 I 0 I 0 I - I 0 I 0 101 4 I 1 I 1 I l I i 101 I I © 7

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LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T [ill]

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~~~~~~ Li.I© I ol 5 I o I o I o I 3 I i I 1 !(?)I o I 9 I o I 1 I ~ I o IG) I 1 I o I o 16 I a 60 61 DOCKET NUMBER 68 69 EVENT CATE 74 75 REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

Io IG) 80 I During a log review while in cold shutdown, it was discovered that both Safety Injection Pumps had been made operable at t:1e same time contrary to the Technical Specification 3.5.3 requirement that a maximum of one shall be operable when the RCS temperature is </= 312°F.

During the interval

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(approximately 25 minutes), both pumps were operable, the flow paths were

[))2J I inoperable due to closed discharge valves to the RCS.

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8 SYSTEM CODE js IF I@

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LEA/RO LVENT YEAR

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11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REPORT NO.

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ATTACHMENT NPR0-4 PRIME COMP.

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

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DJ)) I The supervisor released both pumps for service simultaneously, thereby giving o:::IIJ up the administrative control that he, as the responsible licensed operator, should have retained.

The supervisor was counseled about the error.

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NUMBER DESCRIPTION6 rr:fil I cl al ol@)':-'.:-_N=A..._ _______________________ ~

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9 11 12 LOSS OF OR DAMAGE TO FACILITY '4J'I TYPE

DESCRIPTION

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