05000311/LER-1980-024, Forwards LER 80-024/03L-0

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Forwards LER 80-024/03L-0
ML18082B036
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/28/1980
From: Librizzi F
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082B037 List:
References
NUDOCS 8009090447
Download: ML18082B036 (2)


LER-1980-024, Forwards LER 80-024/03L-0
Event date:
Report date:
3111980024R00 - NRC Website

text

~-c~~ PS~G*

Public Service Electric and Gas Company 80 Park Place Newark. N.J. 07101 Phone 201430-7000 Mr. Boyce H. Grier Director of USNRC August 28, 1980 Off ice of Inspection and Enforcement Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 80-24/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 80-24/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

);,,~

F. P. Librizzi General Manager -

Electric Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control

( 3 copies) 95-2001 1200~~) 2* 78

Report Number:

Report Date:

Occurrence Date:

00A/03L 0121'00 8/01/80 Facility:

Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancock's Bridge, New Jersey*

08038 IDENTIFICATION OF OCCURRENCE:

Rod Position Indication Inoperable CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 DESCRIPTION OF OCCURRENCE:

While withdrawing rods -in preparation for entering Mode 2, 1SC2 individual rod position indicator read 20 steps lower than the bank demand position.

Action Statement 3.1.3.2.2 was entered at 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br /> which requires that with a rod position indicator inoperable, immediately open the reactor trip breakers.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment Failure ANALYSIS OF OCCURRENCE:

When it was determined that the individual rod position indicator was reading inaccurately, the reactor trip breakers were opened.

CORRECTIVE ACTION

The individual rod position indicator meter movement was replaced with a spare.

The indicator was retested and returned to service~

The Action Statement was terminated at 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br />.

FAILURE DATA:

Not Applicable Prepared By R. J. Newman Manager -.Salem Gen~ating Station SORC Meeting No.

66-80