05000311/LER-1980-013-03, /03L-0:on 800714,during Routine tour,21 & 22CS6 Spray Header Isolation Valves Were Found Cleared & Tagged in Closed Position.Caused by Facilitation of Performance of Surveillance Test After Which Valves Were Not Repositioned

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/03L-0:on 800714,during Routine tour,21 & 22CS6 Spray Header Isolation Valves Were Found Cleared & Tagged in Closed Position.Caused by Facilitation of Performance of Surveillance Test After Which Valves Were Not Repositioned
ML18082A935
Person / Time
Site: Salem 
Issue date: 08/13/1980
From: Murphy M
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A929 List:
References
LER-80-013-03L-01, LER-80-13-3L-1, NUDOCS 8008190537
Download: ML18082A935 (1)


LER-1980-013, /03L-0:on 800714,during Routine tour,21 & 22CS6 Spray Header Isolation Valves Were Found Cleared & Tagged in Closed Position.Caused by Facilitation of Performance of Surveillance Test After Which Valves Were Not Repositioned
Event date:
Report date:
3111980013R03 - NRC Website

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((!I) I During a routine tour of the station, it was determined that 21 and 22CS6, Spray

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