05000311/LER-1980-011, Forwards LER 80-011/03L-0

From kanterella
(Redirected from ML18082A867)
Jump to navigation Jump to search
Forwards LER 80-011/03L-0
ML18082A867
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/08/1980
From: Librizzi F
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18082A868 List:
References
NUDOCS 8008130497
Download: ML18082A867 (2)


LER-1980-011, Forwards LER 80-011/03L-0
Event date:
Report date:
3111980011R00 - NRC Website

text

,

Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /430-7000 Mr. Boyce H. Grier Director of USNRC August 8, 1980 Off ice of Inspection and Enforcement Region 1 631 Park Avenue*

King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURP.ENCE 80-ll/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 80-ll/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

? f J,J..,DA?,°/(JJl!J F. P. ::&e General Manager -

Electric Production CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program* Control

( 3 copies)

~ -----~---;-

' 8 0 0 ~ 1 3 0 '~" 1 --._-

~~~~~~~~~~~

95*2001 (200Ml 2-78

Report Number:

80-ll/03L Report Date:

8/8/80 Occurrence Date:

7/10/80 Facility:

Salem Generating Station - Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCTTRRENCE:

Vital Bus Undervoltage Relay Out of Specification CONDITIONS PRIOR TO..OCCURRENCE:

Mode 3 Prior to Initial Criticality DESCRIPTION OF* OCCURRENCE:

During performance of a routine surveillance, it was determined that the 2c;: vi.tal bus undervol tage trip relay was set at 76. 9 vol ts instead of 77.3 volts as specified.

Action Statement 3.3.2.l(a) was entered at 1115 hours0.0129 days <br />0.31 hours <br />0.00184 weeks <br />4.242575e-4 months <br />.

The channel was declared inoperable and Action 14 was ta.ken until the channel is restored to operable status with the trip

. setpoint adjus:ted consistent with the trip setpoint.

The trip relay was placed in a tripped position within one hour as required.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Change in environmental conditions.

I ANALYSIS OF OCCURRENCE:

The undervoltage relays were set to trip at the required voltage during preparation for operation.

A drastic temperature increase occurred when many pieces of equipment were energized and a plant heatup occurred causing a change in the relay setpoint.

CORRECTIVE ACTION

The undervoltage relay was reset under existing conditions and tested satisfactorily.

The Action Statement was terininated.

The ambient conditions now existing should remain relatively constant and a similar problem should not occur again.

Fl\\ILURE DATA:

Not Applicable Prepared By M. J. Murphy

  1. ()/~-

Manager - Salem'Generating Station SORC Meeting No.

58-80